ML20100D969
| ML20100D969 | |
| Person / Time | |
|---|---|
| Site: | Perry |
| Issue date: | 11/21/1984 |
| From: | Edelman M CLEVELAND ELECTRIC ILLUMINATING CO. |
| To: | James Keppler NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| References | |
| (RDC-76(83)), NUDOCS 8412060097 | |
| Download: ML20100D969 (2) | |
Text
t or e c.
THE CLEVELnUD FLECTR!C ILLUMIN AT!NG COMPANY P.o. BOA 5000 - CLEVELAND, oHlo 44101 - TELEPHONE (216) 622-9800 - lLLUMINATING BLDG. - F UBLIC SQUARE Serving The Best Location in the Nation RJRRAY R. EDELMAN VICE PRESIDENT NUCLEA R Mr. James G. Keppler Regional Administrator, Region III Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, Illinois 60137 RE:
P' cry Nuclear Power Plant
' cket Nos. 50-440; 50-441 Safety Relief Valves Supplied by the General Electric Company
[RDC 76(83)}
Dear Mr. Keppler:
This letter serves as a final report pursuant to 10CFR50.55(e) on the significant deficiency concerning the actuators on Safety Relief Valves (SRV) supplied by General Electric Company (GE) to the Perry Nuclear Power Plant (PNPP),
Mr. E. Riley of The Cleveland Electric Illuminating Company notified Mr. P. Pelke of your office of the potential significant deficiency on June 30, 1983. Previous correspondence on this subject was submitted July 29, 1983, and May 15, 1984.
This report contains a description of the potential deficiency, an analysis of safety implications, and the corrective action being taken.
Description of Deficiency During equipment qua.lification testing to NUREG 0588, several seals manufactured of Viton E60C material and located in the pneumatic actuators of the SRVs failed due to high radiation exposure. In addition, during Loss of Coolant Accident (LOCA) testing following replacement of the seals, the solenoid of the actuator failed due to shorting caused by steam intrusion.
General Electric has furnished 57 SRVs to PNPP which are affected by this problem.
Analysis of Safety Implications A failure of the actuator for either of these reasons would render the SRV inoperative for Automatic Depressurization System (ADS) functions. Without the proper function of the ADS mode of the SRV, reactor pressure could not be lowered enough to allcw use of the Low Pressure Core Spray System and possibly other Emergency Core Cooling Systems designed for low pressure use.
8412 gO Pk
_~ -
PDR p;: ; 7 s
NOV 2 6 B84
r Mr. Jcues G. Ksppler Novambar 21, 1984-It should be noted that the mechanical safety relief function of the valve during a' system high pressure event would not have been impaired by an actuator failure.
1 Corrective Actions Relative to equipment qualification testing, the seals in tne. actuator used for testing were replaced with EPDM seals and tha lubrication was changed to
" Super-0-Lube". The SRV was then successfully retested to NUREG 0588, except for the solenoid problem identified during LOCA testing. No further anomalies occurred concerning the actuator seals after their replacement. The solenoid was replaced with a hermetically sealed design which will prevent steam intrusion and retesting is in process. This retesting will be completed by June 1, 1985.
Nonconformance Report OPQC-0448, OPQC-0668 and OPQC-0669 were initiated for the Unit 1, Unit 2, and spare SRVs respectively. General Electric has initiated FDI 139-82411 to implement the changes described above for the Unit I and spare SRV actuatt,rs.
By June 1, 1985, all actions necessary for resolution of this significant deficiency relative to Unit I will be completed.
Completion of the Unit 2 repair will be consistent with the Unit 2 construction schedule prior to turnover of the affected systems.
Please call if there are any questions.
Sincerely, Murray. Edelman Vice President Nuclear Group MRE:pab cc:
Mr. J. A. Grobe NRC Site Office Director Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, D.C.
20555 U.S. Nuclear Regulatory Commission i-j c/o Document Management Branch i
Washington, D.C.~
20555 i
Records Center, SEE-IN l
Institute of Nuclear Power Operations 1100 circle 75 Parkway, Suite 1500 Atlanta, Georgia 30339 l
o
. - _ _ _, _, _. -., _ _... _ _ _,, _ _.. _ _. _. _. _ _ _.,.. _. _ ~. - _... -
. -... -.. _, _,., ~ _.
-