ML20100L515

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Monthly Operating Repts for Oct 1984
ML20100L515
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 10/31/1984
From: Mcbay M, Nix H
GEORGIA POWER CO.
To:
NRC
References
GM-84-1025, NUDOCS 8412110578
Download: ML20100L515 (17)


Text

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NARRATIVB REPORT E- .. s

' UNIT 1 j

Oc t ober 1st 0000- ' Unit' Re fueling Out age in Progress.

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HATCH 1 SAFETY-RELATED MAINTENANCE REQUESTS ~

TO BE REIORTED EDR October 1984 NUMBER DATE COMPLETED DES CRIPTIOu

. A 84-494 05-07-84 Identified tagged 1.y .

.V procedure all equipment installed on CRD Scram Discharge Volume Vents &

Dra ins . Re f . D CR 8 3-032. _

l 82-8041- 10-15-84 Modified existing -

hangers / pipe support s on RHR

& Plant Service Water System (MPL # IP41) . Ref . D CR 80-183.

84-5818 10-17-84 Installed Break Glass Stations around swit ches R26-M07 3 '& R26-M07 4. Ref.

D CR 8 3-0 3 2.

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( OIERATING DATA C7RP 3

  • Q] \ / -[Q DOOG7P 10, 50-321 .

DATE. 11-10-84 CD4PIETED BY: M.G. M:Bny

'IEIEPIENE - (912) 367-7851 OPIRATItU STATts tbtes

l. Unit Nsne: E. I. Hat ch & clear P1 art Unit 1 l 2. kporting Period: 10-84 3.~ Licensed Thermal Ibwer (MWL): 2436
4. &meplate mting (Gross MW): 8 G. 3
5. Design Electrical Rating (Net MW)
777.3

) 6. mximum Dependable Capacity (Gross MW): 801.2

7. mximum Ihperdable Opcity (&t MW): 752.2
8. If Changes Occur in Capcity htincy (Items mmber 3 through 7) Since last Report , Give Reasam:
9. Power Invel to hhich kstricted, If Any (Net MW)
10. Nasons for &strictions, If Any:

l This Pbtth Yr-t o-Dat e Cumulative

11. Hours In Reporting Period 745 73:D 77447
12. Ntaber of Hours Reacta was Critical 0 5633.8 5516 4
13. Reactor Reserve Sutdown Hours 0 0 0
14. Hours Gererata Ot-Line 0 5474.9 51867.9
15. Unit kserve Sutdown Hours 0 0 0 1
16. Gross Thermal Fhergy Generated (MWH) 0 1215116 2 ~109369190
17. Gross Electrical Energy Generated (PMH) ,

0 379 7550 352557 20

18. Net Electrical Ehergy Generated (MMI) - 4 033 3605148 33464511
19. Unit Service hctcr 0 74.8 67.0
20. thit Availability heta  ; O 74.8 67.0
21. Unit Capcity &ctor (Using 20C Net) '

-0.7~ 65.5 57.4.

22. thit Capacity Factor (thing DER Net) -0.7 63.4- 55.6
23. Unit Ibecal Otage hte 0 15 .0 18.1
24. Ehutdowns Scheduled Over Next 6 lbrths (Type, Date, ani Duration of Each):

Refueling 10-1-84 10 week duration

25. If Shutdown at Ehd of Report Period, Estimated Date of Start up:
25. Units in 'Ibst Status (Prior to Consercial Operation): Forecast Achieved i

INITIE CRITICALITY INITIAL EIEC'IRICITY CDff4ERCIE OIERATION i d

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I LEE L AERPGE IAIIY lEIT (~)8 t .

DOGET NO. 50-321 DNIE : 11-10-84 GNPETED BY: M.G. McBly

'IEIEPIINE (912) 357-7851 MCN'IH 1 & 84 DAY AERIGE IAILY WWER MEL DAY AERIGE IRILY WWER LE\EL (MW-Net ) (MM-Net )

1 -9 17 -4 2 -9 18 -4 3 -7 19 -4 4 -7 20 -4 5 ~7 21 -4 6 -7 22 -5 7 -7 23 -4 8 -7 24 -4 9 ~7 25 -4 10 -7 26 -4 11 -7 27 . -4 12 -7 28 '

-4 13 -7 29 -4 14 -5 30 -4 15 -5 31 -4 16 -4 t

l (9/77)

DOCKET NO. 50-321 UNITS!!UTDOWNS AND POWER REDUCTIONS .

UNIT NA'lg Hatch I

  • DATE.11-06-R4 COMPLETED By Mike McBay REPORT MONTil October 1984 TELEPl!ONE 912-367-7851 e.

o .$ ? "g ) .Y Licens:e E,3 "-

. 'Cause & Corrective -

No. Date g 3g  ;; jg5 Event g? o-3 Action to H

35 $ .5 is g Repor! # mo go Prevent Recurrenee a , u ,

a 84-72 84/10/01 S 745.00 C 2 N/A RC FUELXX Jnit Refueling Outage in progress.

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4 I F: Forecd Reason: Method: '

Exhibit G-Iristructions S: S:h:duted A Equipment ~ Failure (Explain) - 1-Manual t for Preparation of Data ,

B. Maintenance of Test 2. Manual Scram. -

Entry Sheets for Licensee  ;

C-Refu: ling . 3 Automaile Scram. j Event Report (LER) File (!JUREG-:

4 --Continuations D Regulatory Rest:iction .

  • ' 0161) -

E Operator Training & License Examination 5-Ioad Paduction '

F.Adminis.ra:!ve 9-Other (Explain) 3  !

  • G Operations! Errer(Explain) *
  • Exhibit I SameSource  ;

ra/77) II.Other(Explain) .. . .

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NARRATIVB REPORT

- (~') ; UNIT 2 V

October 1st 0000 Still off-line follwoing Rx.

Scram due t o loss of vacuum on -

9-30-84.

1400 Repairing valve 2N36-F00 SA extraction t o 4th st age feedwat er heater & also repairing RSULV's 2N11-F00 6A& B.

1933 Valve repairs complet e.

Increasing Rx . Power i o 25 %

t hermal via cont rol ' rods .

October 2nd 0100 Movement o f rods post po ned because of problems wit h Rod Sequence Cont rol System.

Problems are being investigat ed.

1145 Began pulling cont rol rods .

Ramping back t o rat ed power.

2345 Plant st atus at 582 MWe , 1771 MWT

& st il17ampingTo rated pcwer. ~~ ~~

(_) October 3rd 2245 Plant _st at us now at 9 4.5 %_ CMWT, 2303 CMWT.

October 4t h 1903 Automatic reactor scram an MSR hi level readi ng.

October 5 t h 03 07 Reactor crit ical .

g 1020 Ge nerat or t ied to line following Rx. Scram on MSR hi level .

19 36 Holding power at 70% to run OD-1.

2129 OD-1 completed . .

2300 Received high t emp. ala rm on 2B &

2D RHRSW Pumps . Nintenance was found t o be working on these Unit 2 pumps when t hey should have been working on Unit 1 pumps.

Oc t ober 6t h 0445 Problem with RHRSW pumps resolved and unit is ramping to rated .

s' Oc t ober 7t h 0648

Pla nt st at us now at CMWT 2 328 and l

764 GMW'e.

. Oct obsr 7th 15 30 Rsact or ccran on MSR hi- lovel.

2301 Reactor . critical following scram on MSR hi level.

~ r~N October 8t h . 0503 Generator t ied to line : following isf scram. Load i ncrea sing t o .

approximately 15%. Load will be held ~at . this level so t hat MSR t estng may be performed for- more -

probl ems .

Oc t ober 9t h - 0600 Pulling control rods t o increase load to. approximately 200 GMWe . -

09 03 . Load now bei ng incr ea sed t o 500

, WW.

1320 Load being held at 500 GHWe due to APRM rod blocks and STA per forming OD-1.

1900 Start ing . to increase power again. Presently at - 515 GMWe a nd increasing to approximately 540 GMWe by ,recirc flow on precondit ioning ramp.

j Oc t ober 10 t h 2320 Pla nt stat us is now at 97% power wi t h no ma jor problems . Ramping to rated- is st ill in progress .

O October lith 0525 Daily turbine test ing & RFPT t est ing is in progress.

F October 12t h 10 20 'B ' recirc pump ran away to 100%

speed pump is being backed down L wi t h manual crank .

2340 Pla nt stat us back at 97% - 2363 CMWT and 783 MWe.

E October 13 t h 2126 Load reduct ion in progress for rod adjustment & turbine test ing. Load reduced by decreasing recirc flow.

October 14 t h 0212 Turbine test ing and RFPT test s c ompl et e . Loading back t o rat ed.

0645 Load at 2433 CMWT and approximat ely 790 MWe . Load being increased to rated .

l October 18t h 1933 Shi f t noticed condenser vacuum d ecrea si ng. Problem is being investigated.

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2018 ' Low Vacuum' alarm received and load is being decreased by '

recirc. flow t o approximat ely 590 GMW' e.

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Oct obar 19 t h 0043 .Powar being inceeasad to 700 'MWs  !

by recirc. flow.

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' 0518 ~ Ioad increases. stopped.

Presently at 750' MWe , -

2110 load reduction started by recirc.

flow because of condenser vacuum probl ems .

  • October 20t h 0815 Received ' orders for normal

. shut down becau se main condenser vacuum broken . ^

13 18 Iow Power level reactor scram.

Oc t ober 21t h 0500 React or crit ical following scram. -

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1141 Generator tied' to line. Ramping t o rat ed by pulling of control rods. Condenser vacuum is being ob ser ved for more problems.

October 23th 0630 Plant status. now at 97.^2% Q4WT 2 368 and GMWe reading of 783.

October 27th 00 20 Started reducing reactor load to 700 MWe for SRV . valve t esting -

( HNP-2-3901 ) . . Ioad presently at l~' -

792 GMWe.

0235 Began increasing reactor load '

back t o rat ed following completion of SRV's cycling.

Ioad presently at 695 GMWe .

0630 Load now a t 99.1 % CMWT ' of 2414.

Ioad will remain close to rated -

for remaining time of .the month. -

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. HATCH 2- SAFETY-RELATED MAINTENANCE " REQUESTS TO BE RSIORTED FOR October 1984 NLMBER DATE COMPLETED DES GIPTION (3 ,

(-)63-526 08-24-84 . Pulled and terminated all cable & performed all internal wiring for Unit 2 Analog Transmitter Trip ~

System. Also engraved all annunciator windows &

nameplates. Re f . O CR 81- 39 .83-527 08-25-84 Installed inst rument racks, pa nel s , . i'nstrumentat ion, a ir accumulates, piping, tubing, valves and supports required for installation of the Analog Transmitter Trip System. Re f . D CR 81-139.83-528 08-24-84 . Installed raceway &

installed and fabricat ed raceway supports required to complete Analog Transmitter Trip System. Re f . D CR 81- 139 .

, 83-2421 08-23-84 Sealed Rosemount di f f erential pressure 3 - t ransmitters Q2 P7 0-FT-N0 20 4

() A, B & NO2 2A, B by procedure HNP- 69 54. Ref. D CR 81-112.

83-3552 07-31-84 Checked & replaced pressure 4

relief valve 2P 48-S V-3 on Ni t roge n St orage Tank . Re f .

' D CR 8 4- 179.84-213 08-09-84 Replaced existing motor and HPCI Di scharge Isol . Valve &

2841-F008 wit h new motor &

! actuator of class RH

! insulation Type SB to

' satis fy environmental qualification requirements

( of IEB Bullet in IEB-7 9-OL B.

l Re f . D CR 81- 177 .

83-6143 07-11-84 Route and support conduit on Drywell Pneumatics system (MPL # 2 P7 0) . Re f . D CR l 81-112.

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HATCH 2 I-SAFETY-RELATED MAINTENANCE REQUEST 3 TO BE RE PORTED FOR October.1984- 2 s

NLMBER DATE COMPLETED DES GIPTION '84-727, 07-08-84 Modified pipe supports RCIC system (M PL # 2E 51) . Re f .

D CR' 8 2-257.84-897 08-16-84 Modified . pipe supports on -

Turbine Bypass . Piping System (M PL' # 2N 37 ) . ' Ref . D CR 82-257, Rev . 1.

899 06-08-84 Modified existing pipe s upport s 2 Ell-RSW-R17 & R25 on RHR Sys . Service Water Ret urn .

  • Ref . D CR 8 2-257, Rev . 1.84-909 07-23-84 Modified! existing pipe s upport s 2G41-FPC-All7 on Fuel Pool Cooling System.

Re f . D CR 8 2-257, Rev. 1.

84-1049 07-23-84 Modified pipe supports on Turbine Bldg. - High Pressure Steam to steam jet air ejectors. (MPL . # 2N11 ) .

' Ref r D CR 8 2-257, Rev. 1.

O 84-1086 06-13-84 Terminated and redlined cables & wiring on the T

- Drywell Pneumatic System i

Isolation Valve E I Inst ruments Calibrated in st rume nt s 2 P7 0-FT-N0 20A& B

, - and 2 P7 0-FT-N02 2A& B. Also j _ installed supports and modified tubing and per formed , pneumatic test .

! Ref . D CR 81-112.

i L 84-1176 05-16-84 Phbricated & installed

( inst rument supports and I tubing supports on Containment Atmosphere Recombiner Flow & Press.

T ran sai t t er . Removed

existing flott and pressure i- t ransmitters & installed new Ro se mount model flow and

! pressure t ransmit t ers. Also l

per formed Pneumat ic . test on new tubing. Re f . D CR 8 3- 37, q{ } Rev. 1.

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HATCH 2 SAFETY-RELATED MAINTENANCE ' REQUESTS ,

TO BE RS PORTED FOR -October 1984 q NLMBER DATE COMPLETED DES CRIPTION 84-1477 05-30-84 Installed Conduit, Co nduit Support s , Pull Boxes, .

Junction Boxes, Terminal Boxes, Removed existing -

co nduit & rerouted existing-cable for installation of inst rumentat ion on Nit rogen Inerting System.

Calibration of inst rumentation was also performed. Re f . D CR 8 4- 049, Rev. 1.

84-1478 07-13-84 Per formed Installation and routing of air piping, fittings, valves, tubing, tube fittings, fl ex ho se , -

air set , solenoid valve &

pipe aupports for 2 P33-F016.

Re f . D CR 81- 165 .

84-1485 08-18-84 Modified Pipe Supports 2N38-LFS-A34 on the High Pressure Steam Line to

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' Reac t or Feed Pump Turbine.

Ref . D CR 8 2-257.

84-1526 07-23-84 Modified Existing pipe support s for MPL #

2C11-Cont rol Rod Drive System. Ref . D CR 8 2-257, Rev. 1.

84-1812 08-17-84 Installed raceway supports ,

cond uit s , & cable ch=nnel for D.C. Swi t chgea rs Dist ribution Panels &

Cont rol Panels. Installed mounting pads for Swi t chgea rs 2R22-S018 &

S 0 19 . Drilled Cove & set co nduit sleeves. Also chipped floor for installation of ground cables. Installed Swi t chgea rs & D.C.

Dist ribution panels 2R25-S129 & S130. Also installed Cont rol Panels 2H21-P3 48 & P3 49 .

/~' Terminated all rerouted cables.

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HATCH .2 SAFETY-REL'ATED MAINTENANCS REQUESTS TO BE ROIORTED FOR Octobar' 1984 NtNBER DATE COMPLETED DES CRIPTION tm

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84-1921 08-06-84 . ~

. Delete circuit ry, conduit ,

thermostats & other associated equipment making up the old heat i racing .

system on H 022 Analyzero system - MPL # '2 P33-P001A&B.

Re f . D CR 81- 165 .

84-2257 07-18-84 Fabricated and installed startr.up instrumentat ion bracket s at locations A1, A3, B1 & B3. .(MPL # 2831).

Re f . D CR 8 3- 17 3.

84-2327 08-17-84 ,

Installed additional fire barrier, shielding around Remote Shutdown Panel 2 C8 2-P00l A& B. Re f . D CR 83-251. ,

84-2508 08-10-84 Installed & calibrated the

. resistance t emperature 3 det.ectors on start-up

, inst rumentation (MPL #

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DOOTT NO. 50-366 .

DATE 11-10-84 CD4PLETED BY: M.G. ItIhy -

'IEIEPIDIE (912) 367-7851 OPIRATItG STATLE lbtes

1. Unit Mme: E. I. Hat ch Nuclear Plant Unit 2
2. Ibporting Period: 10- 84
3. Licensed Thermal Ibwer (MWt): 2436
4. Mmeplate Ibting (Gross MW): 8 17 .0
5. Ibsicp Electrical Ibting (Ibt MW): 784.0
6. &ximum Ibpendable Capacity (Gross MW): 803.9
7. bilximum Ibperdable Capacity (Nat MW): 7 47.9
8. If Changes O: cur in Capacity Ihtincy (Itens N2mber 3 throucft 7) Since last ReIort , Give Ibasars:
9. Pbwe level to Mich Ibstricted, If 1hy (Net MW3):
10. Ibasors for Ibstrictions, If Any:

This bbnth Yr-to-Qate Cumulative

11. Hours In Ibpcrting Period 745 7320 45073
12. N2mber of Hours Ibact or was Critical 718.5 1778.0 23849.2
13. Rector Ibserve mttdown Hours 0.0 0 0
14. Hours Cererator Ch-Line 680.0 15 54. 3 27342,2
15. thit Ibserve mttdcwn Iburs 0.0 0 0
16. Gross Thermal Ehergy Generated (MWH) 1424CD 3 3139 311 58 355566
17. Gross Electrical Energy Generated (f4fH) 47230 1027810 19199500
18. Nat Electrical Ehergy Generated (MWH) 450751 955732 18 2448 3
19. Unit Service hetcr 91.7 21.3 60.7
20. thit Availability Rictor 91.7 21.3 60.7
21. thit Capacity Factor (Using MDC Net)  ; 81.0 17 .5 54.1
22. thit Capacity &ctor (thing DER mt) 77.3 16.7 51.6
23. Unit Ebrced Outage Ihte 8.5 8.6 13.0
24. mutdcuns Scheduled Over Next 6 bbrdhs (Type, Ihte, ard Ibration of Ehch):

Recirc piping outage still in Irogress.

25. If mutdown at Ehd of Ibport Period, Estimated Date of Start up:
35. Units in 'Ibst Status (Prior to Connercial Operation): Ebrecast Achieved INITIAL CRITICALITY INI'II AL EIEC'IR] CITY CDbNERCIAL OIEPEION t

(9/77)

AERPGE DMLY INIT LEE L -

DOGET 10. 50-366 -

DA'IE : 11-10-84 CD4PIETED BY: M. G. ftBly

'IEIEPIENE (912) 357-7851 MCEIH 10-84 DAY AERIGE DMIY WWER IEEL DAY AERIGE DMLY mWER IEEL (MW3-Nd ) (MWa-Net )

1 61 17 778 2 341 18 748 3 659 '

19 69 4 4 598 '--

20 158 5 193 21 m 127 6 - 63B 22 59 0 7 47 7 23 763 8 83 24 778 9 338 25 -

780 i

10 674 26 774 11 778 27 764 12 746 28 805 13 772 '

29 775 14 779 30 , 77 3 15 7 81

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50-366 .

UNITS!!UTDOWNS AND POWER REDUCTIONS DOCKETNO.

UNIT NA'.1E . Hatch 2 DATE .11-06-84 0 ctober 1984 CDMPLETED BY Mike McBay REPORTMON1Tf TELEPl!ONE 912-367-7R51

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"Cause & Currective -

No. Date Eg  ;; .3 g 5 Q

R Event u Action to

. I-dr $ j dj Report # N u? g ,, Prevent Recurrence o

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i 84-18 84/10/01 F 25.07 A 5 N/A CH VALVEX Repair [ Ext. Valve to 4th stage feedwate'r heater & investigating problem with RSCS .

84-19 84/10/02 S 38'25

. B 5 N/A. CH VALVEX Incre'asing power back to rated.on preconditioning ramp.

84-20 84/10/04 F 15'.28 A- 3 N/A HH HTEXCH Reactor scram on MSR hi level. .

84-21 84/10/05 S 43.67 8- 5 N/A HH HTEXCH Increasing load back to rated. .

84-22 84/10/07 F~ 13.55 A 3' N/A ' HH HTEXCH ReacI;or scram on MSR hi level. .

84-23 84/10/08 66.28 S A 5 N/A HH HTEXCH Holding load for MSR testing &

preconditioning ramp to rated.

n ,

J l 1 3 , . *4 i F: Forced Reason: . Method: 5 Exhibit G-Idstructions -

S: Schedufed A Equiiment' i Failure (Explain) : ' I-Manu:1 ' .: for Preparation of Data ',

B Maintenance of Test 2-Manual Seram.

.. Entry Sheets for Licensee .'

C-Refu: ling; . 3. Automatic Scram. Event R: port (LER) File (NUREG-:  ;

}

4 -Continuations D Rer,ulatory Rest:ic:fon *

  • 0161)  ;*

E-Operator Training & Ucense Examination 5-Icad Paduction F.Actninis.ra:!ve 3 G-Operational Erre (Explain)

  • 9-Other (Explain) Exhibit !-Sa! meSource

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C2177) il-Other (Explain) .. .

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UNIT S!!UTDOWNS AND POWER REDUC"IlONS .

DOCKETNO. 50-366 ,

UNITNA'.!E Hatch 2

. ' DATE ,11-06-84 COMPLET D Ft ke M Ba ,

REPORTMONT!! October 1984 ,

g _

i Q I o .$ 'E }; .E Licensee $wl, - .

'Cause & Corrective -

No. Date o. pg ,g g 5 Event I u,Eg E'

  • 5! Action to N $iE 5 Report # 'N 0

[ b" j18g ,, Prevent Recurrence o

  • 84-24 84/10/12 F 13.33

. A 5 N/A CB PUMPXX Load reduction due to 'B' Recirc Pump 4

running'. to 100%. speed.

84-25 84/10/13 S 4.77 F 5' N/A' HA TURBIN Load reduction for Turbine' test & rod pattern adjustrhent.

84-26 84/10/18 F 41.'75 A 5 N/A HC XXXXXX. Load reduction due to condenser vacuum problems.

84-27 84/10/20 F 22'.38 A' 3 N/A' , HC XXXXXX Reactor . scram on low level due to ti he -

problems with condenser vacuum. ,

84-28 84/10/21 S. 42.82 B 5 '- N/A HC XXXXXX Scram recovery testing condenser. vacuum being observed. .

~

84-29 84/10/27 S 3'.67 B. 5 N/A SH VALVEX SiiV valve tssting being performed.

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t i 2 3 . 4 I F: Forced Reason: '

. Method: 5 Exhibit G-Irlstructions S: Schedu!cd A Equipment *Fe!!ure(Explain) : 1-Mane:1 for Preparatidn of Data B41sintenance of Test 2 Manual Scram. .. Entry Sheets for Licensec  ;

C-Refueling . 3 Automatic Scram. Event R port (LER) File (NUREG :  :

}

4 -Continuations

. D Rogulatory Rest:iction -

. 0161)  ;*' .

',' E-Operator Training & Ucense Examination 5-Icad Reduction '~ ~

F-Adminis,rs:ive 3 G-Operations! Erret(Explain)

  • 9-Other (Explain) Exhibit !-Sa!

, me Source  ;

P2/77) II-Other (Explain) .. .

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l Georgia Power Company Post Office Box 439 Baxley, Georgia 31513 Telephone 912 367-7781 912 537-9444 m -

Edwin 1. Hatch Nuclear Plant .

November 8, 1984

  • G4-8 4-10 2 5 PLANT E. I. HA'ICH NRC Monthly Operating Report Of fice of Plans and Schedules Directorate of Licensing Unit ed States Nuclear Regulatory Commission Was hington , D. C. 20545

Dear Sir:

Per Tech Specs section 6.9.1.6 please find attached the NRC Monthly Operating Report for Hat ch Unit 1, Docket #50-321, and f or Ha t ch Uni t 2, Docket #50-366.

N . %_ J-u.A._.

H. C. Nix

) General Manager 3 c'l $

HOT /CTJ/ JAB /hh f6Y:

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