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Results
Other: 05000336/LER-1983-007, Updated LER 83-007/01T-1:on 830318,nonconservative Safety Analysis Assumption Discovered in Steam Generator Tube Rupture Analysis.Radiological Consequences of Reanalysis Being Analyzed, A03722, Forwards Addl Info Re Effects of Loss of Offsite Power on Steam Generator Tube Rupture & Main Steam Line Break Analyses, B10960, Discusses Steam Generator Tube Rupture Reassessment for Cycle 6 Operation.Radiological Doses Will Be Increased as Result of Lower Reseat Pressure.Releases Expected to Be Significantly Below 10CFR100 Criteria, B11003, Informs That Util QA-verified 831212 Reanalysis of Steam Generator Tube Rupture Event.Reported Results Remain Valid. Verification Completed Prior to Startup for Cycle 6, B11098, Provides Summary of Radiological Results Re Steam Generator Tube Rupture Reanalysis.Table Containing Doses for All Analyzed Cases Encl, ML20087K388, ML20116E663
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MONTHYEAR05000336/LER-1983-007, Updated LER 83-007/01T-1:on 830318,nonconservative Safety Analysis Assumption Discovered in Steam Generator Tube Rupture Analysis.Radiological Consequences of Reanalysis Being Analyzed1983-12-0909 December 1983 Updated LER 83-007/01T-1:on 830318,nonconservative Safety Analysis Assumption Discovered in Steam Generator Tube Rupture Analysis.Radiological Consequences of Reanalysis Being Analyzed Project stage: Other B10960, Discusses Steam Generator Tube Rupture Reassessment for Cycle 6 Operation.Radiological Doses Will Be Increased as Result of Lower Reseat Pressure.Releases Expected to Be Significantly Below 10CFR100 Criteria1983-12-12012 December 1983 Discusses Steam Generator Tube Rupture Reassessment for Cycle 6 Operation.Radiological Doses Will Be Increased as Result of Lower Reseat Pressure.Releases Expected to Be Significantly Below 10CFR100 Criteria Project stage: Other B11003, Informs That Util QA-verified 831212 Reanalysis of Steam Generator Tube Rupture Event.Reported Results Remain Valid. Verification Completed Prior to Startup for Cycle 61984-01-17017 January 1984 Informs That Util QA-verified 831212 Reanalysis of Steam Generator Tube Rupture Event.Reported Results Remain Valid. Verification Completed Prior to Startup for Cycle 6 Project stage: Other A03635, Forwards Info & Comments in Response to 831114 Request for Various Confirmatory Evaluations & Justification for Analytical Models Utilized in Cycle 6 Safety Analyses1984-02-0101 February 1984 Forwards Info & Comments in Response to 831114 Request for Various Confirmatory Evaluations & Justification for Analytical Models Utilized in Cycle 6 Safety Analyses Project stage: Request ML20087K3881984-03-13013 March 1984 Submits Details of Followup Actions on Amend 90 to License DPR-65.Adequate Justification Provided to Demonstrate Applicability of Current Large Break LOCA Evaluation for Operation W/O Thermal Shield Project stage: Other B11098, Provides Summary of Radiological Results Re Steam Generator Tube Rupture Reanalysis.Table Containing Doses for All Analyzed Cases Encl1984-04-13013 April 1984 Provides Summary of Radiological Results Re Steam Generator Tube Rupture Reanalysis.Table Containing Doses for All Analyzed Cases Encl Project stage: Other ML20098B7771984-09-14014 September 1984 Forwards Info to Resolve Concerns Identified During Feb 1984 Meeting Re Large Break Loss of Coolant,Steam Line Break & Steam Generator Tube Rupture Accident Evaluations Submitted to Support Cycle 6 Operation,Per Amend 90 to License DPR-65 Project stage: Meeting ML20112B5431985-01-0909 January 1985 Responds to NRC 831230 Request for Addl Info.Assumption of Complete Mixing Not Concern from DNB Standpoint for Facility Since No Boiling Occurred in Hot Channel for Steam Line Breaks W/Different Mixing Factors Project stage: Request ML20116E6631985-04-22022 April 1985 Discusses Followup Actions to SER for Amend 90 to License DPR-65.New Steam Line Break Generator Tube Rupture Analysis Will Be Submitted for Review 4 Months After Startup from Current Refueling Outage Project stage: Other A03722, Forwards Addl Info Re Effects of Loss of Offsite Power on Steam Generator Tube Rupture & Main Steam Line Break Analyses1985-11-0808 November 1985 Forwards Addl Info Re Effects of Loss of Offsite Power on Steam Generator Tube Rupture & Main Steam Line Break Analyses Project stage: Other ML20212M5601987-01-21021 January 1987 Advises That 840914,850102 & 1108 Supplemental Cycle 6 Analyses Sufficient for Satisfying NRC Request for Confirmatory Calculations.Acceptance of Retran Model Should Not Be Construed as Acceptance for Future Licensing Project stage: Acceptance Review 1984-04-13
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Category:CORRESPONDENCE-LETTERS
MONTHYEARDD-99-12, Informs That Time Provided by NRC Regulation within Which Commission May Act to Review DD-99-12 Has Expired.With Certificate of Svc.Served on 9910281999-10-28028 October 1999 Informs That Time Provided by NRC Regulation within Which Commission May Act to Review DD-99-12 Has Expired.With Certificate of Svc.Served on 991028 ML20217N8261999-10-25025 October 1999 Discusses Errata Re 991021 Filing of Northeast Nuclear Energy Co Answer to Request for Hearing & Petition to Intervene B17901, Submits Statement of Personal Qualification (NRC Form 398) Along with Supporting Certification of Medical Exam by Facility Licensee (NRC from 396) in Support of License Renewal for PM Miner.Encls Withheld,Per 10CFR2.790(a)(6)1999-10-18018 October 1999 Submits Statement of Personal Qualification (NRC Form 398) Along with Supporting Certification of Medical Exam by Facility Licensee (NRC from 396) in Support of License Renewal for PM Miner.Encls Withheld,Per 10CFR2.790(a)(6) B17886, Requests Permission to Utilize Code Case N-623, Deferral of Insps of Shell-to-Flange & Head-to-Flange of Reactor Vessel,Section Xi,Div 1, for Millstone Unit 21999-10-18018 October 1999 Requests Permission to Utilize Code Case N-623, Deferral of Insps of Shell-to-Flange & Head-to-Flange of Reactor Vessel,Section Xi,Div 1, for Millstone Unit 2 05000336/LER-1999-012, Forwards LER 99-012-00,re Unrecoverable CEA Misalignment Entry Into TS 3.0.3 on 990917.Commitments Made by Util Are Encl1999-10-15015 October 1999 Forwards LER 99-012-00,re Unrecoverable CEA Misalignment Entry Into TS 3.0.3 on 990917.Commitments Made by Util Are Encl B17900, Forwards Revised Assumptions Used in Fuel Handling Accident Analysis & Summary of Results.List of Regulatory Commitments Are Listed in Attachment 11999-10-14014 October 1999 Forwards Revised Assumptions Used in Fuel Handling Accident Analysis & Summary of Results.List of Regulatory Commitments Are Listed in Attachment 1 ML20217G9491999-10-14014 October 1999 Forwards Exemption from Requirements of 1-CFR50,App E, Section IV.F.2.c,re Conduct of full-participation Exercise in Sept 1999,at Plant,Units 1,2 & 3 ML20217D9671999-10-12012 October 1999 Forwards Copy of Transcript of Public Meeting Held by NRC Staff & NNECO on 990825 at Waterford,Connecticut on Decommissioning Program for Millstone,Unit 1.Without Encl ML20217D3011999-10-0707 October 1999 Forwards Request for Addl Info Re Util 990118 Request for Amend to License NPF-49 to Allow full-core Offloads to Spent Fuel Pool During Core Offloads to Spent Fuel Pool During Core Offload Events ML20217F0031999-10-0606 October 1999 Forwards Original Petition to Intervene Being Filed on Behalf of Clients,Connecticut Coalition Against Millstone & Long Island Coalition Against Millstone,Iaw Provisions of 10CFR2.714 ML20217P1201999-10-0606 October 1999 Informs NRC of Proposed Acquisition of Parent Holding Company of Central Maine & Requests NRC Concurrence,Based on Threshold Review,That Proposed Acquisition Does Not,In Fact, Constitute Transfer Subject to 10CFR50.80 B17892, Requests Withdrawal of License Amend Application Re 24-month SG Tube Insp Surveillance Extensions,Submitted in Util 950726 & s to NRC1999-10-0505 October 1999 Requests Withdrawal of License Amend Application Re 24-month SG Tube Insp Surveillance Extensions,Submitted in Util 950726 & s to NRC ML20217B4711999-10-0404 October 1999 Informs That Staff Did Not Identify Any Safety Concerns Re Licensee Proposals to Modify Commitments Made for Action Items 4.2.1,4.2.2,4.5.1 & 4.5.2 of GL 83-28 by Providing Addl Justifications or Safety Bases for Changes ML20212K1241999-10-0101 October 1999 Responds to Recent Ltrs to Chairman Jackson,Commissioners & Wd Travers,Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performace of Millstone to Ensure That Public Health & Safety,Adequately Protected ML20212J3051999-10-0101 October 1999 Discusses GL 97-06 Re Degradation of SG Internals,Dtd 971230.GL Requested Each PWR Licensee to Submit Info That Will Enable NRC Staff to Verify Whether PWR SG Internals Comply & Conform to Current Licensing Basis for Facilities ML20212L2081999-10-0101 October 1999 Responds to Recent Ltrs to President Wj Clinton,Chairman Jackson & Commissioners & Wd Travers,Expressing Concerns Re Millstone NPPs & Continued Lack of Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance ML20212J9991999-10-0101 October 1999 Responds to Recent Ltr to President Clinton,H Clinton, Chairman Jackson &/Or Wd Travers Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performance of Plant to Ensure That Public Health & Safety Adequately Protected ML20212L1971999-10-0101 October 1999 Responds to Recent Ltr to Chairman Jackson & Commissioners Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance to Ensure Public Health & Safety ML20212J2451999-10-0101 October 1999 Informs That Util 980807 & 990629 Responses to GL 98-01, Y2K Readiness of Computer Sys at NPPs Acceptable.Nrc Considers Subj GL to Be Closed for Units 2 &3 ML20212L1831999-10-0101 October 1999 Responds to Recent Ltr to Wd Travers Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Performance of Millstone to Ensure Adequate Protection to Public Health ML20212L2171999-10-0101 October 1999 Responds to Recent Ltr to President Wj Clinton,Chairman Jackson & Commissioners,Wd Travers & Ferc,Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island ML20217A9271999-09-30030 September 1999 Discusses Investigation Conducted at Millstone Nuclear Power Station by NRC OI Region I on 980319 to Determine If Contract Training Instructor Was Terminated for Raising Concerns About Quality of Training Matls ML20217B3221999-09-30030 September 1999 Refers to Investigation Rept 1-1997-035 Conducted at Millstone Nuclear Power Station by NRC Ofc of Investigation Field Ofc,Region I on 970915 to Determine Whether Former Health Physics Technician Discriminated Against ML20212J6621999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Units 2 & 3 on 990916.Identified Several Recent Instances in Which Condition Repts Were Not Initiated,Resulting in Untimely or Inadequate C/As.Historical Listing of Plant Issues Encl B17887, Requests Exemption from Requirements of 10CFR140.11(a)(4) Which Requires Licensees to Maintain Secondary Financial Protection Beyond Primary Layer1999-09-28028 September 1999 Requests Exemption from Requirements of 10CFR140.11(a)(4) Which Requires Licensees to Maintain Secondary Financial Protection Beyond Primary Layer ML20216J1341999-09-28028 September 1999 Ltr Contract:Task Order 49, Millstone Units 2 & 3 Employee Concerns Program Insp, Under Contract NRC-03-98-021 B17883, Forwards Mnps Unit 3 ISI Summary Rept,Cycle 6, IAW ASME Section XI,IWA-62301999-09-27027 September 1999 Forwards Mnps Unit 3 ISI Summary Rept,Cycle 6, IAW ASME Section XI,IWA-6230 B17890, Provides Response to GL 99-02, Laboratory Testing of Nuclear-Grade Activated Charcoal1999-09-27027 September 1999 Provides Response to GL 99-02, Laboratory Testing of Nuclear-Grade Activated Charcoal B17888, Informs That There No Longer Exists Need to Maintain Millstone Unit 2 SRO License for CA Hines,License SOP-10741-01,effective 9909151999-09-24024 September 1999 Informs That There No Longer Exists Need to Maintain Millstone Unit 2 SRO License for CA Hines,License SOP-10741-01,effective 990915 B17884, Forwards NRC Form 536, Operator Licensing Exam Data, for Mnps,Units 2 & 3,per Administrative Ltr 99-031999-09-24024 September 1999 Forwards NRC Form 536, Operator Licensing Exam Data, for Mnps,Units 2 & 3,per Administrative Ltr 99-03 ML20212F4961999-09-20020 September 1999 Forwards Insp Repts 50-245/99-08,50-336/99-08 & 50-423/99-08 on 990615-0809.Four Violations of NRC Requirements Occurred & Being Treated as Ncvs,Consistent with App C of Enforcement Policy 05000336/LER-1999-001, Forwards LER 99-001-00 Re Thermal Reactor Power Limit That Was Exceeded.Commitments Made by Util Encl1999-09-20020 September 1999 Forwards LER 99-001-00 Re Thermal Reactor Power Limit That Was Exceeded.Commitments Made by Util Encl B17867, Requests Relief from Requirements of 10CFR50.55a(g),IAW ASME Section XI for Millstone,Unit 3.Util Requests Relief from Performing Visual Exam of Reactor Pressure Supports to Extent Required by Code for Class 1 Supports1999-09-17017 September 1999 Requests Relief from Requirements of 10CFR50.55a(g),IAW ASME Section XI for Millstone,Unit 3.Util Requests Relief from Performing Visual Exam of Reactor Pressure Supports to Extent Required by Code for Class 1 Supports B17865, Provides NRC Staff with Updated Proposed Rev of FSAR Section 14.6.3, Radiological Consequences of SG Tube Failure. Updated Proposed Rev Will Replace Info Provided in Attachment 3 of Initial Submittal1999-09-16016 September 1999 Provides NRC Staff with Updated Proposed Rev of FSAR Section 14.6.3, Radiological Consequences of SG Tube Failure. Updated Proposed Rev Will Replace Info Provided in Attachment 3 of Initial Submittal B17876, Informs That Util Will Adopt Last Approved Northeast Util QA Program (Nuqap) Tr,Rev 21,dtd 990630,as Unit 1 Nuqap,Per Decision to Permanently Cease Operations at Subject Plant1999-09-16016 September 1999 Informs That Util Will Adopt Last Approved Northeast Util QA Program (Nuqap) Tr,Rev 21,dtd 990630,as Unit 1 Nuqap,Per Decision to Permanently Cease Operations at Subject Plant B17882, Forwards NRC Forms 398 & 369 in Support of License Renewal for Bb Parrish,License SOP-10399-2.Encl Withheld Per 10CFR2.790(a)(6)1999-09-15015 September 1999 Forwards NRC Forms 398 & 369 in Support of License Renewal for Bb Parrish,License SOP-10399-2.Encl Withheld Per 10CFR2.790(a)(6) B17881, Forwards NRC Form 398 & NRC Form 396 for Le Olsen,License SOP-10398-2.Encl Withheld Per 10CFR2.790(a)(6)1999-09-15015 September 1999 Forwards NRC Form 398 & NRC Form 396 for Le Olsen,License SOP-10398-2.Encl Withheld Per 10CFR2.790(a)(6) B17859, Forwards up-to-date Distribution Lists for NRC Correspondence to NNECO & NUSCO.Side-bars Indicate Changes from Previous Lists Provided to NRC on 9801281999-09-15015 September 1999 Forwards up-to-date Distribution Lists for NRC Correspondence to NNECO & NUSCO.Side-bars Indicate Changes from Previous Lists Provided to NRC on 980128 B17880, Forwards NRC Form 398 & NRC Form 396 for Rf Martin,License SOP-10397-0.Encls Withheld Per 10CFR2.790(a)(6)1999-09-15015 September 1999 Forwards NRC Form 398 & NRC Form 396 for Rf Martin,License SOP-10397-0.Encls Withheld Per 10CFR2.790(a)(6) B17872, Informs of Election to Consolidate Previous Commitments Re Work Observation Program with Two New Programmatic Commitments Listed in Attachment 11999-09-14014 September 1999 Informs of Election to Consolidate Previous Commitments Re Work Observation Program with Two New Programmatic Commitments Listed in Attachment 1 ML20212A9011999-09-10010 September 1999 Forwards Environ Assessment & Finding of No Significant Impact Re Application for Exemption,Dtd 990803.Proposed Exemption Would Provide Relief from Requirement of 10CFR50 ML20212A3171999-09-10010 September 1999 Discusses Investigation Rept 1-1998-045 Conducted on 981112 to Determine If Former Senior Health Physics Technician Being Denied Employment at Millstone in Retaliation for Having Raised Safety Concerns in Past.Synopsis Encl B17838, Forwards Revs 34 & 35 to Physical Security Plan.Explanation of Changes Provided as Attachment 1.Without Encls1999-09-10010 September 1999 Forwards Revs 34 & 35 to Physical Security Plan.Explanation of Changes Provided as Attachment 1.Without Encls ML20212A7501999-09-10010 September 1999 Forwards Staff Requirements Memo Response,Dtd 990525,which Provides Actions NRC Plans for Continued Oversight of safety-conscious Work Environ & Employee Concerns Program ML20211J9291999-09-0303 September 1999 Forwards mark-ups & Retypes of Proposed Conforming License Changes Required in Connection with Transfers Being Sought in 990615 Application of Montaup Electric Co & New England Power Co for Transfer of Licenses & Ownership Interests ML20211K5171999-09-0202 September 1999 Expresses Appreciation for Support Provided for NRC Public Meeting on 990825 05000336/LER-1999-010, Forwards LER 99-010-00,documenting 990804 Event of Failure to Perform ASME Section XI IST on Pressurizer Relief Line Flow Control Sample Valve Following Maint Activities.List of Util Commitments Contained in Attachment 11999-09-0202 September 1999 Forwards LER 99-010-00,documenting 990804 Event of Failure to Perform ASME Section XI IST on Pressurizer Relief Line Flow Control Sample Valve Following Maint Activities.List of Util Commitments Contained in Attachment 1 ML20216H0591999-09-0202 September 1999 Responds to Re Issues Submitted by Cullen on Behalf of Several Petitioners Concerning Offsite Emergency Prepardeness for Millstone Nuclear Power Station ML20211N9241999-09-0101 September 1999 Forwards Document Classification Form for Insertion Into Emergency Planning Services Department Procedures ML20211H0741999-08-30030 August 1999 Discusses GL 92-01,Rev 1, Rv Structural Integrity, Issued by NRC on 950519 & NNECO Responses for Millstone Unit 2 & 980715.Informs That Staff Revised Info in Rvid & Released Info as Rvid Version 2 Based on Response Review 1999-09-30
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217N8261999-10-25025 October 1999 Discusses Errata Re 991021 Filing of Northeast Nuclear Energy Co Answer to Request for Hearing & Petition to Intervene B17886, Requests Permission to Utilize Code Case N-623, Deferral of Insps of Shell-to-Flange & Head-to-Flange of Reactor Vessel,Section Xi,Div 1, for Millstone Unit 21999-10-18018 October 1999 Requests Permission to Utilize Code Case N-623, Deferral of Insps of Shell-to-Flange & Head-to-Flange of Reactor Vessel,Section Xi,Div 1, for Millstone Unit 2 B17901, Submits Statement of Personal Qualification (NRC Form 398) Along with Supporting Certification of Medical Exam by Facility Licensee (NRC from 396) in Support of License Renewal for PM Miner.Encls Withheld,Per 10CFR2.790(a)(6)1999-10-18018 October 1999 Submits Statement of Personal Qualification (NRC Form 398) Along with Supporting Certification of Medical Exam by Facility Licensee (NRC from 396) in Support of License Renewal for PM Miner.Encls Withheld,Per 10CFR2.790(a)(6) 05000336/LER-1999-012, Forwards LER 99-012-00,re Unrecoverable CEA Misalignment Entry Into TS 3.0.3 on 990917.Commitments Made by Util Are Encl1999-10-15015 October 1999 Forwards LER 99-012-00,re Unrecoverable CEA Misalignment Entry Into TS 3.0.3 on 990917.Commitments Made by Util Are Encl B17900, Forwards Revised Assumptions Used in Fuel Handling Accident Analysis & Summary of Results.List of Regulatory Commitments Are Listed in Attachment 11999-10-14014 October 1999 Forwards Revised Assumptions Used in Fuel Handling Accident Analysis & Summary of Results.List of Regulatory Commitments Are Listed in Attachment 1 ML20217P1201999-10-0606 October 1999 Informs NRC of Proposed Acquisition of Parent Holding Company of Central Maine & Requests NRC Concurrence,Based on Threshold Review,That Proposed Acquisition Does Not,In Fact, Constitute Transfer Subject to 10CFR50.80 ML20217F0031999-10-0606 October 1999 Forwards Original Petition to Intervene Being Filed on Behalf of Clients,Connecticut Coalition Against Millstone & Long Island Coalition Against Millstone,Iaw Provisions of 10CFR2.714 B17892, Requests Withdrawal of License Amend Application Re 24-month SG Tube Insp Surveillance Extensions,Submitted in Util 950726 & s to NRC1999-10-0505 October 1999 Requests Withdrawal of License Amend Application Re 24-month SG Tube Insp Surveillance Extensions,Submitted in Util 950726 & s to NRC B17887, Requests Exemption from Requirements of 10CFR140.11(a)(4) Which Requires Licensees to Maintain Secondary Financial Protection Beyond Primary Layer1999-09-28028 September 1999 Requests Exemption from Requirements of 10CFR140.11(a)(4) Which Requires Licensees to Maintain Secondary Financial Protection Beyond Primary Layer B17883, Forwards Mnps Unit 3 ISI Summary Rept,Cycle 6, IAW ASME Section XI,IWA-62301999-09-27027 September 1999 Forwards Mnps Unit 3 ISI Summary Rept,Cycle 6, IAW ASME Section XI,IWA-6230 B17890, Provides Response to GL 99-02, Laboratory Testing of Nuclear-Grade Activated Charcoal1999-09-27027 September 1999 Provides Response to GL 99-02, Laboratory Testing of Nuclear-Grade Activated Charcoal B17884, Forwards NRC Form 536, Operator Licensing Exam Data, for Mnps,Units 2 & 3,per Administrative Ltr 99-031999-09-24024 September 1999 Forwards NRC Form 536, Operator Licensing Exam Data, for Mnps,Units 2 & 3,per Administrative Ltr 99-03 B17888, Informs That There No Longer Exists Need to Maintain Millstone Unit 2 SRO License for CA Hines,License SOP-10741-01,effective 9909151999-09-24024 September 1999 Informs That There No Longer Exists Need to Maintain Millstone Unit 2 SRO License for CA Hines,License SOP-10741-01,effective 990915 05000336/LER-1999-001, Forwards LER 99-001-00 Re Thermal Reactor Power Limit That Was Exceeded.Commitments Made by Util Encl1999-09-20020 September 1999 Forwards LER 99-001-00 Re Thermal Reactor Power Limit That Was Exceeded.Commitments Made by Util Encl B17867, Requests Relief from Requirements of 10CFR50.55a(g),IAW ASME Section XI for Millstone,Unit 3.Util Requests Relief from Performing Visual Exam of Reactor Pressure Supports to Extent Required by Code for Class 1 Supports1999-09-17017 September 1999 Requests Relief from Requirements of 10CFR50.55a(g),IAW ASME Section XI for Millstone,Unit 3.Util Requests Relief from Performing Visual Exam of Reactor Pressure Supports to Extent Required by Code for Class 1 Supports B17876, Informs That Util Will Adopt Last Approved Northeast Util QA Program (Nuqap) Tr,Rev 21,dtd 990630,as Unit 1 Nuqap,Per Decision to Permanently Cease Operations at Subject Plant1999-09-16016 September 1999 Informs That Util Will Adopt Last Approved Northeast Util QA Program (Nuqap) Tr,Rev 21,dtd 990630,as Unit 1 Nuqap,Per Decision to Permanently Cease Operations at Subject Plant B17865, Provides NRC Staff with Updated Proposed Rev of FSAR Section 14.6.3, Radiological Consequences of SG Tube Failure. Updated Proposed Rev Will Replace Info Provided in Attachment 3 of Initial Submittal1999-09-16016 September 1999 Provides NRC Staff with Updated Proposed Rev of FSAR Section 14.6.3, Radiological Consequences of SG Tube Failure. Updated Proposed Rev Will Replace Info Provided in Attachment 3 of Initial Submittal B17881, Forwards NRC Form 398 & NRC Form 396 for Le Olsen,License SOP-10398-2.Encl Withheld Per 10CFR2.790(a)(6)1999-09-15015 September 1999 Forwards NRC Form 398 & NRC Form 396 for Le Olsen,License SOP-10398-2.Encl Withheld Per 10CFR2.790(a)(6) B17880, Forwards NRC Form 398 & NRC Form 396 for Rf Martin,License SOP-10397-0.Encls Withheld Per 10CFR2.790(a)(6)1999-09-15015 September 1999 Forwards NRC Form 398 & NRC Form 396 for Rf Martin,License SOP-10397-0.Encls Withheld Per 10CFR2.790(a)(6) B17859, Forwards up-to-date Distribution Lists for NRC Correspondence to NNECO & NUSCO.Side-bars Indicate Changes from Previous Lists Provided to NRC on 9801281999-09-15015 September 1999 Forwards up-to-date Distribution Lists for NRC Correspondence to NNECO & NUSCO.Side-bars Indicate Changes from Previous Lists Provided to NRC on 980128 B17882, Forwards NRC Forms 398 & 369 in Support of License Renewal for Bb Parrish,License SOP-10399-2.Encl Withheld Per 10CFR2.790(a)(6)1999-09-15015 September 1999 Forwards NRC Forms 398 & 369 in Support of License Renewal for Bb Parrish,License SOP-10399-2.Encl Withheld Per 10CFR2.790(a)(6) B17872, Informs of Election to Consolidate Previous Commitments Re Work Observation Program with Two New Programmatic Commitments Listed in Attachment 11999-09-14014 September 1999 Informs of Election to Consolidate Previous Commitments Re Work Observation Program with Two New Programmatic Commitments Listed in Attachment 1 B17838, Forwards Revs 34 & 35 to Physical Security Plan.Explanation of Changes Provided as Attachment 1.Without Encls1999-09-10010 September 1999 Forwards Revs 34 & 35 to Physical Security Plan.Explanation of Changes Provided as Attachment 1.Without Encls ML20211J9291999-09-0303 September 1999 Forwards mark-ups & Retypes of Proposed Conforming License Changes Required in Connection with Transfers Being Sought in 990615 Application of Montaup Electric Co & New England Power Co for Transfer of Licenses & Ownership Interests 05000336/LER-1999-010, Forwards LER 99-010-00,documenting 990804 Event of Failure to Perform ASME Section XI IST on Pressurizer Relief Line Flow Control Sample Valve Following Maint Activities.List of Util Commitments Contained in Attachment 11999-09-0202 September 1999 Forwards LER 99-010-00,documenting 990804 Event of Failure to Perform ASME Section XI IST on Pressurizer Relief Line Flow Control Sample Valve Following Maint Activities.List of Util Commitments Contained in Attachment 1 ML20216H0591999-09-0202 September 1999 Responds to Re Issues Submitted by Cullen on Behalf of Several Petitioners Concerning Offsite Emergency Prepardeness for Millstone Nuclear Power Station ML20211N9241999-09-0101 September 1999 Forwards Document Classification Form for Insertion Into Emergency Planning Services Department Procedures B17851, Forwards Semiannual fitness-for-duty Program Performance Data for 990101-990630 for Millstone Nuclear Power Station, Units 1,2 & 3,IAW 10CFR26.71(d)1999-08-27027 August 1999 Forwards Semiannual fitness-for-duty Program Performance Data for 990101-990630 for Millstone Nuclear Power Station, Units 1,2 & 3,IAW 10CFR26.71(d) B17855, Forwards NRC Forms 398 & 396 in Support of License Renewal for SRO TE Grilley,SOP-4053-04.Encl Withheld,Per 10CFR2.7901999-08-17017 August 1999 Forwards NRC Forms 398 & 396 in Support of License Renewal for SRO TE Grilley,SOP-4053-04.Encl Withheld,Per 10CFR2.790 B17849, Forwards Second Quarter Backlog Performance Rept for 1999, Which Represents Fourth Rept on Mnps Performance Since Restart of Unit 3 & First Status Update for Unit 2.No Regulatory Commitments Are Contained in Ltr1999-08-16016 August 1999 Forwards Second Quarter Backlog Performance Rept for 1999, Which Represents Fourth Rept on Mnps Performance Since Restart of Unit 3 & First Status Update for Unit 2.No Regulatory Commitments Are Contained in Ltr B17854, Forwards Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2,per TS 6.9.1.7.Revised Repts for May & June Also Encl Which Reflect Correct Faulty Printometer Readings1999-08-14014 August 1999 Forwards Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2,per TS 6.9.1.7.Revised Repts for May & June Also Encl Which Reflect Correct Faulty Printometer Readings B17850, Forwards First Lhc Quarterly Assessment Rept for Assessment Performed 990621 to 990701.NNECO Taking Appropriate Actions to Address Observations in Rept1999-08-11011 August 1999 Forwards First Lhc Quarterly Assessment Rept for Assessment Performed 990621 to 990701.NNECO Taking Appropriate Actions to Address Observations in Rept B17837, Forwards COLR for Cycle 7, for Millstone Unit 3,IAW TS 6.9.1.6.Explanation of Changes to COLR Also Encl1999-08-0707 August 1999 Forwards COLR for Cycle 7, for Millstone Unit 3,IAW TS 6.9.1.6.Explanation of Changes to COLR Also Encl B17657, Requests Schedular Exemption from Emergency Plan Exercise Requirements of 10CFR50,App E,Part Iv,Section F,Paragraph 2.c.Requests That Nrc/Fema Evaluated Exercise Be Conducted in Mar 2000 Rather than Sept 19991999-08-0303 August 1999 Requests Schedular Exemption from Emergency Plan Exercise Requirements of 10CFR50,App E,Part Iv,Section F,Paragraph 2.c.Requests That Nrc/Fema Evaluated Exercise Be Conducted in Mar 2000 Rather than Sept 1999 B17845, Forwards Revised Commitment for Surveillance Scheduling & Tracking.Options for Surveillance Scheduling & Tracking Methodologies to Be Incorporated in Standardized Station Surveillance Program Are Currently Being Reconsidered1999-08-0202 August 1999 Forwards Revised Commitment for Surveillance Scheduling & Tracking.Options for Surveillance Scheduling & Tracking Methodologies to Be Incorporated in Standardized Station Surveillance Program Are Currently Being Reconsidered B17831, Informs NRC Staff That Change 3 to Rev 25 of Mnps Emergency Plan Was Implemented on 990715.Change Removes Facility Organizational Charts from Emergency Plan & Identifies Relocation to Nuqap1999-07-26026 July 1999 Informs NRC Staff That Change 3 to Rev 25 of Mnps Emergency Plan Was Implemented on 990715.Change Removes Facility Organizational Charts from Emergency Plan & Identifies Relocation to Nuqap B17834, Forwards Proprietary Revised NRC Form 398,which Certifies That SL Doboe Has Completed Eligibility Requirements for Sro,Per 10CFR55.31.Proprietary Info Withheld1999-07-20020 July 1999 Forwards Proprietary Revised NRC Form 398,which Certifies That SL Doboe Has Completed Eligibility Requirements for Sro,Per 10CFR55.31.Proprietary Info Withheld B17836, Forwards Revised NRC Form 396 & Supporting Physician Rept for Licensed Operator Restricted from Licensed Duties, Effective 990628,due to Medical Condition.Without Encl1999-07-20020 July 1999 Forwards Revised NRC Form 396 & Supporting Physician Rept for Licensed Operator Restricted from Licensed Duties, Effective 990628,due to Medical Condition.Without Encl B17811, Submits Response to NRC AL 99-02,requesting That Licensees Provide Numerical Estimates of Licensing Actions to Be Expected to Be Submitted in Fy 2000 & 20011999-07-20020 July 1999 Submits Response to NRC AL 99-02,requesting That Licensees Provide Numerical Estimates of Licensing Actions to Be Expected to Be Submitted in Fy 2000 & 2001 ML20210S9911999-07-18018 July 1999 Requests NRC Intervene for All Shareholders of New England Electric System & to Help with Merger with National Grid Group & That NRC Petition Security & Exchange Commission to Investigate Matter Relative to No Shareholder Options B17835, Forwards Rev 33 to Millstone Station Physical Security Plan, Per 10CFR50.54(p)(2).Licensee Determined That Changes Do Not Decrease Effectiveness of Plan.Rev Withheld from Public Disclosure,Per 10CFR2.790(d)(1)1999-07-16016 July 1999 Forwards Rev 33 to Millstone Station Physical Security Plan, Per 10CFR50.54(p)(2).Licensee Determined That Changes Do Not Decrease Effectiveness of Plan.Rev Withheld from Public Disclosure,Per 10CFR2.790(d)(1) B17818, Provides NRC Staff with Change to TS Bases Sections 3/4.5.2 & 3/4.5.3, ECCS Subsystems for Info Only.Change Was Reviewed & Approved by Unit 3 Plant Operations Review Committee IAW Provisions of 10CFR50.591999-07-16016 July 1999 Provides NRC Staff with Change to TS Bases Sections 3/4.5.2 & 3/4.5.3, ECCS Subsystems for Info Only.Change Was Reviewed & Approved by Unit 3 Plant Operations Review Committee IAW Provisions of 10CFR50.59 B17824, Forwards Monthly Oeprating Rept for June 1999 & Revised Monthly Operating Rept for May 1999 for Millstone Unit 21999-07-13013 July 1999 Forwards Monthly Oeprating Rept for June 1999 & Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 ML20212K1701999-07-13013 July 1999 Submits Concerns Re Millstone & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Should Provide Adequate Emergency Planning in Case of Radiological Accident B17816, Provides Certification That M Lettrich,Has Completed Eligibility Requirements,Per 10CFR55.31 for Operator License.Util Requests That Licensing Action Be Taken for Named Individual1999-07-0101 July 1999 Provides Certification That M Lettrich,Has Completed Eligibility Requirements,Per 10CFR55.31 for Operator License.Util Requests That Licensing Action Be Taken for Named Individual B17801, Forwards 10CFR50.59 Annual Rept for Period Jan-Dec 1998. Various Changes That Were Initiated in Previous Yrs & Completed in 1998,also Incorporated Into Annual Rept1999-06-30030 June 1999 Forwards 10CFR50.59 Annual Rept for Period Jan-Dec 1998. Various Changes That Were Initiated in Previous Yrs & Completed in 1998,also Incorporated Into Annual Rept B17819, Forwards Rev 17 to FSAR & Addendum 6 to Annual Rept.Nneco Recently Completed Review of Unit 2 Design & Licensing Bases Which Resulted in Changes to FSAR Provided in Encl 1.Encl 2 Includes Info Covering Changes Not Included in1999-06-30030 June 1999 Forwards Rev 17 to FSAR & Addendum 6 to Annual Rept.Nneco Recently Completed Review of Unit 2 Design & Licensing Bases Which Resulted in Changes to FSAR Provided in Encl 1.Encl 2 Includes Info Covering Changes Not Included in B17780, Forwards Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) TR, IAW 10CFR50.54(a)(3).Changes to TR Are Shown as Text in Bold Italics1999-06-30030 June 1999 Forwards Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) TR, IAW 10CFR50.54(a)(3).Changes to TR Are Shown as Text in Bold Italics B17723, Responds to NRC Request for Info Re GL 98-01, Y2K Readiness of Computer Sys at Npps. Y2K Readiness Disclosure for Units 2 & 3 Encl.Without Encl1999-06-29029 June 1999 Responds to NRC Request for Info Re GL 98-01, Y2K Readiness of Computer Sys at Npps. Y2K Readiness Disclosure for Units 2 & 3 Encl.Without Encl B17767, Forwards Rev 12 to FSAR & Addendum 3 to Annual Rept, for Millstone Unit 3,per 10CFR50.71(e) & 10CFR50.4(b)(6). No New Regulatory Commitments Contained in Ltr1999-06-29029 June 1999 Forwards Rev 12 to FSAR & Addendum 3 to Annual Rept, for Millstone Unit 3,per 10CFR50.71(e) & 10CFR50.4(b)(6). No New Regulatory Commitments Contained in Ltr 1999-09-03
[Table view] Category:UTILITY TO NRC
MONTHYEARML20064A8071990-09-11011 September 1990 Forwards Core Operating Limits Rept for Four & Three Loop Operation,Per Tech Spec 6.9.1.6.d A08900, Responds to Expressing NRC Views on Access to Util Internal or third-party Assessment Repts.Believes Internal Analysis to Support Amend of One of Util NRC OLs to Authorize Higher Power Level Is within NRC Purview & Access1990-09-11011 September 1990 Responds to Expressing NRC Views on Access to Util Internal or third-party Assessment Repts.Believes Internal Analysis to Support Amend of One of Util NRC OLs to Authorize Higher Power Level Is within NRC Purview & Access B13628, Forwards Correction to Error Discovered in Util 900727 Response to Notice of Violation from Insp Rept 50-336/90-09. Statement Corrected to Read That Contract Personnel That Have long-term Assignments,Certified as Testing Personnel1990-09-0707 September 1990 Forwards Correction to Error Discovered in Util 900727 Response to Notice of Violation from Insp Rept 50-336/90-09. Statement Corrected to Read That Contract Personnel That Have long-term Assignments,Certified as Testing Personnel B13624, Forwards Addl Info Re Relief Request from ASME Code Section XI Requirements for Temporary Repair to Piping Adjacent to Valve 2-SW-97A,per 900817 Telcon1990-09-0505 September 1990 Forwards Addl Info Re Relief Request from ASME Code Section XI Requirements for Temporary Repair to Piping Adjacent to Valve 2-SW-97A,per 900817 Telcon A08977, Advises of Commitment to Install Hardened Wetwell Vent at Facility,In Response to NRC .Util Will Be Proceeding W/Initial Design & Engineering of Hardened Vent, to Support Installation During 1993 Refueling Outage1990-09-0404 September 1990 Advises of Commitment to Install Hardened Wetwell Vent at Facility,In Response to NRC .Util Will Be Proceeding W/Initial Design & Engineering of Hardened Vent, to Support Installation During 1993 Refueling Outage B13596, Forwards Millstone Unit 3 Individual Plant Exam for Severe Accident Vulnerabilities, Per Generic Ltr 88-20.Rept Identified That No Major Severe Accident Vulnerabilities Requiring Corrective Action Needed1990-08-31031 August 1990 Forwards Millstone Unit 3 Individual Plant Exam for Severe Accident Vulnerabilities, Per Generic Ltr 88-20.Rept Identified That No Major Severe Accident Vulnerabilities Requiring Corrective Action Needed B13626, Informs That Info Provided in Re safety-related Equipment Classification Programs Also Applicable for Unit 3 of Facility1990-08-31031 August 1990 Informs That Info Provided in Re safety-related Equipment Classification Programs Also Applicable for Unit 3 of Facility B13618, Forwards Addl Info on Util 900815 Relief Request from ASME Code Section XI Requirements,Per 10CFR50.55a(g)(6)(i),for Repairs to Pipe 3SWP-006-050-031990-08-24024 August 1990 Forwards Addl Info on Util 900815 Relief Request from ASME Code Section XI Requirements,Per 10CFR50.55a(g)(6)(i),for Repairs to Pipe 3SWP-006-050-03 ML20059C2061990-08-23023 August 1990 Forwards Vols 1 & 2 to Semiannual Radioactive Effluents Release Rept Jan-June 1990, Per 10CFR50.36a.Rept Includes Summary of Quantities of Solid Radwaste & Liquid & Gaseous Effluents A08918, Responds to Notice of Violation & Proposed Imposition of Civil Penalty Re Insp Rept 50-245/90-08.Mitigation of Civil Penalty Requested.Corrective Action:List of Procedural Changes Provided1990-08-22022 August 1990 Responds to Notice of Violation & Proposed Imposition of Civil Penalty Re Insp Rept 50-245/90-08.Mitigation of Civil Penalty Requested.Corrective Action:List of Procedural Changes Provided B13610, Requests Relief from ASME Boiler & Pressure Vessel Code Section XI Requirements Re Mods to Pipe 3SWP-006-050-03. Results of Insps & Required Repairs Will Determine Schedule for Future Insps1990-08-15015 August 1990 Requests Relief from ASME Boiler & Pressure Vessel Code Section XI Requirements Re Mods to Pipe 3SWP-006-050-03. Results of Insps & Required Repairs Will Determine Schedule for Future Insps B13595, Notifies NRC That Utils Volunteer to Participate in Emergency Response Data Sys Project for All Four Nuclear Units,Per Generic Ltr 89-15 & NUREG-13941990-08-14014 August 1990 Notifies NRC That Utils Volunteer to Participate in Emergency Response Data Sys Project for All Four Nuclear Units,Per Generic Ltr 89-15 & NUREG-1394 B13607, Requests Relief from ASME Code Section XI to Reflect Mod to Piping Adjacent to Valve 2-SW-97A,in Response to Generic Ltr 90-051990-08-10010 August 1990 Requests Relief from ASME Code Section XI to Reflect Mod to Piping Adjacent to Valve 2-SW-97A,in Response to Generic Ltr 90-05 A08845, Responds to NRC Backfit Analyses of Hardened Wetwell Vent, Contained in .Benefit of Installing Hardened Wetwell Vent to Satisfy Basic Design Objective of Preventing core-melt Event Not Sufficient for Immediate Decision1990-08-0808 August 1990 Responds to NRC Backfit Analyses of Hardened Wetwell Vent, Contained in .Benefit of Installing Hardened Wetwell Vent to Satisfy Basic Design Objective of Preventing core-melt Event Not Sufficient for Immediate Decision ML20058N2181990-08-0707 August 1990 Notification of Change in Senior Operator Status.Util Determined That Need to Maintain Senior OL of LS Allen No Longer Exists.Determination Effective 900719 ML20058M8321990-08-0707 August 1990 Discusses Spent Fuel Racks Poison Surveillance Coupon Boraflex Degradation.Visual Exam of Remaining Surveillance Coupons Revealed Similar Situation Existed in All Coupon Samples B13590, Responds to NRC 900718 Request for Addl Info Re Util 900418 Request for Schedular Exemption from 10CFR50,App E,Section IV.F.3 to Allow Dec 1990 Full Participation Exercise to Be Exchanged W/Oct 1991 Partial Participation Exercise1990-08-0101 August 1990 Responds to NRC 900718 Request for Addl Info Re Util 900418 Request for Schedular Exemption from 10CFR50,App E,Section IV.F.3 to Allow Dec 1990 Full Participation Exercise to Be Exchanged W/Oct 1991 Partial Participation Exercise A08881, Responds to NRC Re Violations Noted in Insp Rept 50-423/90-08.Corrective Action:Operators Directly Involved W/Event Removed from Licensed Duties & Counseled by Operations Manager on Causes of Event1990-07-31031 July 1990 Responds to NRC Re Violations Noted in Insp Rept 50-423/90-08.Corrective Action:Operators Directly Involved W/Event Removed from Licensed Duties & Counseled by Operations Manager on Causes of Event B13594, Forwards Rev 13 to Physical Security Plan.Rev Withheld (Ref 10CFR73.21(b) & 2.790(a))1990-07-30030 July 1990 Forwards Rev 13 to Physical Security Plan.Rev Withheld (Ref 10CFR73.21(b) & 2.790(a)) ML20055J4621990-07-27027 July 1990 Advises That Need to Maintain OL or Senior OL for Listed Individuals No Longer Exists,Effective 900701 B13585, Provides Supplemental Response to Generic Ltr 89-19 Re Request for Action Concerning Resolution of Unresolved Safety Issue A-47.Plant Procedures Modified to Provide Operability Verification of Steam Generator Protection Sys1990-07-26026 July 1990 Provides Supplemental Response to Generic Ltr 89-19 Re Request for Action Concerning Resolution of Unresolved Safety Issue A-47.Plant Procedures Modified to Provide Operability Verification of Steam Generator Protection Sys A08565, Responds to NRC 900302 Request for Addl Info Re LPCI Swing Bus Transfer Design & Single Failure Vulnerabilities1990-07-26026 July 1990 Responds to NRC 900302 Request for Addl Info Re LPCI Swing Bus Transfer Design & Single Failure Vulnerabilities B13592, Requests Extension to Respond to NRC Backfit Analyses of Hardened Wetwell Vent1990-07-24024 July 1990 Requests Extension to Respond to NRC Backfit Analyses of Hardened Wetwell Vent ML20063P9791990-07-23023 July 1990 Notification of Change in SL Jackson Status Effective 900701,due to Permanent Reassignment within Util B13563, Discusses Util Comprehensive Review of Options Re Degraded Grid Undervoltage Protection.Confirms Previous Conclusion That Splitting Loss of Normal Power Logic Would Have Overall Adverse Impact on Plant Safety1990-07-20020 July 1990 Discusses Util Comprehensive Review of Options Re Degraded Grid Undervoltage Protection.Confirms Previous Conclusion That Splitting Loss of Normal Power Logic Would Have Overall Adverse Impact on Plant Safety B13566, Advises That Util Has Reasonable Assurance That Safety Relief Valves Operable & Will Perform as Expected Until Next Outage1990-07-20020 July 1990 Advises That Util Has Reasonable Assurance That Safety Relief Valves Operable & Will Perform as Expected Until Next Outage B13588, Corrects 900703 Submittal of Results of Second in-cycle Insp of Steam Generators.All Tubes W/Cracks Stacked & Plugged1990-07-18018 July 1990 Corrects 900703 Submittal of Results of Second in-cycle Insp of Steam Generators.All Tubes W/Cracks Stacked & Plugged A08822, Submits Addl Info Requested Re Util Response to Generic Ltr 88-11, Radiation Embrittlement of Reactor Vessel Matls. Charpy Impact Use Values for Welds Provided in Evaluation of Irradiated Capsule W-971990-07-18018 July 1990 Submits Addl Info Requested Re Util Response to Generic Ltr 88-11, Radiation Embrittlement of Reactor Vessel Matls. Charpy Impact Use Values for Welds Provided in Evaluation of Irradiated Capsule W-97 ML20055G5331990-07-18018 July 1990 Forwards Decommissioning Financial Assurance Certification Rept B13587, Requests Temporary Waiver of Compliance from Tech Spec 3.5.F.2 Re Emergency Diesel Generator (EDG) Limiting Condition for Operation.Waiver Would Extend Available Time to Repair Damaged Electrical Components1990-07-16016 July 1990 Requests Temporary Waiver of Compliance from Tech Spec 3.5.F.2 Re Emergency Diesel Generator (EDG) Limiting Condition for Operation.Waiver Would Extend Available Time to Repair Damaged Electrical Components ML20055D3461990-07-0303 July 1990 Responds to NRC Bulletin 90-001 Re Loss of Fill Oil Transmitters Mfg by Rosemount.Operability Determinations Performed & Documented for All Rosemount 1153 & 1154 Transmitters at Facility B13545, Forwards Rev 3 to Updated FSAR for Millstone Unit 31990-06-29029 June 1990 Forwards Rev 3 to Updated FSAR for Millstone Unit 3 ML20055D7191990-06-29029 June 1990 Amends 900604 Rev 13 to QA Program ML20055D3481990-06-29029 June 1990 Forwards Addl Info Re Facility Crdr & Isap,Including Justification for Human Engineering Discrepancies Dispositioned for No Corrective Action B13531, Forwards Rev 8 to Updated FSAR for Millstone Unit 21990-06-29029 June 1990 Forwards Rev 8 to Updated FSAR for Millstone Unit 2 B13550, Responds to Generic Ltr 90-04, Request for Info on Status of Generic Safety Issues Resolved W/Imposition of Requirements or Corrective Actions. Implementation & Completion Tables for staff-imposed Requirements Encl1990-06-27027 June 1990 Responds to Generic Ltr 90-04, Request for Info on Status of Generic Safety Issues Resolved W/Imposition of Requirements or Corrective Actions. Implementation & Completion Tables for staff-imposed Requirements Encl B13499, Forwards Corrected Tech Specs Page 3/4 9-1 for Incorporation Into Proposed Amend 36 to License DPR-21 Re Auxiliary Electrical Sys1990-06-26026 June 1990 Forwards Corrected Tech Specs Page 3/4 9-1 for Incorporation Into Proposed Amend 36 to License DPR-21 Re Auxiliary Electrical Sys ML20043F8721990-06-11011 June 1990 Corrects Name of Vendor Supplying Replacement Plug Valves, Per Util 900511 Ltr.Replacement Bolts,Not Valves,Purchased from Cardinal Industrial Products Corp ML20043H0161990-06-0808 June 1990 Requests Exemption from App J to 10CFR50 for 12 Valves in Reactor Bldg Closed Cooling Water Sys.Valves Not within Definition of Containment Isolation Valves in App J & Not Required to Be Tested ML20043E8831990-06-0505 June 1990 Requests NRC Authorization to Use Plugs Fabricated of nickel-chromium-iron Uns N-06690 Matl Alloy 690 to Plug Tubes in Steam Generators of Plant ML20043D0451990-05-30030 May 1990 Discusses Proposed Rev to Tech Specs Re Facility ESF Actuation Sys Instrumentation Trip Setpoint,Per 900330 Ltr ML20042H0311990-05-0909 May 1990 Discusses Steam Generator Safety Assessment.Concludes That Continued Operation Through Remainder of Current Cycle 10 Fully Justified ML20042F0941990-04-30030 April 1990 Provides Addl Info Re Environ Impact of 900226 Application for Amend to License NPF-49,revising Tech Specs to Allow Containment Pressure to Increase to 14 Psia During Modes 1-4,per NRC Request ML20042F0661990-04-30030 April 1990 Responds to NRC 900404 Ltr Re Violations Noted in Safety Insp Rept 50-336/90-01 on 900120-0305.Corrective Action:Ler 90-004 Submitted on 900430 to Document Condition Prohibited by Plant Tech Specs ML20042E8331990-04-27027 April 1990 Forwards Annual Environ Protection Plan Operating Rept for 1989, & Monitoring Marine Environ of Long Island Sound at Millstone Nuclear Power Station Annual Rept 1989. ML20012E2681990-03-23023 March 1990 Responds to NRC 900226 Ltr Re Violations Noted in Insp Rept 50-423/89-23.Corrective Actions:Requirement to Review All Changes on Safety Sys for Potential Operating Procedure Changes Stressed to Operations & Engineering Personnel ML20012C3141990-03-13013 March 1990 Forwards Info Re Insp of Facility Emergency Operating Procedures,Per 900119 Ltr ML20012B4111990-03-0202 March 1990 Provides Addl Info Requested to Clarify Changes Proposed to Tech Spec Action Statements for Inoperable Accumulator B13453, Advises That Mods to Steam Generator Blowdown Sample Sys Completed,Per Violations Noted in Insp Rept 50-423/89-14 & Salp.Sys Will Be Evaluated for Next 2 Wks to Ensure Blowdown Radiation Monitor Operating Reliably1990-02-26026 February 1990 Advises That Mods to Steam Generator Blowdown Sample Sys Completed,Per Violations Noted in Insp Rept 50-423/89-14 & Salp.Sys Will Be Evaluated for Next 2 Wks to Ensure Blowdown Radiation Monitor Operating Reliably ML20011F7541990-02-26026 February 1990 Notifies That Jh Parillo Reassigned & No Longer in Need of License SOP-10263-2 as of 900219 1990-09-07
[Table view] |
Text
IR s
General Offices
- Seiden Street, Berlin, Connecticut HARTFORD. CONNECTICUT 06141-0270 L L T J Z',"O'C,g"" (203) 665-5000 September 14,1984 Docket No. 50-336 Bil286 A03722 Director of Nuclear Reactor Regulation Attn: Mr. James R. Miller Operating Reactors Branch #3 U. S. Nuclear Regulatory Commission Washington, D. C. 20555
References:
(1) K. L. Heitner letter to W. G. Counsil, dated December 30, 1983.
(2) W. G. Counsil letter to 3. R. Miller, dated February 1,1984.
Gentlemen:
Millstone Nuclear Power Station, Unit No. 2 Followup Actions to Amendment No. 90 to Operating License No. DPR-65 The NRC Staff forwarded Amendment No. 90 to Facility Operating License No.
DPR-65 in Reference (1). The amendment au:horized Cycle 6 operation for Millstone Unit No. 2. The NRC Safet; Evaluation Report (SER) accompanying the amendment addressed various aspects of the core reload including the accident analysis evaluations submitted to support Cycle 6 operation. The Staff documented several concerns relating to the large break loss-of-coolant, steam line break and steam generator tube rupture accident evaluations submitted to support Cycle 6 operation of the plant following the core reload and thermal shield removal.
Northeast Nuclear Energy Company (NNECO) addressed the majority of the concerns identifled in the Cycle 6 SER in Reference (2). The Staff concerns were further discussed at length with Mr. Jack Guttman and representatives from Argonne National Laboratories (ANL) during a meeting at NNECO corporate offices in February,1984.
The purpose of this submittal is to address the concerns identified in Reference (1), as clarified in the February meeting with :he NRC and ANL, and to provide the information which NNECO committed to submit daring the February meeting. Specifically, the at:achment hereto addresses the following issues for Millstone Unit No. 2:
1.
Justification for the large break loss-of-coolant evaluation performed to support Cycle 6 operation without the thermal shield.
\
8409260261 840934 Y PDR ADOCK 05000336 'h g
2-
- 2. ' Discussion of efforts to evaluate the steam line break accident assuming
- limited mixing.
- 3. The results of our evaluation of the steam generator tube rupture event considering the effects of potential reactor vessel upper head voiding.
i.(NNECO agreed to pro ride this information during the February,1984 meeting with ANL).
- 4. Conformance to General Design Criterion 17 and its applicability to the steam line break analysis performed to support Cycle 6 operation.
The attached information is Intended to resolve the concerns identified by the Staff in Reference (1) and as discussed during the February,1984 meeting.
NNECO intends to review the groundrules document for reload safety analyses with the fuel vendor to ensure that appropriate assumptions are made which reflect the licensing and design bases for Millstone Unit No. 2. Based on the information reviewed to date it is expected that no changes will be required to the reload safety analyaes assumptions to reflect the bases on which Millstone Unit No. 2 was licensed to operate.
We wish to point out that differences identified by either ourselves or the Staff between current licensing criteria and historical practices at Millstone Unit No. 2 are not automatically deemed appropriate for inclusion in the Mllistone Unit No. 2 licensing basis. In any event, the Cycle 7 reload reanalysis effort will reflect the appropriate plant design and licensing bases.
We trust you find this inf rmation satisfactory.
L Very truly yours, NORTHEAST NUCLEAR ENERGY COMPANY 191d '
W. G. Counsil ~~
Senior Vice President
r; h
s -
l /-
1 Docket No. 50-336 i-Attachment Millstone Nuclear Power Station, Unit'No. 2 Additional Information Supporting the Cycle 6 Reload Safety Analyses i-August,1984 L. .. . . .. .
- 1. Impact of Thermal Shield Removal on the Cycle 6 Large Break LOCA Evaluation The Reference (1) report provided the results of analyses and evaluations of operation of Millstone Unit No. 2 without a thermal shield. Our fuel vendor performed a detailed review of the large break LOCA model for Millstone Unit No. 2 to determine what impacts the removal of the thermal shield would have on the limiting large break LOCA analysis results. This review coupled with the fuel vendor's extensive experience in the area of accident analyses formed the basis for the conclusions documented in Reference (1). The results of the review of the large break LOCA model for Millstone Unit No. 2 did not justify a need to perform a reanalysis of the accident.
Section 8.2.3 of Reference (1) included a discussion of the impact of removing the thermal shield on the large break LOCA analysis. The thermal hydraulic phenomena associated with the transient were evaluated for the system design change and the results of expected system response changes negligible with or respect of a beneficial to peak nature clad temp a lower (erature ultimate were determined peak clad to be temperature). We refer you to Reference (1) for the detailed discussion of these effects. Several effects were identified which will benefit the PCT while other effects were identified which will adversely effect the PCT.
The integrated effects, however, would be expected to result in a negligible beneficial change in the PCT calculated for the large break LOCA analysis. The evaluation of the thermal hydraulic phenomena was based on numerous LOCA analyses and sensitivity studies performed by our fuel vendor in which the individual blowdown and reflood hydraulic phenomena were observed. These data supported the qualitative assessment documented in Reference (1).
The conclusions presented in Reference (1) are further substantiated by the j results of large break LOCA evaluations performed for another plant of essentially identical design which recently removed its thermal shield.
NNECO is confident that the results of the evaluations of the large break LOCA analysis for the plant design change of removing the thermal shield
[ are accurate. A reanalysis of this event solely for this design change is not considered necessary nor a prudent resource expenditure. The plant design change has been incorporated into the reload safety analysis checklist and will be reflected in future safety analyses for Millstone Unit No. 2.
This information is considered responsive to the Reference (2) request for additionalinformation regarding large break LOCA PCT.
- 2. Steam Line Break Accident Assuming Limited Mixing An evaluation of the steam line break event for Millstone Unit No. 2 is underway to address the NRC Staff concern regarding mixing factors assumed for the broken loop. Preliminary results of this evaluation indicate no significant changes to previous conclusions which assumed good mixing.
4 The analysis is being performed assuming limited mixing between the
. reactor vessel inlet and outlet loops containing the broken and intact steam generators.
- NNECO will provide the Staff with results of this evaluation when they are
' finalized.
- 3. Effects of Upper Head Voldinst on the Results of the Steam Generator Tube Ruoture Event with increased Safety Valve Blowdown ~
During .the February,' 1984 meeting between NNECO, the NRC Staff and ANL representatives, the steam generator tube rupture evaluation was discussed at length. The effects of reactor vessel upper head modeling and ,
steam generator safety valve blowdown characteristics were addressed.
NNECO committed to provide the Staff the results of an evaluation of reactor vessel upper head. voiding on the steam generator tube rupture accident assuming a 12% safety valve blowdown. NNECO had previously-provided the results of the ube rupture analysis considering upper head -
voiding in Reference (3); however this evaluation assumed the _ steam generator safety valves reseat at their opening pressures. The impact of
- additional safety valve blowdown was addressed in Reference (4). This calculation provides the results considering the combined effects ' of potential upper head voiding and the worst case safety valve blowdown s12%). -
The results of this evaluation are summarized below.
^
Head voiding would cause a less rapid primary system depressurization and result In an increase in primary-to-secondary system break flow following reactor. trip. The slower depressurization is caused by flashing of the hot' water contained in the relatively stagnant head region. The calculation was performed with RETRAN02 MOD 002. Although this calculation does -
- not specifically represent the upper head in RETRAN,' It conservatively bounds the.possible increase .in flow from the primary system into the steam generator that ' might be caused by upper head volding. The maximum post-trip pressure -drop between the primary and secondary systems corresponds to the saturation pressure of the upper head region (1600 psla).minus the steam-generator safety valve closing pressure (870
. psia assuming 12% blowdown). The increased break flow based on these conditions was modeled in RETRAN as a fill junction with a constant flow rate for- the time following reactor trip. Since the increased break flow is ~
modeled as a fill junction, the primary system response in this evaluation is essentially the same as that in Reference (4). Prior to reactor trip, the
. break flow is calculated identically to the Reference (4) calculation. A comparison between the break flow calculated in Reference (4) and this evaluation is shown in Figure 1.
' This analysis predicts that the increase in steam flow to the environment caused by head volding is bounded by 1.2 percent compared to the worst-case analysis presented in Reference (4).
1
lThe radiological dose for the worst case presented in Reference (4) is less than 1 Rem. . The increase in offsite dose caused by an increase in steam release to the atmosphere of 1.2 percent is small and well within the 10CFR100 limits. It is therefore concluded that the effects of head voiding on the analyzed consequences of the Millstone Unit No. 2 steam generator tube rupture are negligible.
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- 4. Conformance to General Design Criterion 17 for the Steam Line Break Event Millstone Unit No. 2 was granted an operating license in August,1975. The NRC Staff Safety Evaluation Report (SER) supporting the operating license was issued on May 10, 1974. Based on a review of the original SER, the NRC Staff (at the time the Atomic Energy Commission Staff) assessed the design of Millstone Unit No. 2 against the General Design Criteria (GDC) in effect as of February 20,1971. The staff concluded that the plant design conformed to the intent of the GDC.
The Staff review, as documented in the SER, concluded that the onsite and offsite electric power system conformed to the requirements of GDC 17 and 18. Clearly, this conclusion was based upon a combination of information provided by NNECO as well as the Staff's independent review.
It is obvious that the regulatory review criteria have increased in scope and depth since Millstone Unit No. 2 was licensed in 1975. In fact, the Systematic Evaluation Program (SEP) was initiated, in part, as a result of the changes in licensing criteria and eleven of the oldest nuclear power plants were reviewed to determine their level of conformance to current licensing criteria. Millstone Unit No. 2 was not evaluated in the SEP.
Plant licensing and safety analyses performed to support reloads as well as other plant design changes have reflected bases established on the docket since the original Staff SER was issued. The volume of documentation is extensive and includes five refuelings, a power uprating, and a change in fuel vendors. The power uprating and fuel vendor change both involved a reanalysis of the transients and accidents included in the licensing basis. In all cases, favorable NRC Staff review and approval for continued operation was obtained, and the bases for those conclusions was clearly articulated.
NNECO's position regarding conformance to the GDC is predicated on the original plant design, as documented in the FSAR, and the Staff review of that design and analysis as documented in the SER, as amended and supplemented in docketed correspondence.
In accordance with 10CFR50.59, NNECO makes changes to the plant design and operation without NRC Staff approval if the changes do not involve an unreviewed safety question or require a change to the Technical Specifications. The tests delineated in 10CFR50.59(a)(2) are performed against the docketed FSAR, as updated annually. When a reload is evaluated under 10CFR50.59, the bases for the conclusions regarding the unreviewed safety question determinations are the transient and accident analyses included in the FSAR. No attempt is automatically made to evaluate how SRP revisions or other regulatory guidance might impact the determinations if they were applied.
The Cycle 6 reload safety analyses were reviewed against the FSAR to determine, in accordance with 10CFR50.59, if the refueling constituted an unreviewed safety question. The Cycle 6 safety analyses were performed in a manner consistent with past practices and methodologies which have been reviewed and approved by the NRC Staff.
Subsequently, the Staff has questioned the appropriateness of assumptions utilized in the Cycle 6 steam line break analysis regarding the availability
. of off-site power. A review of the impact of assuming loss of off-site power coincident with a steam line break has been performed. . The purpose of this review was not to alter the Cycle 6 submittal, but to provide assurance that NNECO has reasonably bounded the worst case for Millstone Unit No. 2. This review has utilized an evaluation which was performed for the Cycle 5 analysis. Because both Cycle 5 and Cycle 6 have very similar
. boundary conditions, the conclusions of the Cycle 5 evaluation are fully applicable to Cycle 6.
In the case of a steam line break with a loss of off-site power, an additional delay is assumed following the generation'of a safety. injection signal to start the diesel generators and to commence loading of the safety injection equipment. Since the reactor coolant pumps are coasting down with a loss of off-site power, the ability of the affected steam generator to extract heat from the reactor coolant system is reduced. Considering moderator fee &ack, a reduction in reactor coolant flow will result in a slower reactivity insertion rate due to the cooldown since the rate of water density increase would be reduced. The minimum approach to criticality will occur later in the transient and the core power increase will be slower
. than in the similar case with off-site power. In both cases, significant margin to DNB exists. The studies with and without off-site power available, which were performed for Cycle 5, were not carried to completion due to the significant DNB margin available.
The steam line break analysis submittal for Millstone Unit No. 2 Cycle 6 is reasonably representative of the limiting case. The Cycle 5 study indicates that ample margin exists . for cases with and without off-site power available and that the impact of assuming loss of off-site power is small.
NNECO has attached a chronology of correspondence which demonstrates the level of review performed for current analysis methodologies and assumptions for the steam line break accident. In each instance, the Staff documents their acceptance of the assumptions regarding off-site power for the steam line break accident. NNECO has accepted these documents for the purpose of establishing an appropriate licensing basis.
Not withstanding the previous discussion, NNECO fully understands and accepts its responsibility to assure conformance to all applicable regulations, including GDC-17. We hereby reiterate our previous position that Millstone Unit No. 2 complies with GDC-17. As we have confirmed in
. previous discussions, with the Staff, conformance to the GDCs can.be achieved in various ways, with many of the variations being a direct function of the age and vintage of the plant in question. For instance, the volume of docketed correspondence demonstrating our Millstone 3 unit's conformance to the regulations is significantly larger than Millstone Unit No. 2.~ There exists a higher degree of conformance with SRP criteria at Unit 3 as compared to Unit 2. These differences are not, a priori.
Indicative of any deficiencies at Millstone Unit No. 2. Qualitative, technically-sound, - engineering evaluations represent one suitable alternative to quantitative calculations generatsi using NRC-approved models. A portion of our basis for compilance with GDC-17 utilizes the
I
. former technique. NNECO periodically reviews the bases for the transient
'and accident analyses which support operation of all the Millstone Units. l The licensing bases for the three Units are varied with one unit being of SEP vintage and one being an NTOL with an FSAR Chapter 15 consistent with the SRP. As information is made available to NNECO which has a potentially significant impact on the safety analyses assumptions or results for any of the units, NNECO will revise the assumptions utilized in reload safety analyses to conform with the Plant's regulatory basis, if deemed appropriate.
Correspondence Chronology Steam Line Break Evaluations 1.- W. G. Counsil letter to R. Reid, dated March 6,1980.
Northeast Nuclear Energy Company (NNECO) dockets the Basic Safety Report (BSR) for Millstone Unit No. 2. The BSR is intended to serve as the
. reference fuel assembly and safety analysis report for use of Westinghouse
- fuel assemblies at Millstone Unit No. 2
- 2.. ' R. A. Clark letter to W. G. Counsil, dated September 18, 1981.
~ Additional information requested on the transient and accident analyses presented in the BSR. Question 5a requested NNECO to provide a qualitative discussion of the steam line rupture event assuming a loss of
. offsite power.
- 3. ' W. G. Counsit letter to R. A. Clark, dated October 27,1981.
NNECO's response to the September 18, 1981 request for additional information on the BSR transient and accident analyses. '
- 4. W. G. Counsil letter to R. P 9d, dated January 25,1980.
NNECO dockets the steam line break analysis with automatic auxiliary ,
v feedwater initiation. Analysis assumes off-site power available.
- 5. T. M. Novak letter to W. G. Counsil, dated January 14, 1981.
Amendment No. 63 to DPR-65 is issued. NRC reviews steam line break analysis supporting automatic auxiliary feedwater initiation and concludes that off-site power availability is a conservative assumption.
- 6. W. G. Counsil letter to R. A. Clark, dated December 17,1981.
NNECO dockets the results of the Cycle 5 steam line rupture accident evaluation assuming offsite power is available.
- 7. R.' A. Clark letter to W. G. Counsil, dated January 12, 1982.
The NRC Staff documents their review of ' the transient and accident analyses submitted in the BSR. The Staff concludes that the events analyzed, including the steam line rupture, are acceptable.
- 8. E. L. Conner letter to W. G. Counsil, dated March 5,1982.
The NRC staff issues Amendment No. 74 to DPR-65 for Millstone Unit No.
2 authorizing Cycle 5 operation. Section 2.4.7 of the accompanying safety evaluation report addresses the steam line rupture evaluation for Cycle 5 and concludes that the appropriate analysis has been performed and that the results are acceptable.
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- l. .
References
- 1. W. G. Counsil letter. to 3. R. Miller, dated December 12, 1983 (B10968).
2.- K. L. Heitner letter to W. G. Counsil, dated December 30,1983.
- 3. W. G. Counsil letter to 3. R. Miller, dated July 15,1983.
- 4. .W. G. Counsil letter to 3. R. Miller, dated December 12, 1983 (B10960).
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