ML20105C859

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Special Rept 92-005:on 920818,emergency Diesel Generator 11 Tripped Due to High Vibration Signal During Maint Run. Instructions Will Be Issued to Perform Simulated Diesel Run as post-maint Partial Check of Pneumatic Computer
ML20105C859
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 09/15/1992
From: Cottle W
ENTERGY OPERATIONS, INC.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
92-005, 92-5, GNRO-92-00120, GNRO-92-120, NUDOCS 9209230014
Download: ML20105C859 (2)


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..H September 15, 1992

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U.S.

Nuclear Regulatory Commission Mail Station F1-137 Washington, D.C.

20555 Attention:

Document Control-Dcsk

SUBJECT:

Grand Gulf Nuclear Station Unit 1 Docket No. 50-416 License No. NPF-29 Special Report 92-005 In"alid Failure of Emergency Diesel Generator 11 During Maintenance Run GNRO-92/00120 On August 18, 1992 following a planned outage for Emergency Diesel Generator (EDG) 11, preparations were made to perform a maintenance run in accordance with System Operating Instruction 04-1-01-P75-1.

The run was to verify the correctness of previously performed maintenance.

The EDG was started in accordance with the ' above procedure and achieved rated RPM. However approximately one minute following the start and prior to a load attempt, EDG 11 tripped. It is surmised that the trip was due to a high vibration signal. EDG 11 had been declared inoperable prior to the start attempt. An investigation was performeat to determine the cause of the diesel' failure.

The troubleshooting. activities included simulated diesel runs; however the diesel trip could not be duplicated by the simulations.

All vibration switches were manually tripped and -their reset operation verified. No abnormal conditions were observed during troubleshooting.

Following the investigation, a maintenance run was performed without occurrence. The diesel responded as designed. The EDG was.

loaded to approximately 3 NW and no abnormalities were observed.

The maintenance performed during - the EDG outage required the removal of control air to the EDG' control panel. Removal of the control air de-pressurizes the pneumatic computer and pneumatic control devices.

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l perte$,ber 15, 1992 GNRO-92/00120 Pnge 2 of 3 i

1 The root cause of this event could not be positively identified; however, thu de-prescurization and subsequent re-pressurization of the pneumatic control logic board is suspected to be the underlying cause. This is believed to have caused a failure of a vibration switch to reset.

Instructions will be issued to perform a simulated diesel run as a im s-maintenance partial check of the pneumatic computer / logic-i board an' 3accciated engine vibration trips following de-pressurization of the pneumatic control board.

The occurrence was caused by operation of a Group 2 trip signal.

The only Group 2 trip that is not bypassed during tne emergency operating mode of the EDG is Low Pressure Lube Oil. The Low Pressure Lube oil trip is pressurized through a dif ferent flow path during an emergency condition. Therefore, this condition would not have rendered the EDG incapable of performing its intended safety function.

Therefore this occurrence is considered an invalid failure of the EDG unit.

Yours truly, c O 6~~~ C *c a ~,~.

WTC/RR/

cc:

Mr.

D.

C. Hintz (w/a)

Mr.

R. H. Bernhard (w/a)

Mr.

R.

B. McGehee (w/a)

Mr. N.

S. Reynolds (w/a)

Mr.

H. L. Thomas (w/o)

Mr. Stewart D. Ebneter (w/a)

Regional Administrator U.S.. Nuclear Regulatory Commission Region II 101 Marietta St.,

N.W.,

Suite 2900 Atlanta, Georgia 30323 Mr.

P.

W.

O'Connor Office of Nuclear Reactor Regulation U.S.

Nuclear Regulatory Commission Mail Stop 13H3 Washington, D.C.-20555 SR92005. DOC

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