ML20093L884

From kanterella
Jump to navigation Jump to search
Responds to NRC Re Deviation Noted in Insp Rept 50-322/84-31.Corrective Actions:Startup Test Procedures 14 & 15 Revised to Agree W/Fsar & FSAR Revised,Deleting Requirement to Test HPCI at TC-6
ML20093L884
Person / Time
Site: Shoreham File:Long Island Lighting Company icon.png
Issue date: 10/11/1984
From: Leonard J
LONG ISLAND LIGHTING CO.
To: Martin T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
SNRC-1091, NUDOCS 8410190256
Download: ML20093L884 (4)


Text

(.

'o s

gewzra:wmmin=rzwnq

/gj@

LONG ISLAND LIGHTING COM PANY 8=.ww m eunm7my SHOREHAM NUCLEAR POWER STATION P.O. BOX 618, NORTH COUNTRY ROAD e WADING RIVER. N.Y.11792 JOHN D. LEON ARD, JR.

VICE PR ESIDENT. NUCLEAR OPE R ATIONS October 11, 1984 SNRC-1091 Mr. Thomas F. Martin, Director Division of Engineering and Technical Programs U.S. Nuclear Regulatory Commission - Region I 631 Park Avenue King of Prussia, PA 19406 NRC Inspection of July 23 - 26, 1984 Shoreham Nuclear Power Station - Unit 1 Report No. 50-322/84-31

Dear Mr. Martin:

In accordance with Title 10CFR Part 2, Appendix C, of this letter provides LILCO's response to the Notice of Deviation contained in Appendix A of your letter dated September 12, 1984, which forwarded the results of routine inspection 50-322/84-31.

Our response includes (1) the corrective steps which have been taken and the results achieved; (2) the corrective steps taken to prevent recurrence of similar deviations; and (3) the date when full compliance is expected to be achieved.

While we anticipate that you will find this response acceptable, please do not hesitate to call my office should you require further information or clarification regarding our reply.

Very truly yours Cd f?, f-on Leonard, Jr.

Vice President - Nuclear Operations TD:ck Attachment cc:

P.

Eselgroth C.

Petrone 8410190256 841011 gDRADOCK 05000322 L

PDR l

IE Ol

AFFIDAVIT STATE.OF NEW YORK)

SS.:

COUNTY OF SUFFOLK)

JEFFREY L.

SMITH, being duly sworn, deposes and says that'I am the Manager, Nuclear Operations Support Department for Long Island Lighting Company, the owner of the Shoreham Nuclear Power Station.

I have read the Notice of Deviation dated September 12, 1984, and also the response thereto dated October 11,-1984, prepared under my direction.

The facts set-forth in said response-are based upon reports and information provided to me by the employees, a' gents, and representative of Long Island

' Lighting Company responsible for the activities described in said Notice of Deviation and in said response.

I believe the facts set forth in said responses are true.

Jgfleg1. Smith Sworn to before me this

/,Q c day of (Ocfo664 1984

()

{.

~~

t CONNIE-MARIA PARDO

. MTARY PUBLIC, State of New York No. 52-4615810 Qualifir.d in Suffork County

,mmission Expires gg g

.~

ri -

t i

e i

ATTACHMENT I Response:to Notice of Deviation Deviation.

I Final Safety Analysis Report :(FSAR) Chapter-14, " Initial Tests and Operations" states the following:

114.1.4.8.12 RCIC System Startup Test Acceptance Criteria

.(Level 1)

"3.-

The RCIC turbine must not trip off during the startup."

.4.1.4.8.13 HPCI System Startup Test Acceptance Criteria 1

(Level 2)

"1.

The turbine gland seal condenser system shall be capable of preventing steam leakage to the atmosphere in excess of allowable releases."

Table 14.~1.1-1 item 14.1.4.8.13, HPCI System Startup Test, specifies the test be done during plant heatup, Test Condition (TC)-2 and TC-6.

~ Contrary:to the above it was_ identified that certain startup test procedures did not conform to the above FSAR commitments as follows:

~STP-14, RCIC System, level (1) acceptance criteria restricted the turbine trip to overspeed trip only, rather than any RCIC trip, regardless of cause.

-STP-15 HPCI System, does not provide for performing a HPCI system test at TC-6 and for the' identification of-turbine steam leakage during testing.

Response

(1)

Corrective steps taken and results achieved:

Startup_ Test Procedures (STPs) 14 and 15 have been revised to

-agree with sections 14.1.4.8.12 and 14.1.4.8.13 of the Final Safety Analysis Report (FSAR), Revision 33 - September, 1984.

The requirement to test HPCI at TC-6, as stated in the FSAR,-

was incorrect.

Revision 33 - September 1984, of the FSAR

~

. deletes this requirement.

(2)

Corrective steps taken to prevent recurrence of similar-deviations.

We performed a detailed review of Chapter 14 and the l

associated STPs, in order to ensure that similar deviations do not exist in other STPs.

As a result of this review STPs 14 and 15 were revised (see (1) above) along with various sections of Chapter 141(via revision 33 of the FSAR) which was revised to comply with the most recent General Electric Startup Test Specification.

e.

L

-*Attschmsnt I

.SNRC.-1091 Paga 2-(3)' The date when. full compliance will be achieved:

Chapter 14Lwas revised (Revision 33 'of the FSAR) and issued on September-28,-1984.

Startup Test Procedures 14 and 15

- have been. revised and approved by the Review of Operations Committee j (ROC).

Based on the above, full compliance has

.been facliieved.

-