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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217H5811999-10-15015 October 1999 Forwards 1999 Update to FSAR, for McGuire Nuclear Station.With Instructions,List of Effective Pages for Tables & List of Effective Pages for Figures ML20217G7861999-10-13013 October 1999 Forwards MOR for Sept 1999 & Revised MOR for Aug 1999 for McGuire Nuclear Station,Unit 1 & 2 ML20217F3591999-10-13013 October 1999 Forwards Info Copy of Cycle 14 COLR for McGuire Nuclear Station,Unit 1 ML20217F3261999-10-13013 October 1999 Submits Quantity of Tubes Insp from Either Side of SGs A-D & Lists Tubes with Imperfections,Locations & Size.No Tubes Removed from Svc by Plugging.Total of Eleven Tubing Wear Indications Identified at Secondary Side Supports in SGs ML20217F8011999-10-13013 October 1999 Informs That on 990930,NRC Completed mid-cycle PPR of McGuire Nuclear Station.Areas That Warranted More than Core Insp Program Over Next Five Months,Not Identified.Historical Listing of Plant Issues Encl ML20217J5091999-10-0606 October 1999 Forwards Revs to Section 16.15-4.8.1.1.2.g of McGuire Selected Licensee Commitments Manual.Section Has Been Revised to Allow Testing of Portions of DG Fuel Oil Sys Every 10 Yrs ML20217C8351999-10-0505 October 1999 Communicates Correction to Info Provided During 990917 Meeting with Duke Energy & NRC Region Ii.Occupational Radiation Safety Performance Indicator Values Should Have Been Presented as 1 Instead of 0 ML20217C4471999-10-0404 October 1999 Forwards Insp Repts 50-369/99-06 & 50-370/99-06 on 990801- 0911.Determined That One Violation Occurred & Being Treated as Non-Cited Violation ML20212J2191999-10-0404 October 1999 Informs That Util 980326 Response to GL 97-06, Degradation of SG Internals Provides Reasonable Assurance That Condition of Steam Generator Internals Are in Compliance with Current Licensing Bases for Facility ML20212J7801999-10-0404 October 1999 Discusses GL 98-01 Issued by NRC on 980511 & DPC Responses for McGuire NPP & 990615.Informs That NRC Reviewed Responses & Concluded That All Requested Info Re Y2K Readiness Provided.Subj GL Considers to Be Closed ML20212M1651999-09-23023 September 1999 Refers to 990917 Meeting at Region II Office Re Licensee Presentation of self-assessment of McGuire Nuclear Station Performance.List of Attendees & Licensee Presentation Handouts,Encl ML20212D1671999-09-20020 September 1999 Forwards Exemption & SER from Certain Requirements of 10CFR50,App A,General Design Criterion 57 Re Isolation of Main Steam Branch Lines Penetrating Containment.Exemption Related to Licensee Application ML20212B6491999-09-15015 September 1999 Informs That Encl Announcement Re 990913 Application for Amend to Licenses NPF-9 & NPF-7 Forwarded to C Observer in North Carolina,For Publication ML20212D5321999-09-15015 September 1999 Informs That Duke Energy Corp Agrees to Restrict Max Fuel Rod Average Burnup to 60,000 Mwd/Mtu,In Order to Support NRC Final Approval & Issuance of Requested Amend ML20212A4131999-09-14014 September 1999 Informs That TR DPC-NE-2009P Submitted in 990817 Affidavit, Marked Proprietary,Will Be Withheld from Public Disclosure, Pursuant to 10CFR2.709(b) & Section 103(b) of Atomic Energy Act of 1954,as Amended ML20216E8791999-09-14014 September 1999 Forwards Monthly Operating Repts for Aug 1999 & Revised Monthly Operating Rept for July 1999 for McGuire Nuclear Station ML20212A0501999-09-10010 September 1999 Informs That Postponing Implementation of New Conditions Improved by RG 1.147,rev 12,acceptable Since Evaluation on Relief Based on Implementing Code Case for Duration of Insp Interval ML20212A2631999-09-0909 September 1999 Forwards Rev 25 to McGuire Nuclear Station,Units 1 & 2 Pump & Valve Inservice Testing Program, IAW 10CFR50.55a. Section 8.0 Contains Summary of Changes & Detailed Description of Changes Associated with Rev 25 ML20212A5191999-09-0808 September 1999 Requests NRC Approval for Relief from Requirements of ASME Boiler & Pressure Vessel Code,Section XI,1989 Edition,App VI,VI-2430(c) & 2440(b).Approval of 99-GO-002 Is Requested by 000301 ML20211J3671999-08-31031 August 1999 Forwards Public Notice of Application for Amend to License NPF-9 Seeking one-time Extension of Surveillance Frequency for TS SR 3.1.4.2 Beyond 25% Extension Allowed by TS SR 3.0.2 ML20211M4451999-08-30030 August 1999 Forwards Summary of Util Conclusions Re Outstanding Compliance Issue Re Staff Interpretation of TS SR 3.0.1,per Insp Repts 50-369/99-03 & 50-370/99-03,as Discussed with NRC During 990618 Meeting ML20211H1741999-08-30030 August 1999 Forwards Comments on Catawba Nuclear Station Units 1 & 2 & McGuire Nuclear Station,Units 1 & 2 Specific Reactor Vessel Info Contained in Rvid.Ltr Dtd 990107,rept ATI-98-012-T005 & Partial marked-up Rept WCAP-14995 Encl ML20211K8831999-08-26026 August 1999 Forwards Insp Repts 50-369/99-05 & 50-370/99-05 on 990620-0731.Two Violations Occurred & Being Treated as NCVs ML20211G5181999-08-24024 August 1999 Forwards SE Re second-10-yr Interval Inservice Insp Program Plan Request for Relief 98-004 for Plant,Unit 1 ML20211F2971999-08-17017 August 1999 Forwards non-proprietary & Proprietary Updated Pages for DPC-NE-2009,submitted 980722.Pages Modify Fuel Design & thermal-hydraulic Analysis Sections of DPC-NE-2009. Proprietary Page 2-4 Withheld,Per 10CFR2.790 ML20211B1121999-08-16016 August 1999 Forwards Topical Rept DPC-NE-2012, Dynamic Rod Worth Measurement Using Casmo/Simulate, Describing Results of Six Drwm Benchmark Cycles at Catawba & McGuire & Discusses Qualification to Use Drwm at Catawba & McGuire ML20210V0171999-08-13013 August 1999 Confirms Conversation Between M Cash & M Franovich on 990806 Re Mgt Meeting,Scheduled for 990917 to Present self- Assessment of Plant Performance.Meeting Will Be Held in Atlanta,Ga ML20210S2231999-08-12012 August 1999 Forwards Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2.Revised Rept for June 1999,encl ML20210T4511999-08-10010 August 1999 Forwards Response to NRC RAI Re 981014 Standby Nuclear Svc Water Pond Dam Audit Conducted by FERC ML20210R4311999-08-10010 August 1999 Forwards Summary Rept of Mods,Minor Mods,Procedure Changes & Other Misc Changes Per 10CFR0.59 ML20210R0031999-08-10010 August 1999 Forwards Revised TS Bases Pages to NRC for Info & Use. Editorial Changes Were Made to Correct Incorrect UFSAR Ref Number Associated with Certain Reactor Coolant Sys Pressure Isolation Valves ML20210Q3701999-08-0505 August 1999 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 991006.Authorized Representative of Facility Must Submit Ltr as Listed,Thirty Days Before Exam Date in Order to Register Individuals to Take Exam ML20210H7691999-07-21021 July 1999 Submits Summary of 990715 Meeting at Facility Re Presentation of Results of Most Recent Periodic Ppr.List of Meeting Attendees Encl ML20209H1551999-07-14014 July 1999 Forwards Monthly Operating Repts for June 1999 for McGuire Nuclear Station,Units 1 & 2.Revised Rept for May 1999 Also Encl ML20210E1931999-07-13013 July 1999 Forwards Insp Repts 50-369/99-04 & 50-370/99-04 on 990509-0619.Four Violations of NRC Requirements Occurred & Being Treated as Ncv,Consistent with App C of Enforcement Policy NUREG-1431, Forwards SER Agreeing with Util General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation1999-07-0909 July 1999 Forwards SER Agreeing with Util General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20209G5151999-07-0808 July 1999 Forwards Amended Pages to Annual Radioactive Effluent Release Repts, for 1997 & 1998 for McGuire Nuclear Station. Portion of Rept Was Inadvertently Omitted Due to Administrative Error,Which Has Been Corrected ML20196J9001999-07-0606 July 1999 Informs That 990520 Submittal of Rept DPC-NE-3004-PA,Rev 1, Mass & Energy Release & Containment Response Methodology, Marked Proprietary Will Be Withheld Per 10CFR2.790(b)(5) & Section 103(b) of AEA of 1954 ML20196J4381999-06-29029 June 1999 Informs That as Result of Staff Review of Util Responses to GL 92-01,rev 1,suppl 1,NRC Revised Info in Rvid & Releasing Rvid Version 2 ML20196G3721999-06-24024 June 1999 Documents Verbal Info Provided to NRR During Conference Call Re Relief Requests 98-002 & 98-003 ML20196G7461999-06-22022 June 1999 Requests Exemption from Requirements of 10CFR54.17(c) That Application for Renewed Operating License Not Be Submitted to NRC Earlier than 20 Yrs Before Expiration of Operating License Currently in Effect ML20195K3601999-06-14014 June 1999 Forwards MORs for May 1999 for McGuire Nuclear Station,Units 1 & 2 & Revised MORs for Apr 1999.Line 6 Max Dependable Capacity (Gross Mwe) on Operating Data Rept Should Be Revised to 1114 from Jan 1998 to Apr 1999 ML20195D5691999-06-0303 June 1999 Submits Ltr to Facilitate Closing of Inspector Follow Up Item 50-369,370/97-15-05,re Revising Site Drawings in UFSAR Into Summary one-line Flow Diagrams,Per NRC 990327 Telcon ML20195F1851999-06-0202 June 1999 Forwards Insp Repts 50-369/99-03 & 50-370/99-03 on 990328- 0508.Two Violations of NRC Requirements Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20195E8771999-06-0202 June 1999 Confirms Telcon with M Cash on 990524 Re Public Meeting for 990715.Purpose of Meeting to Discuss Results of NRC Most Recent PPR ML20207D0521999-05-21021 May 1999 Informs That in Telcon on 990519 Between a Orton & Rf Aiello Arrangements Made for Administration of Initial Written Exam for McGuire Nuclear Station on 990603.Exam Will Be Administered at Catawba Simultaneously with Written Exam ML20196L1791999-05-20020 May 1999 Communicates Util Licensing Position Re Inoperable Snubbers. Licensee Has Determined That Structure of ITS Has Resulted in Certain Confusion Re Treatment of Inoperable Snubbers ML20196L1851999-05-20020 May 1999 Forwards Proprietary & non-proprietary Version of Rev 1 to TR DPC-NE-3004, Mass & Energy Release & Containment Response Methodology, Consisting of Finer Nodalization of Ice Condenser Region.Proprietary Info Withheld ML20206T4481999-05-13013 May 1999 Forwards Rev 3 to Topical Rept DPC-NE-3002-A, UFSAR Chapter 15 Sys Transient Analysis Methodology, IAW Guidance Contained in NUREG-0390 ML20206R0791999-05-13013 May 1999 Forwards Monthly Operating Repts for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 & Revised Monthly Operating Repts for Mar 1999 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217H5811999-10-15015 October 1999 Forwards 1999 Update to FSAR, for McGuire Nuclear Station.With Instructions,List of Effective Pages for Tables & List of Effective Pages for Figures ML20217F3261999-10-13013 October 1999 Submits Quantity of Tubes Insp from Either Side of SGs A-D & Lists Tubes with Imperfections,Locations & Size.No Tubes Removed from Svc by Plugging.Total of Eleven Tubing Wear Indications Identified at Secondary Side Supports in SGs ML20217F3591999-10-13013 October 1999 Forwards Info Copy of Cycle 14 COLR for McGuire Nuclear Station,Unit 1 ML20217G7861999-10-13013 October 1999 Forwards MOR for Sept 1999 & Revised MOR for Aug 1999 for McGuire Nuclear Station,Unit 1 & 2 ML20217J5091999-10-0606 October 1999 Forwards Revs to Section 16.15-4.8.1.1.2.g of McGuire Selected Licensee Commitments Manual.Section Has Been Revised to Allow Testing of Portions of DG Fuel Oil Sys Every 10 Yrs ML20217C8351999-10-0505 October 1999 Communicates Correction to Info Provided During 990917 Meeting with Duke Energy & NRC Region Ii.Occupational Radiation Safety Performance Indicator Values Should Have Been Presented as 1 Instead of 0 ML20212D5321999-09-15015 September 1999 Informs That Duke Energy Corp Agrees to Restrict Max Fuel Rod Average Burnup to 60,000 Mwd/Mtu,In Order to Support NRC Final Approval & Issuance of Requested Amend ML20216E8791999-09-14014 September 1999 Forwards Monthly Operating Repts for Aug 1999 & Revised Monthly Operating Rept for July 1999 for McGuire Nuclear Station ML20212A2631999-09-0909 September 1999 Forwards Rev 25 to McGuire Nuclear Station,Units 1 & 2 Pump & Valve Inservice Testing Program, IAW 10CFR50.55a. Section 8.0 Contains Summary of Changes & Detailed Description of Changes Associated with Rev 25 ML20212A5191999-09-0808 September 1999 Requests NRC Approval for Relief from Requirements of ASME Boiler & Pressure Vessel Code,Section XI,1989 Edition,App VI,VI-2430(c) & 2440(b).Approval of 99-GO-002 Is Requested by 000301 ML20211M4451999-08-30030 August 1999 Forwards Summary of Util Conclusions Re Outstanding Compliance Issue Re Staff Interpretation of TS SR 3.0.1,per Insp Repts 50-369/99-03 & 50-370/99-03,as Discussed with NRC During 990618 Meeting ML20211H1741999-08-30030 August 1999 Forwards Comments on Catawba Nuclear Station Units 1 & 2 & McGuire Nuclear Station,Units 1 & 2 Specific Reactor Vessel Info Contained in Rvid.Ltr Dtd 990107,rept ATI-98-012-T005 & Partial marked-up Rept WCAP-14995 Encl ML20211F2971999-08-17017 August 1999 Forwards non-proprietary & Proprietary Updated Pages for DPC-NE-2009,submitted 980722.Pages Modify Fuel Design & thermal-hydraulic Analysis Sections of DPC-NE-2009. Proprietary Page 2-4 Withheld,Per 10CFR2.790 ML20211B1121999-08-16016 August 1999 Forwards Topical Rept DPC-NE-2012, Dynamic Rod Worth Measurement Using Casmo/Simulate, Describing Results of Six Drwm Benchmark Cycles at Catawba & McGuire & Discusses Qualification to Use Drwm at Catawba & McGuire ML20210S2231999-08-12012 August 1999 Forwards Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2.Revised Rept for June 1999,encl ML20210T4511999-08-10010 August 1999 Forwards Response to NRC RAI Re 981014 Standby Nuclear Svc Water Pond Dam Audit Conducted by FERC ML20210R0031999-08-10010 August 1999 Forwards Revised TS Bases Pages to NRC for Info & Use. Editorial Changes Were Made to Correct Incorrect UFSAR Ref Number Associated with Certain Reactor Coolant Sys Pressure Isolation Valves ML20210R4311999-08-10010 August 1999 Forwards Summary Rept of Mods,Minor Mods,Procedure Changes & Other Misc Changes Per 10CFR0.59 ML20209H1551999-07-14014 July 1999 Forwards Monthly Operating Repts for June 1999 for McGuire Nuclear Station,Units 1 & 2.Revised Rept for May 1999 Also Encl ML20209G5151999-07-0808 July 1999 Forwards Amended Pages to Annual Radioactive Effluent Release Repts, for 1997 & 1998 for McGuire Nuclear Station. Portion of Rept Was Inadvertently Omitted Due to Administrative Error,Which Has Been Corrected ML20196G3721999-06-24024 June 1999 Documents Verbal Info Provided to NRR During Conference Call Re Relief Requests 98-002 & 98-003 ML20196G7461999-06-22022 June 1999 Requests Exemption from Requirements of 10CFR54.17(c) That Application for Renewed Operating License Not Be Submitted to NRC Earlier than 20 Yrs Before Expiration of Operating License Currently in Effect ML20195K3601999-06-14014 June 1999 Forwards MORs for May 1999 for McGuire Nuclear Station,Units 1 & 2 & Revised MORs for Apr 1999.Line 6 Max Dependable Capacity (Gross Mwe) on Operating Data Rept Should Be Revised to 1114 from Jan 1998 to Apr 1999 ML20195D5691999-06-0303 June 1999 Submits Ltr to Facilitate Closing of Inspector Follow Up Item 50-369,370/97-15-05,re Revising Site Drawings in UFSAR Into Summary one-line Flow Diagrams,Per NRC 990327 Telcon ML20196L1791999-05-20020 May 1999 Communicates Util Licensing Position Re Inoperable Snubbers. Licensee Has Determined That Structure of ITS Has Resulted in Certain Confusion Re Treatment of Inoperable Snubbers ML20196L1851999-05-20020 May 1999 Forwards Proprietary & non-proprietary Version of Rev 1 to TR DPC-NE-3004, Mass & Energy Release & Containment Response Methodology, Consisting of Finer Nodalization of Ice Condenser Region.Proprietary Info Withheld ML20206R0791999-05-13013 May 1999 Forwards Monthly Operating Repts for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 & Revised Monthly Operating Repts for Mar 1999 ML20206T4481999-05-13013 May 1999 Forwards Rev 3 to Topical Rept DPC-NE-3002-A, UFSAR Chapter 15 Sys Transient Analysis Methodology, IAW Guidance Contained in NUREG-0390 ML20206S9151999-05-11011 May 1999 Forwards Rev 29 to McGuire Nuclear Station Selected Licensee Commitments. Section 16.11-16.2 Has Been Revised to Apply Guidance of NUREG-0133 for Performing Gaseous Effluent Dose Pathway Calculations ML20206K1341999-05-0303 May 1999 Forwards 1999 Interim UFSAR for McGuire Nuclear Station. UFSAR Update Includes Items Relocated During Improved Tech Specs Implementation.Next Regular UFSAR Update as Required 10CFR50.71(e) Is Due in Oct 1999 ML20206F3321999-04-28028 April 1999 Forwards Annual Radioactive Effluent Release Rept for 1998 for McGuire Nuclear Station. Listed Attachments Are Contents of Rept.Revised ODCM Was Submitted to NRC on 990203 ML20206E4101999-04-26026 April 1999 Forwards Four Copies of Rev 9 Todpc Nuclear Security & Contingency Plan,Per 10CFR50.54(p)(2).Changes Do Not Decrease Safeguards Effectiveness of Plan.Encl Withheld,Per 10CFR73.21 ML20206B4791999-04-20020 April 1999 Requests Exemption from GDC 57 Re Reactor Containment - Closed Sys Isolation Valves,As Described in 10CFR,App a for Containment Penetrations M393 & M261.Detailed Technical Evaluation & Justification for Exemption Request,Encl ML20205S9731999-04-19019 April 1999 Submits Info Re Quantity of SG Tubes Inspected,Tube Indications of Imperfections & Tubes Removed from Svc by Plugging,Per TS 5.6.8,part B 05000369/LER-1999-001, Forwards LER 99-01(S)-00 Re Contract Employee Submittal of False Info Resulting in Gaining Unescorted Access.No Licensee Planned Corrective Actions or Other Regulatory Commitments Were Identified as Result of Incidence1999-04-16016 April 1999 Forwards LER 99-01(S)-00 Re Contract Employee Submittal of False Info Resulting in Gaining Unescorted Access.No Licensee Planned Corrective Actions or Other Regulatory Commitments Were Identified as Result of Incidence ML20205P8891999-04-13013 April 1999 Forwards Monthly Operating Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2.Revised Rept for Feb 1999 Encl ML20206K3561999-04-13013 April 1999 Forwards Revised McGuire Nuclear Station Selected Licensee Commitments (SLC) Manual. Significant Changes Are Marked by Vertical Bars on Right Margin ML20205K5131999-04-0707 April 1999 Forwards Complete Response to NRC 981209 & 990105 RAIs on Question 11 Re LARs for McGuire & Catawba Nuclear Stations. Addl Info Received from W & Contained in Encl W ML20205B6011999-03-23023 March 1999 Requests That NRC Place Technical Interface Agreement 97-02 Re URI 96-11-03,raising Operability & Design Criteria Conformance Issues Re Hydraulic Snubbers Installed at Plant & NRR Response on Dockets to Provide Record of Issue ML20205C4611999-03-23023 March 1999 Submits Correction to Violation Against 10CFR50 App B, Criterion VII, Control of Purchased Matl,Equipment & Svcs, Issued to McGuire Nuclear Station on 980807 ML20205B6161999-03-23023 March 1999 Provides Addl Info & Correction to Typo in Re License Bases Record Change Re License Amend Submittals ,approved as FOL NPF-9 & NPF-17,amends 184 & 166, respectively.Marked-up TS Pages,Encl ML20204J0051999-03-19019 March 1999 Forwards Response to 990127 & 28 RAIs Re GL 96-05 for Catawba & McGuire Nuclear Stations ML20204E1791999-03-18018 March 1999 Reflects 990318 Telcon Re License Bases Record Change for License Amend Submittals ,approved as Amends 184 & 166,respectively for Licenses NPF-9 & NPF-17.TS Pages Encl ML20204C8821999-03-15015 March 1999 Forwards Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2.Revised Rept for Jan 1999 Encl ML20207C2071999-02-25025 February 1999 Informs of Revised Expected Submittal Date of Proposed License Amend Presented at 990127 Meeting Re Soluble Boron & Boraflex.Util Plans to Submit Proposed License Amend in First Quarter of 1999 ML20207C7691999-02-22022 February 1999 Forwards Annual Occupational Radiation Exposure Rept for 1998. Rept Provides Tabulation of Number of Station,Utility & Other Personnel Receiving Exposure Greater than 100mRem/yr Followed by Total Dose for Each Respective Worker ML20207C6851999-02-22022 February 1999 Forwards Revised TS Bases Pages,Reflecting Removal of SI Signal on Low Steamline Pressure on Page B 3.3.2-16 & Adding Clarification for Increasing Hydrogen Recombiner Power During Testing on Page B 3.6.7-4 ML20206S3341999-01-28028 January 1999 Forwards Proprietary & non-proprietary Responses to NRC 981209 & 990105 RAIs Re Util Lars,Permitting Use of W Fuel at McGuire & Catawba Stations.Proprietary Info Withheld,Per 10CFR2.790 ML20199E0081999-01-12012 January 1999 Forwards MOR for Dec 1998 & Revised MOR for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 ML20199C9861999-01-0707 January 1999 Forwards Annual Lake Norman Environ Summary Rept for 1997,as Required by NPDES Permit NC0024392,including Detailed Results & Data Comparable to That of Previous Years.With Corrected Pages 3 & 19 to 1994-95 Lake Norman Creel Rept 1999-09-09
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.. Duke her Company T C Af,wt m v kicGmer Nuclear Centratwn Department nce President
. 12700 flagers ferry Road (%IGCIA) (704)8754800 llantersatir, M'lMib Hb5 (704)875 4M9 TAM DUlW POWER June 17, 1992 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555
Subject:
McGuire Nuclear Station Docket Nos. 50-369, -370 Inspection Report No. 50-369, -370/92-08 Gentlemen:
Please find attached Duke Power Company's revised response to Violation 369/92-08-01 and 369, 370/92-08 for McGuire Nuclear Station as c9ferenced in your June 4, 1992 letter. The revised response to the violations gives completion dates for the corrective actions to be taken.
Should there be any questions concerning this matter, contact Larry Kunka at (704) 875-4032.
Very truly yo rs, T.f@McMeekin C.
HL Attachment xc: Mr. S. D.-Ebneter Administrator, Region II e U.S. Nuclear Regulatory Commission 101 Marietta St., NW, suite 2900 Atlanta, GA 30323 3
Mr. E m Reed U.S. Nuclear Regulatorg fe, mission Office of Nuclear Reactor negulation Washington, D.C. 20555 f
9206260243 920617 -
h PDR G
ADOCK 05000369 PDR 6U( l l >
. t'/ -l a w w w m,,a 1
. Document Control Dorsk
- Page 3 i . June 17, 1992
'l McGUIRE NUCLEAR STATION a
RESPONSE TO VIOLATION 369/92-08-01 VIOLATION 369/92-08-01 10 CFR 50 Appendix B Criterion XVI and the licensee's accepted Quality Ascureince Program (Duke-1-A) Section 17.2.16 collectively require that measures be established to assure that conditions adverse to quality are promptly identified and corrected.
Contrary to the above, although measures were established, they were not effectively implemented. On February 26, 1992, while conducting daily rounds, a non licensed operator reported to the Unit Supervisor that the-1A diesel generator fuel oil tank level was low. This condition was not corrected until February 28, 1992. During this time, the 1A diesel generator fuel oil tank level was 38,000 gallons which was below the 39,500 gallon minimum level required by Technical Specification 3.8.1.1 This is a Severity Level IV (Supplement I) violation and applies to Unit 1 only.
THE REASON FOR THE VIOLATION On February 26, 1992, during sampling of the Unit _1 Fuel- Oil Storage Tanks (FOST's), Chemistry technicians inadvertently left two valves on the-recirculation pump suction of the-1A FOST open while recirculating the 1B.FOST. Therefore, during the four hour recirculation period for the IB FOST, the recirculation pump was taking suction on both 1A and 1B FOST but was discharging only to the IB FOST. This caused the level in the 1A FOST to be lowered '
below the Technical Specification (TS) limit.
Later that evening, an Operations '(OPS) non-licensed operator (NLO) was performing the first night shift inspection of the Service Building and Outside. Equip t per OMP 2-8. He observed the 1A FOST level was 38,000 gar ons and noted this value in the appropriate-block on Attachment 3 of OMP 2-8. The rounds standard _,
instructions in OMP 2-8 specifies for any out of. normal value or l value parameter that is noted on the enclosure, the person perf orming the: rounds inspection shall write "E1" in the parameter space along with the parameter _value. The required value listed on the rounds sheet was " greater than 40,000 " gallons. The NLO.did l
Document Control Desk Page 4 June 17, 1992 not flag the out of normal value. The NLO did inform the Assistant Shift Supervisor of the 1A FOST level. The assistant shift Supervisor acknowledged the level and stated he would look into it.
He believed the level was within the TS limits, when the TS limit is actually 39,500 gallons. Another Senior Reactor Operator (SRO) was given the rounds sheets to review. The normal practice for SRO review of rounds sheets is to focus primarily on values that are flagged as out of normal. Since the NLO had not flagged the FOST value as out of normal, the low value was not detected during the SRO's review and no action was taken.
The next day, an NLO on the day shift noted the value of the 1A FOST as 37,500 gallons, but again due to attention to detail, the value was not noted as out of normal and the subsequent SRO review did not detect the low value. Therefore, once :# gain no action was taken to increase the low level in the 1A FOST.
When the night shift returned, the NLO recorded 37,500 gallons in the 1A FOST. Since he had informed the Assistant Shift Supervisor of the low level on the previous shift, he saw no reason for concern and once again did not flag the value as out of normal.
When the SRO reviewed the rounds sheets, once again the low value .
was not detected and no action was taken to raise the level in the 1A FOST.
During the day shift on February 38, the NLO assigned to perform the rounds noted 37,500 gallons as the 1A FOST level but again the value was not flagged as out of normal. The rounds sheets were given for review to a shift supervisor who had not performed this review recently and was not as familiar with the rounds sheet review. Therefore, he was very thorough in looking at the data..
During this review the Shift Supervisor realized that the 1A FOST was outside of TS limits and actions were taken to increase the level to within TS limits.
Therefore, the low level on the 1A FOST was not immediately corrected due to inattention to detail by various OPS personnel while performing and reviewing the rounds sheets.
THE CORRECTIVE STEPS TAKEN AND RESULTS ACHIEVED
- 1. IA FOST valves were closed and locked by Chemistry personnel.
- 2. OPS personnel returned 5,000 gallons of fuel oil from 1B FOST to 1 A FOST which raised the 1 A FOST level above the TS limit.
THE CORRECTIVE STEPS THAT WILL BE TAKEN TO AVOID FURTHER VIOLATIONS
Document Control Desk 2 Pagn 5 June 17, 1992
- 1. OPS management personnel will evaluato the current NLO rounds turnover policy and initiato changes to the policy as necessary.
- 2. The importanco of N!.O rounds shoots, managemont's expectations of how to complete rounds shoots, propor rounds turnover, and proper rounds techniques will be re-emphasized in NLO training.
- 3. OPS personnel will revise rounds shoots to highlight TS related items.
- 4. OPS personnel will evaluate how out. of normal values are flagged on rounds sheets and make changes as necessary.
- 5. OPS manac 2 uent, will devise an Equipment Training and Qualification Standard (ETQS) that incorporates having an OPS supervisor accompany each NLO and Reactor Operator during rounds activities at least once every two years.
DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED McGuire will be in full compliance September 25, 1992.
b Document Control Desk I Paqq 6 Jur e 17 1992 McGUIRE NUCLEAR STATION RESPONSE TO VIOLATION 369, 370/92-08-03 h ,
,h O v. N1' ION 36 9, 370/92-08-03 Technical Specification 6.8.1 requires that written procedures 7 .q 'e established, implemented, and maintained covering the oplicable procedures recommended in Appendix '. of Regul6 tory
'% 1.33, Revision 2, February, 1978, whjo includes the
., , tion of safety related systems, maintain,ig containment
};( o m
.urity, and performing surveillance tests on safety related
> ment.
k
- 7trary to the above, procedures were not u.f quately
lemented to maintain configuration control as evidenced by following examples:
- 1. On At: gust 12, 1991, the licensee discovered valves 1SA-40 i and 1SA-39, the above and below seat drains for the auxiliary feedwater turbine stop valve, open. Licensee procec.ure , OP/1/A/6250/02, Auxiliary Feedwater System, requires that these valves be closed.
- 2. On September 30, 1993, the licensee discovered valve 1RN-951, Containment Spray (MS) System Pump 1A Air Handling A Unit Outlet Control, in the Nuclear Service Water syst am shut THs resulted in the "A" train of NS being i nt g u for an indeterminate period of time. During the pnj o<i when the systm was inoperable, the unit was in a refueling outage when NS was not required to be operrble. This valve is required to be maintained in a partially open configurar.lon by procedure OP/1/A/6100/22, Unit 1 Data Book.
- 3. On February 28, 1992, the licensee discovered that the suction valves to the recirculation lines between the 1A and 1B diesel generator fuel oil ,torage tanks were left open. Licensee procedure CP/1/A/8600/411, C1'emistry Procedure for Sampling of Oils in Unit i, requires that the valves be closed following the comple* ton of f uel oil s recirculation which was performed on Fr vuary 2F, 1992.
- 4. On January 30, 1992, while attempting to terminate a containment atmosphere sample on Unit 2, the Radiation Protection technicians isolated the EMF supply valve and the EMF sample nlet valves, rendering the EMF's
n Document Control Desk Page 7 June 17, 1992 inoperable for approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />. The valves intended to be isolated were the sample inlet and outAet valves, as required by MP/0/B/1003/39, VQ/VP/Incore Release Procedure. This occurred while the unit was in a refueling outage.
- 5. On April 1, 1992, pret = re transmitter 2NSPT5390 was discovered with its isolation valve closed by Operations personnel.- With the transmitter isolation valve in the closed position, the Containment Pressure Control System (CPCS) for the Containment Air Return Exchange -and Hydrogen Skimmer (VX) system Train 2A is inoperable.
This example was given in Inspection Report 369,370/92-10.
This is a Severity Level IV (Supplement I) violation.
REASON FOR THE VIOLATION The rer. son for each of the five_ examples of configuration control problems will be addressed separately.
- 1. The rounds non licensed operator (NLO) opened the valves as instructed by the rounds sheet. He then went into the RN Pump Strainer Room to continue his rounds with the intention of returning to the pump room to close the valves. This is a common practice. While in the RN Strainer Room, he was distracted by a radio call directing him to ant:her location in the plant. The NLO left to respond to the cell, leaving the valves open. Later he resc ed his round but forgot to reclose the valves.
The NLO was distracted by other activities after opening the valves-but before reclosing them. No guidance was given in the procedure to ensure the operator does not have concurrent duties while cycling these valves. The cause was determined o to be an inadequate procedure that did not specify_the valves should be opened and shut-without concurrent duties and the NLO not having sufficient attention-to detail.
- 2. On September 30, 1991, valve-1RN-951, Containment Gpray (NS)
System Puri4 1A Air Handling Unit Outlet Contrc', was found mispositioned in the closed -position during maintenance activities. The misposition of 1RN-951 5as brought to the attention of Operations Control Room personnci auring ,
discussion of the misposition of valve 1RN-949, Residual Heat r
_ Removal (ND) System Pump 1A- Air Handling Unit Outlet Control, j which was_dl; covered on October 4, 1991. ;
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t i Valve 1RN-951 had been in the incorrect position for an i unknown period of time after September 4, 1991, when ths. air j handling unit had been operated with no abnormal temperatures
! noted. This resulted-in Train IA of the NS system being 3 inoperable for an unknown period between September 4, 1991 and l October 4, 1991. The NS . system had been required to be i operable September 4 through September 21, 1991, until Unit 1 1
entered Mode 5. No definite or probable cause could be found
- for the incorrect positioning of 1RN-951.
, 3. On February 26, 1992, Chemistry technicians were assigned the
! task of obtaining samples from the Unit 1 and 2 Diesel
! Generator (DG) Fuel Oil E%orage TankF (FOST). Prior to l sampling the fuel oil inside cach FOST mu, be recirculated at
- least four hours. The technicians proce%Jod to the-Unit 1 i FOST location, and placed the 1A FOST in recirculation mode. .
F Tht.s required the unlocking and opening of four valves.
t Approximately four hours later, the technicians obtained the j sample from the 1A FOST and placed the 1B FOST in recirculation mode for the required four hours.
1 The technicians did not realize that the two valves for the 1A FOST in the suction header of the recirculation pump were not closed. The procedure being used did not specify an
! individual sign of f for the valve position. Therefore, during i the four hour recirculation period for the 1B FOST, the
! recirculation pump was taking suction on both 1A-and 1B FOST but was discharging only to the 1B FOST. This caused the j level in the 1A FOST to be lowered below the Technical
< Specification limit of 39,500 gallons.
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- 4. On January 30, 1992, 2 EMF. 38, 39, and 40, Containment i Particulate, Gas and Iodine monitor was taken out of service to perform monthly maintenance. Unit 2 Containment Purge (VP) system operation was secured during the maintenance. The-VP system was to be rettarted on _the day shift. Radiation Protection (RP) day shift personnel started a sample at 0800 to measure and accoont for any changes in containment airborne activity levels. Af ter returning to the- RP shift-lab, the personnel realized the VP system had not been restarted-and the sample was not required. At 0907, the VP purge was restarted. At approximately 0930, the RP personnel stopped the sample. At approximately 1130, RP personnel working on the EMF noticed the EMF sample supply valve and the EMF supply valve were both closed.
Both of the RP personnel involved with the securing of the sample believed that thuy were the ones who performed the Independent Verification when the sample' was secured. Neither could remember actually operating the valves but both were
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, Page 9 i June 17, 1992 I confident they had IV'ed the valves. Since neither of the
- individuals could remember operating the valves, they could not have been in the correct position when they were IV'ed.
i The cause of this event is f ailure to follow the procedure for j the EMF Sampling (HP/0/B/1003/39) and inattention to the details of the task at hand.
- 5. On April 1, 1992, Operations (OPS) personnel ruticed the
, handle on the isolation valve for CPCS t ansmitter 2NSPT5390 was not fully extended in the open direction. The OPS personnel attempted to move the transmitter isolation valve in i the closed direction and found the valve closed. With the j transmitter isolation valve in the closed position, the CPCS l
for Containment Air Return Exchange and Hydrogen Skimmer d
system 2A was inoperable. No reason as to how, why or when i the transmitter isolation was closed could be determined.
CORRECTIVE STEPS TAKEN AND RESULTS ACHIEVED i
l For all of the above configuration control events, the appropriate plant personnel were informed and tne mispositioned component was returned to its correct position.
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- Other corrective actions will be listed for the individual events, a
i 1. The rounds sheet has been changed to require the NLO to stand by the valves while they are being cycled.
l 2. A. The remaining Unit 1 ND and NS pump air handling unit i outlet throttle valves were verified by OPS personnel to i be in the correct position.
1 i- B. Performance personnel ensured that the valve stem lock
< nuts were Lightened on_all Unit 1 and 2 throttled RN system flow balance related valves.
i C. OPS personnel revised Station Directive 3.1.5, Activities Af fecting Station Operations or Operating Indications to i add a requirement for station personnel to notify the Control Room SRO if a plant device is found mispositioned j or misaligned.
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} 3. A. Procedures CP/1(2)/8500/41, CHM Procedure for Sampling of Oils on Unit 1 and Unit 2, were revised to require sign l ofts for individual valve alignments. <
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B. Chemistry . (CHM) management personnel discussed this event with the chemistry technicians involved.
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, Document Control Desk j Pag.e 10 1 June 17, 1992 j 4. A. Discussions were held with the two RP specialists d
involved in the event.
B. Discussions were held with all RP shift personnel d
reinforcing the requirements of the RP IV responsibilities covered in RP Manual Section 8.6, the necessity to follow the procedure in the field, and the need to not switch from the performer to the IVer-within the same step of a procedule.
- 5. A. Instrument and electrical (IAE) personnel verified all CPCS transmitter-isolation valves were open'on Units 1 and 2.
B. Isolation valves were verific i positioned properly on-the following system for instruments without continuous indication:
Auxiliary Feedwater Residual Heat Removal Chemical and Volume Control Nuclear Service Water Containment Air Addition and Release Liquid Waste CORRECTIVE STEPS TO BE TAKEN TO AVOID FURTHER VIOLATIONS The corrective steps to be taken will be addressed for each example with generic corrective steps listed at the end.
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- 1. The change to the rounds sheet and the reason for the chcage will be communicated to all rounds NLOs. This will be completed by September 25, 1992.
- 2. Maintenance management will cover- this event with .all maintenance technicians. The Jmportance cf notifying OPS Control Room personnel if' a plant device is found mispositioned or misaligned will be stressed. This will be completed by September 30, 1992.
- 3. A. OPS and CHM personnel will evaluate the interf ace process for operation of plant equipment which is under the dual control-of OPS and. CHM and enhance current practices as appropriate. This action will be completed by July 1, 1992.
Document Control Desk Pag.e 11
,-June 17, 1992 B. Cm:r management will cover this event with appropriate CHM personnel. This action will be completed by July-1, 1992.
C. CUM personnel will review all procedures under their control that are directly involved with state, federal or-NRC regulations and assure that component configuration control is adequately addressed. This action will- be completed by July 1, 1992.
D. CHM personnel will evaluate'the practice of locking _open valves during tank recirculation activities and revise this policy as appropriate. This action will- be completed by July 1, 1992.
E. CHM management will revise the task of obtaining fuel oil samples during routine monthly sampling of FOSTs so thet Train A tanks will be sampled on.a different day than Train B tanks. This action will be completed by-July 1, 1992.
F. Procedures CP/1(2)/A/8600/41 will be revised by CHM staf f to require notification of the duty SRO prior to FOST recirculation and sampling activities. This action will be completed by July 1, 1992.
- 4. A. Procedure HP/0/B/1003/39 will be changed so that only the steps that require IV are identified in bold so they will not be confused with steps that do not require IV. This action will be completed by September 1, 1992.
B. When other shift RP procedures are due for review or are updated, the IV requirements will be reviewed and placed in bold type. This action will be completed by September 1, 1992.
The corrective action to be taken for example 5 will also address the configuration control concerns generically.
- 5. The Component M,ispositioning Working ' Group _ (CMWG) has been-formed to use the Human Performance Enhancement System methodologies to find the . root or probable causes- of the component mispositioning events and _ upon determining the causes, recommend - ef fective means _to prevent recurrence of mispositioning events. The team will be composed of members of the site staff and management representing the principle work groups who position components.
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- The initial recommendations from this working group will be
, made to management by December 31, 1992. Management will then j evaluate the recommendations for implementation.
l Additionally, - since many component mispositionings are cue to
- procedure adherence, the excellence group formed to look at
!- procedure adherence in response to the violation given in Inspection Report 91-22 will also serve to address component l mispositioning.
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j DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED i McGuire will be in full compliance at the indicated date for each
. of the actions above.
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