ML20106E388
| ML20106E388 | |
| Person / Time | |
|---|---|
| Site: | Peach Bottom |
| Issue date: | 09/30/1984 |
| From: | Alden W, Ullrich W PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC |
| To: | NRC OFFICE OF ADMINISTRATION (ADM), NRC OFFICE OF INSPECTION & ENFORCEMENT (IE) |
| References | |
| NUDOCS 8410290201 | |
| Download: ML20106E388 (10) | |
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OPE 2ATING. DATA REPORT 4..
..e DOCKET NO. 50 - 2 77 DATE OCTOBER 15, 1984 COMPLt TED 8Y PHILADELPHIA ELECTRIC COMPANY.
W.M.ALDEN E N GI NE E R -I N-CH A RGE LICENSING SECTION GENERATION DIVISION-NUCLEAR TELEPHONE 12153 841-5022
~GPERATING STATUS
- 1. UNIT NAMER PEACH'3OITOM UNIT 1 NOTE 58 UNIT.2 CONTINUED ITS l
i i
2.' REPOR TING PERIOD: SEPTEMBER, 1964 i
SCHE DULED SHUTDOWN FOR l
l 1
- 3. LICENSE 3 THERMAL POWERIMWilt 3293 1
ITS SIXTH REFUELING AND I
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- 4. NAMEPLATE RATING (GROSS MWEle 1152 i
MAINTEN ANCE OUTAGE.
I l
4
- 5. DESIGN ELECTRTCAL RATING INET PWElt 1065 I
i 1
1
- 6. MAXIMUM DEPENDABLE 'C APACITY IGR055 MWEls 1098 l
l I
l
- 7. M4x! MUM DEPENDA8LE CAPACITY (NET MWEls 1051 l
l
- 8. IF CHANGES OCCUR IN CAPACITY R ATIN(.5 (ITEMS NUMBER 3 THROUG,4 71 SINCE LAST REPORT, GIVE RE A50N52
- 9. POWER LEVEL TO WHICH RESTRICTED, IF ANY 'tNET MhEls
- 10. RE ASONS FOR RESTRICTIONS, IF ANY:
THIS MONTH YR-TO-DATE CUMULATIVE
- 11. HOURS IN REPORTING PERIOD 720 6,575 89.783
- 12. NUMBE R OF HOUR 5 REACTOR WAS CRITICAL h
2,584.7 62,283.6
- 13. REACTOR RE5ERVE SHUT 00WN HOURS 0.0 0.0 0.0
- 14. HOURS GENERATOR ON-LINE 0.0 2,544.8 60,556
- 15. UNIT RESERVE SHUTCOWN HOURS 0.0 0.0 0.0 16 GROS 5 THERMAL ENERGY GENERATED (MWil 0
7,869,391 1T8,420,001
- 17. GR355 ELECTRICAL ENERGY GENERAIED (MWHI O
2,547,570 58,718,660
-3,910 2,438,271 56,274.701
- 20. UNIT AVAIL ABILITY F ACTOR 0.0 38 67.4
- 23. UNIT FORCED OUTAGE RATE 0.0 4.4 12.5 I
- 24. SHUTDOWNS SCHEDULED OVER NEXT 16 MONTHS ITYPE, DATE, AND DURATICN OF EACHit SCHEDULED SHUTDOWN FOA REFUE L(NG AND M AINTEN ANC E, STARTED 4/27/f4
- 25. IF 5HUTDOWN AT END OF REPOR T PE A !OO, ESTIMATED DATE OF STARTUPt 02/15/85
- 26. UNIIS IN TEST STATUS (PR101 TO CLMMERCI AL OPER AT10 Nil FORECAST ACHIEVED INITI AL CRITICALI TY INITIAL ELECTRICITY COMMERCIAL OPERATION
- - NEG ATIVE VALUE REPORIED FOR CONSISTENCY WITH FEDERAL ENERGY REGULATORv COMMISSION REPORTS.
N 8410290201 840930 DR ADOCK 0500027]
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OPERATIN3 DAT A REPORT ;
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DOCKET NO. 50 - 278 DATE OCTOBER 15, 1984 i
COMPLETED BY PHILADELPHIA ELECTRIC COMP ANY t
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W.M. AL DE N ENGINEER-IN-CHARGE' LICENSING SECTION GENERATION DIVISION + NUCLEAR TELEPHONE 1215) 841-5022 OPERATING STATUS
- 1. UNIT NAME: PEACH SDTTOM UNIT 3 i NOTES: UNIT 3 EXPERIENCED ONE LOAD l
l l
- 2. REPORTING PTRIODs SEPTEMBER, 1984 i
REDUCTION TO ACCOMODATE A l
I l
- 3. LICENSED THERMAL POWER (MWT):
3293 i
CONTROL ROD PATTERN I
i 1
- 4. NAMEPLATE RATING (GROSS MWEls 1852 l
ADJUSTMENT AND MAINTEN ANCE OF l l
1
- 5. DESIGN ELECTRICAL RATING (NET MWE):
1065 1
CIRCULATING WATER SCREENS, l
I 1
- 6. max! MUM DEPENDABLE C AP ACITY (GROSS MWE): 1098 l
.AND A CONDENSATE PUMP.
I 1
1
- 7. MAXIMUM DEPENDABLE CAPACITY (NET MWEle 1035 l
l
- 8. IF' CHANGES OCCUR IN CAPACITY R ATINGS (ITEMS NUMSER 3 THROUGH 71 SINCE LAST REPORT, GIVE RE ASONSI
- 9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWEle
[
- 10. REASONS FOR RESTRICTIONS. IF ANY:
l THIS MONTH YR-TO-DATE CUMULATIVE
' 11. HOURS IN REPORTING PERIOD 720 6,575 85.679
- 13. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 00
- 14. HOURS GENERATOR ON-LINE 720.0 5,614.4 60,930.6
- 15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0 l
- 16. GROSS THERMAL ENERGY GENERATED (MWH) 2,251 536 17,794,023 178,832,328 l
- 17. GROSS ELECTRICAL ENERGY GENERATED (MWHI 765,220 5,939,240 58,754.360
- 18. NET ELECTRICAL ENERGY GENERATED (MWH) 741,237 5.749.548 56,413,333
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- 19. UNIT SERVICE F ACfDR 100.0 85.4 71.1
- 20. UNIT AVAIL ABILITY F ACTDR 100.0 85.4 71.1 3
- 21. UNIT C APACITY F ACTOR (USING MDC NET) 99.5 84.5 63.6 i
- 22. UNIT CAP ACITY F ACTOR (USING DER NET)
~+ 96.7 82.1
-- 61.8
- 23. UNIT FORCED Duf AGE R ATE 0.0 11 7 7.7
- 24. CHUTDOWNS $CHEDULED DVER NEXT e HONTHS (TYPE, DATE, AND DURATION OF EACH)2 i
n
- 25. s F SHUTDOWN AT END OF REPORT' PERIOD, ESTIMATED DATE OF STARTUP
- 26. UNITS IN TEST STATUS (PRIOR TO COMMERCI AL OPERATIONis FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY CCMMERCIAL OPERATION l
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UNIT SHUTDOWNS AND POWER REDUCTIONS
. DOCKET NO. 50 - 277 n-UNIT NAME PEACH 80TTbH UNIT 7 DATE OCTOBER 15, 19849; s
REPORT MONTH SEPTEMBER, 1984 COMPLETEDBYPHILADELPHIAELECTU Am W.M.ALDEN ENGINEE R-IN-CH ARGE
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LICENSING SECTION GENERATION DIVISION-TECED10NE I2153 841-5022
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1 METHOD OF l LICENSEE ISYSTEMICOMPONENTI CAUSE AND CORRECTIVE l
I TYPE l DUR A TION I RE A SON I S HJTTI NG DOWN 1 EVENT l CODE l CODE I ACTION TO 01 DATE l (11l (HOURSil (21 1 REACTOR y 1 l, R L:POR T.].- l (4) 1 (5) l PREVENT RECURRENCE 1
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- FORC EO REASON IMETHOD EXHIBIT G - INSTRUCTIl t
- SCHE DULED A - EQUIPMENT F AILURE ( EXPL AlfJ)
II - MANUAL FOR PREPARATION OF DA' B - MAINTENANCE OR TEST 2 - M ANU A L SC RA M.
ENTRY SHELY3 FOR LICEI C - REFUELING 3 - AUTOMATIC SCR AM.
EVENT REPORT (LERI M.
D -. REGUL ATORY RESTRICT ION 4 - OTHER (E8 PLAIN)
FILE (NUREG-0161)
E - OPERATOR TRAINING + LICENSE EXAMIN ATION
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G,- (IPERATIONAL ERROR (EXPLAIN)
H? fiTHER(EXPLAINI EXHIBIT I - SAME SOURt y
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UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50 - 278 UNIT NAME PEACH BOTTOM UNIT 3 DATE OCTOBER 15, 1984 REPORT MONTH SEPTEMBER, 1984 COMPLETED BY PHILADELPHIA ELECTRIC CI W.M.ALDEN ENGINEER-IN-CHARGE LICENSING SECTION GENERATION DIVISION-NUCl TELEPHONE (215) 841-5022 l
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l METHOD OF l LICENSEE lSYSTEMICOMPONENTl CAUSE AND CORRECTIVE lTYPElDURATIONlREASONISHUTTING DOWN!
EVENT l CODE I CODE I ACTION TO DA TE I (131 (HOUR $11 (2) l REACTOR (3) l REPORT # 1 (4) l (5) l PREVENT RECURRENCE I
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- 0RCED REASON METHOD EXHIBIT G - INSTRUCTIONS ICHE00 LED A - EQUIPMENT FAILURE (EXPLAIN) 1 - M ANUAL FOR PREPARATION OF DATA B - MAINTENANCE OR TEST 2 - M ANUAL SCRAM.
ENTRY SHEETS FOR LICENSEI C - REFUELING 3 - AUTOMATIC SCRAM.
EVENT REPORT (LERI D - REGULATORY RESTRICTION 4 - OTHER (EXPLAIN)
FILE INUREG-01611 I
E - OPERATOR TRAINING + LICENSE EXAMINATION F - ADMINISTRATIVE 15)
G - OPERATIONAL ERROR (EXPLAIN)
H - OTHiiR(EXPLAIN)
EXHIBIT I - SAME SOURCE O
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y AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50 - 277
==-
UNIT PEACH BOTTOM UNIT 2 DATE OCTOBER 15, 1964 COMPANY PHILADELPHI A ELECTRIC COMPANY W.M.ALDEN ENGINEER-IN-CHARGE-LICENSING SECTION GENERATION DIVISION-NUCLEAR TELEPHONE (215) 841-5022 MONTH SEPTEMBER 1984 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL
{
(MWE-NET)
(MWE-NET) 1 0
17 0
2 0
18 0
3 0
19 0
4 0
20 0
5 0
21 0
6 0
22 0
7 0
23 0
8 0
24 0
6 9
0 25 l
0 10 0
26 0
11 0
27 0
2 12 0
28 0
13 0
29 0
14 0
30 0
15 0
16 0
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AVERAGE DAILY ' tNIT POWER LEVEL DCCKET NO. 50 - 278 UNIT PEACH BOTTOM UNIT 3 DATE OCTOBER 15, 1984 COMPANY PHILADELPHIA ELECTRIC COMPANY W.M.ALDEN ENGINEER-IN-CHARGE LICENSING SECTION GENERATION DIVISION-NUCLEAR TELEPHONE I215) 841-5022 e
MONTH SEPTEM8ER 1984 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWE-NET)
(MWE-NETI 1
1032 17 1055 2
1057 18 1055 3
1057 19 1059 4
1024 20 1056 5
1028 21 1048 6
1058 22 1048 7
1064 23 1043 8
1064 24 1042 1
9 1057 25 i
1044 i
10 1058 26 1043
]
11 1059 27 1045 12 1058 28 1011 13 1058 29 666 14 1054 30 834 15 1053
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16 1055 4
m
-s Docket No. 50-277 Attachmant to Monthly Operating Report for September, 1984 REFUELING INFORMATION 1.
Name of facility:
l-Peach Bottom Unit 2 a
2.
Scheduled date for next refueling shutdown:
April 27, 1984 a.
doneauled date for restart following refueling:
February 15, 1985 4.
Will refueling or resumption of operation thereafter require a technical specification change or other license amendment?
Yes If answer is yes, what,-in general, will these be?
Technical Specifications to accommodate reload fuel.
Modifications to reactor core operating limits.
Technical specification changes associated with snubber reduction program.
5.
Scheduled date(s) for submitting proposed licensing action and supporting information:
Reload 6 license amendment application submitted September 7, 1984.
6.
Important licensing considerations associated with refueling, e.g.,
new or different fuel design or supplier, unreviewed design i
l or performance analysis methods, significant changes in fuel design, new operating procedures:
None expected.
7.
The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool:
(a)
Core
-764 Fuel Assemblies (b)
Fuel Pool - 1170 Fuel Assemblies, 58 Fuel Rods 8.
The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies:
r The spent fuel pool storage capacity has been relicensed for 2816 fuel assemblies.
9.
The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity.
September, 1990 (March, 1986, with reserve full core discharge)
L
Docket No. 50-278 Attcchm2nt to Monthly Operating Report for September, 1984 REFUELING INFORMATION 1.
Name of facility:
Peach Bottom Unit 3 7
2.
Scheduled date for next refueling shutdown:
March 30, 1985.
3.-
Scheduled date for restart following refueling:
June 8, 1985.
4.
Will refueling or resumption of operation thereafter require a technical specification change or other license amendment?
Yes.
If answer is yes, what, in general, will these be?
Technical Specifications to accommodate reload fuel.
Modifications to reactor core operating limits.
Technical specification changes associated with snubber reduction program.
5.
Scheduled date(s) for submitting proposed licensing action and supporting information:
March 1, 1985 for reload fuel 6.
Important licensing considerations associated with refueling, e.g.,
new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures:
None expected.
7.
The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool:
(a)
Core - 764 Fuel Assemblies (b)
Fuel Pool - 1212 Fuel Assemblies, 6 Fuel Rods l
8.
The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies:
The spent fuel pool storage capacity has been relicensed for 2816 fuel assemblies.
9.
The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity.
September, 1991 (March, 1987, with reserve for I
full core discharge)
3 Docket'Nos. 502277/50-278 4
a s v.*
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-Attachm nt-to Monthly.
Operating Raport for September, 1984 Peach Bottom' Atomic. Power Station i
Narrative Summary of Operating Experiences September, 1984
-UNIT'2
-H Unit.2's Refueling / Pipe Replacement outage continued throughout
~
- the month of. September. -control blade relocation and replacement, removal ~of the jet pump nozzle plugs, and radiography on the Recirculation N-2 nozzles have been completed.
LThe "A"iand "B" Recirculation suction and discharge valves have been disassembled.and removed from the drywell, and-temporary
= reactor water cleanup pumps have been installed in-the reactor vessel.
Local Power Range Monitor detectors, Source Range-Monitor / Intermediate Range Monitor drytube replacement, and Condenser tube. cleaning are in-progress.
Removal ~of Recirculation and Residual Heat Removal pipe continues.
i UNIT 3 l
The unit-began the. month at_ full power.
On September 1, power was reduced in order to regenerate two condensate filter I
demineralizers and the unit was returned to full power the next day.
A diesel generator output circuit breaker failed to close during a diesel generator surveillance test on September 4.
After inspection,-the circuit breaker was racked in and tested satisfactorily.
The Recombiner jet compressor steam pressure controller failed the same day causing recombiner process flow to oscillate.
Load was reduced to maintain condenser vacuum, and s
.the controller was placed in manual mode.
Full power was attained the next day.
On September 6, a Primary Containment Isolation System initiation relay was discovered to have failed 'in the non-conservative condition.
The relay was replaced and all other normally energized safety-related relays were inspected.
On September 12, a controlled shutdown was initiated when secondary containment tested unsatisfactorily following~the discovery of a collapsed Standby Gas Treatment System (SGTS) duct.
The unit was returned i
to full power after adjustments were made to the SGTS fan vortex dampers.
On September 21, the High Pressure Coolant Injection l
System was declared inoperable when a turbine exhaust rupture
. disk' failed.
Following repairs, the system was tested 7
satisfactorily'and returned to service the same day.
3 i-Load was. reduced on September 29 to 650 MWe for a control rod pattern adjustment.
The unit ended the month at 950 MWe, ramping back to full power.
I:
'/SLZ
31111;;
PHILADELPHIA ELECTRIC COMPANY 23O1 M ARKET STREET P.O. BOX fi399 PHILADELPHl/i. PA.19101 1215)841 4000 October 15, 19 8 M.
4 Docket Nos. 50-277 50-278 Director Office of Inspection & Enforcement US Nuclear Regulatory Commission Washington, DC 20555 Attention:
Document Control Desk
SUBJECT:
Peach Bottom Atomic Power Station Monthly Operating Report Centlemen:
Attr.ched are twelve copies of the monthly operating report for Peach Bottom Units 2 and 3 for the month of September, 1984 forwarded pursuant to Technical Specification 6.9.1.C under the guidance of Regulatory Guide 10.1, Revision 4.
Ve ru
)yours, J
W.
T. Ullrich Superintendent Nuclear Generation Division Attachment cc:
Dr. T.
E. Murley, NRC Mr. A.
R. Blough, NRC Site Inspector Mr. Stan P.
Mangi, Dept. of Envir. Resources Mr.
P. A.
Ross, NRC INPO Records Center fe %Y
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