ML20098F708

From kanterella
Jump to navigation Jump to search
Interim Deficiency Rept (55(e)-84-32) Re Problems W/Hpcs Diesel Generator.Initially Reported on 840809.Investigation Continuing.Next Rept Will Be Submitted by 840107
ML20098F708
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 09/10/1984
From: Mangan C
NIAGARA MOHAWK POWER CORP.
To: Starostecki R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
(55(E)-84-32, (55(E)-84-32), (NMP2L-0156), (NMP2L-156), 55(E)-84-32, NMP2L-156, NUDOCS 8410030285
Download: ML20098F708 (2)


Text

. _ ______- ______ - __ _ _ - ___ ________-__ _____________ _ ______________

..._ < d.

2 M V NIAGARA RUMOHAWK NIAGARA MOHAWK POWER CORPORATION /300 ERIE BOULEVARD WEST. SYRACUSE, N.Y.13202/ TELEPHONE (315) 4741511 September 10, 1984 (NMP2L 0156)

Mr. R. W. Starostecki, Director U.S. Nuclear Regulatory Comission Region I Division of Project and Resident Programs i

631 Park Avenue King of Prussia, PA 19406 Re:

Nine Mile Point Unit #2 Docket No. 50-410 g

r

Dear Mr. Starostecki:

Enclosed is an interim report, in accordance with 10CFR50.55(e) for the problems concerning high pressure core spray diesel generator. This condition-was reported via tel-con from G. Griffith (Niagara Mohawk Licensing) to P.

Russ of your staff on August 9,1984 Very truly yours, C.V. Mangan Vice President Nuclear Engineering and Licensing CVM/sc xc: Director of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, D.C.

20555 R. A. Gram, NRC Site Inspector Project File (2)

BAD B

I W.>cTL_

7 4

NIAGARA M0 HAWK POWER CORPORKiION NINE MILE POINT - UNIT 2 DOCKET NO. 50-410 Interim Report for Problems Concerning High Pressure Core Spray Diesel Generator

( 55(e)-84-32) l Description of the Problem During a review of the high pressure core spray diesel generator equipment, various modifications to this equipmment were identified which we believe are l

necessary for the proper operation of the high pressure core spray system.

The following safety related problems were identified:

1.

In switchgear 2 ENS *SWG102, current transformer terminals on nonsafety-related short-circuiting terminal block A are not properly spaced and/or separated from similar terminals on safety-related short-circuiting terminal block B.

2.

In relay panel H22-P02B, nonsafety-related terminal block points A-1 and A-2 are not properly spaced and/or separated from safety-related points A-7 and A-8.

i 1

3.

Non-Class 1E station battery monitor relays were connected to the Division III Class 1E battery system with on'iy single fusing.

4.

Improper separation of non-Class 1E panel light power wiring from Class 1E wiring.

5.

GE has identified a problem with its NGV relays, containing defective ohmite mode E potentiometers, that were manufactured I

between October 1,1973, and November 1,1976.

The matter is still under investigation and a final report will be submitted by January 7,1985 n

e

~'

_. - - _ _ - _ _. _ _. _ _. _. _ _ _. - _ _ -