Similar Documents at Cook |
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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17335A5201999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Dccnp Unit 1.With 990208 Ltr ML17335A5191999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Dccnp,Unit 2.With 990208 Ltr ML17335A4831998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for DC Cook Nuclear Plant,Unit 2.With 990108 Ltr ML17335A4841998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for DC Cook Nuclear Plant,Unit 1.With 990108 Ltr ML17335A3951998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for DC Cook Nuclear Plant,Unit 2.With 981207 Ltr ML17335A3941998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for DC Cook Nuclear Plant,Unit 1.With 981207 Ltr ML17335A3331998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for DC Cook Nuclear Plant,Unit 1.With 981105 Ltr ML17335A3381998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for DC Cook Nuclear Power,Unit 2.With 981105 Ltr ML17335A2931998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for DC Cook Nuclear Plant,Unit 2.With 981005 Ltr ML17335A2941998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for DC Cook Nuclear Plant,Unit 1.With 981005 Ltr ML17335A2131998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DC Cook Nuclear Plant,Unit 2.W/980903 Ltr ML17335A2151998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DC Cook Nuclear Plant,Unit 1.W/980903 Ltr ML17335A1741998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DC Cook Nuclear Plant Unit 2.W/980806 Ltr ML17335A1731998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DC Cook Nuclear Plant Unit 1.W/980806 Ltr ML17334B8171998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DC Cook Nuclear Plant Unit 2.W/980706 Ltr ML17334B8131998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DC Cook Nuclear Station,Unit 1.W/980706 Ltr ML17334A7511998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DC Cook Nuclear Plant,Unit 2.W/980609 ML17334A7521998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DC Cook Nuclear Plant,Unit 1.W/980609 Ltr ML17334B7921998-04-30030 April 1998 Addendum to Monthly Operating Rept for Apr 1998 for DC Cook Nuclear Station,Unit 2 ML17334B7721998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for DC Cook Nuclear Plant,Unit 1.W/980506 Ltr ML17334B7911998-03-31031 March 1998 Addendum to Monthly Operating Rept for Mar 1998 for DC Cook Nuclear Plant,Unit 2 ML17334B7171998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Donald C Cook Nuclear Plant,Unit 1.W/980407 Ltr ML17334B7181998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Donald C Cook Nuclear Plant,Unit 2.W/980407 Ltr ML17334A6831998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Donald C Cook Nuclear Plant,Unit 2.W/980309 Ltr ML17334A6811998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Donald C Cook Nuclear Plant,Unit 1.W/980309 Ltr ML17334B7901998-02-28028 February 1998 Addendum to Monthly Operating Rept for Feb 1998 for DC Cook Nuclear Plant,Unit 2 ML17334A6481998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for DC Cook Nuclear Plant,Unit 2.W/980209 Ltr ML17334B7891998-01-31031 January 1998 Addendum to Monthly Operating Rept for Jan 1998 for DC Cook Nuclear Plant,Unit 2 ML17334A6051997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Donald C Cook Nuclear Plant,Unit 2 ML17334A6021997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Donald C Cook Nuclear Plant,Unit 1.W/980108 Ltr ML17334B6711997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Plant,Unit 2.W/971208 Ltr ML17334A6061997-11-30030 November 1997 Revised Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Station,Unit 2 ML17334B6651997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Plant,Unit 1.W/971208 Ltr ML17333B1421997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Donald C Cook Nuclear Plant,Unit 1.W/971110 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5481999-09-30030 September 1999 Non-proprietary DC Cook Nuclear Plant Units 1 & 2 Mods to Containment Sys W SE (Secl 99-076,Rev 3). ML17335A5451999-09-28028 September 1999 Rev 1 to Containment Sump Level Design Condition & Failure Effects Analysis for Potential Draindown Scenarios. ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1481999-09-17017 September 1999 Independent Review of Control Rod Insertion Following Cold Leg Lbloca,Dc Cook,Units 1 & 2. ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17335A5461999-08-0202 August 1999 Rev 0 to Evaluation of Cook Recirculation Sump Level for Reduced Pump Flow Rates. ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B5671999-03-0202 March 1999 Summary of Unit 1 Steam Generator Layup Chemistry from 980101 to 990218. ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors 1999-09-30
[Table view] |
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.DCC:I No. 50-316 Da.4_- 11/3/84 ..
C .*.* :' - . ., . .v. c1imer T-* r uC~N. 610-4 0 3-3 90
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- 1. Uni:N:==: ~ Donald C. cook" Unit 2 Nor:s ,
. . 2. Repor:i=;?: dad: October 1984
- 3. ' *--- -d Ti-- ' ?swer C.tW::: 3411 ,.
- 4. N ===!:i: ?d.;(Cro:s 5:W:): 1133 .
- 5. Desi;=II::=i=!?d.;(Ne 11We): 1100
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- 6. 3'- " =:= Dry ==d..ht C:p:d:7 (Cicts 31We):
1100 T. Sf:xi== De;=d:-h!: r ---- 7 ry:: 3 we): 1060 3 8,. If Ch=:;:: C:=:in C:Mf R::i=;: (1: =: Ne. ah:: 3 Th::=;h 7) 3;::: I =: R:per:. Cive R:= ens:
i
- 9. Power Leve! To Whid R==i==d. !! Any (N:: 3:W:): * .
- 10. R=:oas Toe ?.. =i:d:=.1f A.w: . .
s
! - T'..is Stand Y:..<o.cas: . ce==!=ive
!!. Ho== != R:ponia; ?:d:d 745 7.320 59,904
- 12. Nu=ht.- Cf Hoc = R==:r W:s Cdd=.1 . 745 4,327.4 42,112.6
'13. R==:r R=e. e Sh:: des.n E=== . 0 0 0
- 14. Ec = Cc===::: Ca.! *=, 745 4,241.U 41,041.9
- 15. U:!: R::.:. e Sh=:down Ec= 0 0 0
. 16. Cross Th_._ ! I==;y C4===::d O1WE) 2,423,846 13,913,558 129,962,680-
- 17. Crost II :=i=!I:=;7 Gent =::d G.!WE) 792,10n _ 4,525,650 42.752,260 l 13. N :II::=i=!I:=;y Cc===::d C. WE) 763.916 4,367,243 41,220,614 l 19. Uni: Servi = .::=:r 100 57.9 71,3 I 20. Uci: Ari*.diII:7F =:or 100 57.9 71.3 l 2!. Un!: C:p:=i:/7::::r(Us!=; >!rC Ne:P . , 96.7 56.3 68.1
- 22. Unit Cae:d:y 7:::::(Usin; OIF. <*4:3 9J 2 54.2 66.8 0 2.6
- 23. Uni: For::d C ::;e R : 12.8
- 4. Sh:: downs 5d:de!:d Cver Nc.u 5.%=:h (Type. 0:::.:=d 0==:n of 2:si: .
Surveillance and maintenance outace scheduled to start 12/22/84.
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Estimated duration - two weeks l
- 05. If Sh : Oown A: Ind Cf R:; :: ?Eried. I::i==::d 0::: ei 5:: ::::
25'. Units is Tes: 5::::s iP=cr ta C:===::i:1 C;:=:ic=t: Fore. .:t . -Achieved IN1. ., *. -* r".".. *. .,* IJ , v. _
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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-316 ' -
UNIT 2 DATE 11/3/84 COMPLEiEDBY climer' TELEPHONE 616-465-5901 MONTH october 1984 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWE-Net)
(MWe-Net) 1 1065 17 1065 2 1035 18 1072 .
3 .
1064 1080
_ 19 .
- 1068 3077 20' 5 1069 21 1079 6 1072 22 1074 7 1069 23 1065 8 1067 24
~ _1076 9- 1054 .
25 1048 10 1066 25 818 11 1068- 791 27 12 1073 798 28 13 1071 813 29 1074 14 860-30 15 1066 31 1082 16 1053 -
INSTRUCTIONS On this famat list the average daily unit pcwer level in MWe-Net for each Cemnnea +, -
__ day in t.5e reportinn mnnv% _
r .
DOCKET NO. 50-316 ,
UNITSilUTDOWNS AND POWER REDllCTIONS UN8T NAME D.C. Cook - Unit 2 DATE 11-12-84 October, 1984 COMPLETED RY B.A. Svensson KEPORT MONTil TELEPilONE 616/465-5901 "L -
w = c
- ,E E 3 Licensee h f., Cause & Cinacclive No. Date h Eg % )YE {gE livent y?
idO 3 Action to Psevent Recmrence P
$$ gE j iy3 g Rep.HI # g b
151 841025 F 0 F 4 84-028-0 ZZ ZZZZZZ Reactor power was reduced to 80% as a precautionary measure due to a 17%
i deficiency in available au:tiliary feedwater flow under certain accident conditions involving a feedwater line break. A further reduction to 75%
for additional conservatism occurred on 841026. On 841029 the Unit was released to increase reactor power to 80% based on analysis performed by Westinghouse. Following the NRC's review of the analysis, the NRC 1 authorized the Unit to be returned to 100% power. The reactor power was restored to 100% on 841031.
l i
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i 1 2 3 4 1: l'os ceJ Heason: Method: Exlubis G - Instinctions j- A-Equipmesa Failme(Explain) 1 Manual for Pseparalism of Data S: Scheiluleil ll-Maintenance of Test 2 Manual Scram. Entiy Sheels fm 1.icensee C Refueling .l Automatic Scram. liven Repost (I I!R) File INllRl!G-D Regulatoiy Restsiccion 4-Othes ( Explain) 0161) l li-Opesatos l'eaining & ljcense lixaminalion F Administsative 5 a'
G Operational linor (lixplain) lixtuliit I - Same Somce 19/T1) 11 Other (Explain)
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UNIT SHUTDOWNS AND POWER REDUCTIONS INSTRUCTIONS This report should describe all plant shutdowns during the :n accordance with the table appearmg on the report form.
report period. In addition,it should be the source of explan. If category 4 must be used. supply brief comments.
ation of signincant dips in average power levels. Each sieni.'
ficant reduenon in power level (greater than 20% reduction LICENSEE EVENT REPORT =. Reference the applicable in average . daily power level for the preceding 24 hnurs) reportable occurrence pertainmg to the outage or power should be noted, even though the unit may not have been reduction. Enter the Erst four parts (event year, sequent:21 shut down completelyl . For'such rrductions in power level, report number. occurrence code and report type) of the rive the duration should be listed as zero,the method of reducnon part designation as desenbed in Item 17 of instruenons for should be listed as 4 (Other) and the Cause and Correcuve Preparation of Data Entry Sheets for Licensee Event Report Acnon to Prevent Recurrence column should explain. The (LER) File (NUREG.0161). This information may not be Cause and Correcuve Action to Prevent Recurrence column immediately evident for all such shutdowns, of course, since should be used to provide any needed explanation to fully further investigation may be required to ascertam whether ur describe the circumstances of the outage or power reduction. not a reportable occurrence was involved.) If the outage or power reduction will not result in a reportable occurrence.
NUMBER. This column should indicate the sequential num- the positive indication of this lack of correlation should be ber assigned to each shutdown orsigmticant reduction m power noted as not applicable (N/A).
, for that calendar year. When a shutdown or significant power reduction begins m one report penod and ends m another, SYSTEM CODE. The system in which the outage or power
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an entry shomd be made for both report penods to be sure reduction onginated sh'ould be noted oy the two digit code of all shutdowns or sigmilcant power reductions are reported. Exhi.ott. G . Instructicas for Preparation of Data Entry Sheets Until a unit has achieved its first power generation, no num. f r Licensee Event Report (LER) File (NUREG 0161).
ber should be assigned to each entry.
Systems that do not fit any existmg code should be designa.
ted XX. The code ZZ should be used for those events where DATE. This' column should ;ndicate the date of the start a system is not applicable, of each shutdown or signincant pcwer reducnon. Report as year. month, and day. August i.t.1977 would be reported COMPONENT CODE. Select the most appropriate component as 770814. When a shutdown or sigmficant power reduction from Exhibit i . Instructions for Preparanon of Data Entr>
begms m one report pened and ends in another, an entry should Sheets for Licensee Event Report (LER) File (NCREG.0161).
be made for both report periods to be sure all shutdowns using the followmg cdtiena:
or sigmncant power reductions are reported.
TYPE. Use "F" or "S" to indicate either "Forerd" or " Sche-duled." respectively, for each shutdown or signifcant power B. If not a component failure, use the related component:
reduction. Forced shutdowns include those rest. ired to be e.g wrong valve operated through error: list valve as initiated by no later than the weekend following discovery comoonent.
of an off-normal condition. It is recognized that some judg.
ment is required in categorizmg shutdowns in this way. In C. If a chain of failures occurs. tne first component to mai.
general a forced shutdown is one that would not have been function should be listed. The sequence of events.includ.
3_ completed in the absence of the condition for which corrective ing the other components which fail, should be desenbed action was taken.
under the Cause and Corrective Action to Prevent Recur.
rence column.
DURATION. Self. explanatory. When a shutdown extends beyond the end or a report penod count only the time to the Components that do not fit any existmg code should be de.
end of the report penod and pick up the ensuing down tune signated XXXXXX. The code 777777 should be used for in the following report penods. Report duration of outages events where a component designation is not applicable.
j rounded to the nearest tenth of an hour to facilitate summation.
The sum of the total outage hours plus the hours the genera. CAUSE & CORRECTIVE ACTION TO PREVENT RECUR-
- tor was on ime should equal the gross hours in the reportmg RENCE. Use the column in a narrative fashion to amplify or penod. explain the circumstances of the shutdown orpower reduenon.
The column should include the specific cause for each shut.
- n r5 n cant power %cdon and the immdate and REASON. CateEonze by letter deugnattun in accordance with the table appearing on the report form. If category H contemolated long term correenve action taken. if appropn.
must be used, supply bnet comments. ate. This column should alsc be used for a desenption of the l
major safety related corrective maintenance performed durma i
METHOD OF SHUTTING' DOWN THE REACTOR OR the outage r p wer reduction including an identification ot}
REDUCING POWER. Categonze bv numner designation the entreal path activity and a report of any single release et l_
radioactivtry or smgle radiation exposure speettically assoet-INote that this differs trom the Edison Electric insuture 3t'd *'th the outaae which accounts for more than 10 percent (EED dermitions of " Forced Panial Outage" and " Sche. of the allowsole annual values.
duled Partial Outage." For these terms. eel uses a shange of For long textual reports continue narrative on separate paper 20 MW as the break pomt. For 1.irger power reactors.30 MW and reference the shutdown or power reduetton fue im, l :s w small a Shange to wanant esplanation. narrative.
19'77 l
Dockht No.: 50-316
- ^ Unit Namas D.C. Cook Unit 2 Completed By: D. A. Bruck Telephone: (616) 465-5901 Date: 11-14-84 Page: 1 of 2 MONTHLY OPERATING ACTIVITIES - OCTOBER, 1984 HIGHLIGHTS:
The Unit entered the reporting period.in Mode 1 at 100%
of reactor thermal power. A major power reduction occurred because of a discrepancy in the Auxiliary Feedwater flow calculations resulting in a deficiency of approximately 17%-
in auxiliary'feedwater flow under certain accident conditions.
The Unit ended the reporting period at 100% rated thermal power.
Total electrical generation for the, month was 763,916 MWH.
SUMMARY
10-01-84 #2 CD Diesel was inoperable at 0507 hours0.00587 days <br />0.141 hours <br />8.382936e-4 weeks <br />1.929135e-4 months <br /> due to a failed inverter. The diesel was returned to service at 1844 hours0.0213 days <br />0.512 hours <br />0.00305 weeks <br />7.01642e-4 months <br /> on 10-01-84.
10-01-84 #2 AB Diesel was inoperable at 1853 hours0.0214 days <br />0.515 hours <br />0.00306 weeks <br />7.050665e-4 months <br /> due to an injector problem. The diesel was returned to service at 0328 hours0.0038 days <br />0.0911 hours <br />5.42328e-4 weeks <br />1.24804e-4 months <br /> on 10-02-84.
10-09-84 #2 E Essential Service Water Pump was inoperable at 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br /> due to low discharge pressure. The pump was returned to service at 1540 hours0.0178 days <br />0.428 hours <br />0.00255 weeks <br />5.8597e-4 months <br /> on 10-11-84.
10-13-84 Turbine Driven Auxiliary _ Feed Pump was inoperable at 0350 due to trip and throttle valve not latching.
The pump was returned to service at 0912 on 10-13-84.
, 10-19-84 Turbine Driven Auxiliary. Feed Pump was inoperable at 0608 hours0.00704 days <br />0.169 hours <br />0.00101 weeks <br />2.31344e-4 months <br /> due to steam leaks. The pump was returned to service at 1356 hours0.0157 days <br />0.377 hours <br />0.00224 weeks <br />5.15958e-4 months <br /> on 10-19-84.
10-25-84 At 2039, power was reduced to 80% as a precautionary measure due to a 17% discrepancy in available auxiliary feedwater flow under certain accident conditions involving-a feedwater line break.
10-26-84 A further reduction to 75% occurred at 1814 for the same reason.
10-26-84 At 1855, power was reduced because:#24 accumulator boron concentration was out of specification. The accumulator was declared operable at 0055 on 10-27-84.
, 10-27-84 Power reduction stopped at 63% at 0123. Power then-returned to 75% at 0435.
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'[ Dockst No. ' 50-316 Unit Namn D.C. Cook Unit'2 Completed By: D. A.:.Bruck Telephone: (616) 465-5901 Date: 11-14-84 l- Page: 2 of 2 10-29-84 At 1630, the. Unit was released to-increase. power to 80%.
'10-30-84 At 1800, the NRC authorized.the Unit to return to 100%
power. The power increase started at 2048, delayed due a chemistry hold. ,
10-31-84 At 0025, power.was returned:to 100%.
The Control Room Cable Vault Halon System remains inoperable as of 1707 hours0.0198 days <br />0.474 hours <br />0.00282 weeks <br />6.495135e-4 months <br /> on 4-14-83. The backup CO 2 system remains operable.
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, e DOCKET NO. 50 - 316 UNIT NAME D. C. Cook - Unit ~No. 2 DATE 11-13-84 COMPLETED BY B. A. Svensson TELEPHONE (616) 465-5901 -
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MAJOR SAFETY-RELATED MAINTENANCE" OCTOBER, 1984 M-1, Replaced fuel injector and fuel line on #1-F cylinder of 2-AB Emergency Diesel Generator. The engine was test.run to verify oil leakage had been eliminated.
M-2 No. 3 B. A. Transfer Pump was replaced by a rebuilt unit. De-fective pump will be rebuilt and returned to stock for, spare.
C&I-l The CD diesel inverter failed and C&I found one diode and~two" SCR's shorted. Replaced all four diodes and all four'SCR's.
Tested on load bank and placed in service.
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C&I-2 An intermediate range trip signal was being received from the Solid ~ State Protection System. An isolation board and memory board were replaced in the demultiplexing cabinet.of SSPS.
C&I-3 Terry' turbine trip and throttle valve solenoid operator would not latch up. The coils on trip solenoid 20X TDTV were found open preventing the latch-up. The coils were replac'ed.
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$zy,,, _ IN0iANA & MICHIGAN ELECTRIC C]MPANY Donald C. Cook Nuclear Plant P.O. Son 458, Bridgman, Michgan 49106
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' November 13, 1984 Director, Office Of Management Information and Program Contrel-U. S. Nuclear Regulatory Commission Washington, D. C. 20555 Gentlemen:
Pursuant to the requirements of Donald C. Cook Nuclear Plant Unit 2 Technical Specification 6.9 l.6, the attached Monthly Operating Report for the Month of October, 1984 is submitted.
S*ncerely, bd- A W. G. Smith, Jr.
Plant Manager WGS:ab Attachments cc: J. E. Dolan M. P. Alexich R. W. Jurgensen NRC Region III B. L. Jorgensen R. O. Bruggee (NSAC)
R. C. Callen S. J. Mierzwa R. F. Kroeger B. H. Bennett P. D. Rennix J. H. Hennigan Z. Cordero J. J. Markowsky J. F. Stietzel PNSRC File INPO Records Center ANI Nuclear Engineering Department ges4
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