ML20092F152
| ML20092F152 | |
| Person / Time | |
|---|---|
| Site: | North Anna |
| Issue date: | 01/31/1992 |
| From: | Mladen C, Stewart W VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| 92-105, NUDOCS 9202190112 | |
| Download: ML20092F152 (12) | |
Text
,
f Vil40lNI A I!LI:CTitlO ANil I' owl lt COMI'ANY liarsiuoxas,Vinuixar utiuol l
t February 12, 1992 U. S. Nuclear Regulatory Commission Serial No.
92 106 Attention: Document Control Desk NL&P/JMJ:jmj Washington, D.C. 20555 Docket Nos.
50 338 1
50 339 License Nos. NPF 4 NPF 7 t'
Gentlemen:
VIRGINIA ELECTRIC AND POWER COMPANY NORTH ANNA POWER STATION UNITS 1 AND_2 MONTHLY OPERATING REPORT-Enclosed is the Monthly Operating Report for North Anna Power Station Units 1 and 2 for the month of January 1992.
Very trulyyours,
)l 0
)
.~\\l.-Lj@J
\\
W. L. Stewart Senior Vice President Nuclear Enclosures.
cc:
U.S. Nuclear Regulatory Commission 101 Marietta Street, NW Suite 2900 Atlanta. GA 30323 Mr. M. S. Lesser NRC Senior Resident inspector North Anna Power Station i
.i i
i 9202190112 920131 PDR ADOcK 0500o338 k,
/
I
- R PDR
/,
u
~
i
?-
j i
t i
t a
I VIRGINIA POWER COMPANY i
NORTN ANNA POWER STATION MONTMLY OPERATING REPORT MONTN Januarv YEAR:
1992 i
i n
1 i
Approved:
i.
l' Statitni Pfinager _
l l
i t
i v.
i..-
s m._. _.,,,
s.,.,_,,...-
m.. _ ;,,,, _ -,.
1 f
J OPf RAtits Data RIP 0af 00CKtt No.:
50 338 j
DA't I f ebr uary 3,1992 COMPit tf D 6f
't. Mladen PHONE: (703) 894 2T74 (ttRA1tho $tAtus 1.
tel t h ome s................................ kor t h Anna 1 2.
R epor t t h0 Pe r i od s......................... J erwary 1992
- 3. - 1 ( c eris ed t h erma l Powe r ( t/Jt ' n..,..........
2,893 e
4.
homeplate Rating (Gross W e).............
94T 1
Design (tectrical Rating (ket Mue):.......
907 6.
Maxinue Deperdable Capacity (Cross We)..
959 T.
Maalaus Deperdable Capacity (Wet We)....
911 t
8.
If changes occur in Capacity Ratir.gs (items to, 3 thro T) since last report, give reasons:
j N/A 9.
Power levet to which restricted, if any (het Mile): _ /A W
- 10. Reasons for restrictions, if any N/A this Month fat D CLswletive
- 11. H our s i n R epor t i ng Per i od................................
744.0 744.0 119.316.0
- 12. Ctsntser of Hours Reet t or was Cr i t i c al.....................
0.0 0.0 86,688.5
- 13. R eactor R eserve Shut down Hours...........................
0.0 0.0 6,721.7
- 14. tours Gener a t or 0n L i ne..................................
0.0 0.0 83.771.5
- 15. Uni t R eserve Shut down Hours..............................
0.0 0.0 0.0
- 16. Gros s t hermal E ner gy Generat ed (WM ).....................
0.0 0.0 222,152,772.4
- 17. Gross tiec t ricot Energy Genera t ed (WH)..................
0.0 0.0 73,257,047.0 18, tot E lec t rical Ener gy Gener st ed (WN)....................
0.0 0.0 69,354,617.0
-19. Unit Service factor......................................
0.0%
0.0%
70 2%
- 20. Uni t Ava i l abi l i t y f ac t or.................................
0.0%
0.0%
T0.2%
- 21. Uni t cepec i t y f ac t or (us ing MDC het ).....................
0.0%
0.0%
64.0%
- 22. Uni t Capac i t y f ac t or (us ing DE R Wet ).....................
0.0%
0.0%
64.1%
- 23. forced Outege Rate.......................................
29.0%
29.0%
12.6%
- 24. thutdowns $cheduled Over Next 6 Months (Type, Date, and Duration of f ach)
N/A
- 25. If Shutdown et ord of Report Period, estimated time of Startup 03/13/92
- 26. Units in Test Status (Prior to Connerclet Operation):
i forecast Achieved INITIAL CRifitAllif IWillAL ELECTRICITY COMMERCIAL OP[ RATION
i 4
Avr. RAGE DAILY UNIT POWER LEVEL Docket No.t 5.Q-2) 8 Unit
.,__ jilc 1 -
Dat6i f.9)n qary_1 1122 completad by 8.__Ca..lilad.cn Phone
.[2.Q21 894-2774 MONTH January 192 L DAY AVERAGE DAILY POWER DAY AVERAGE DAILY LEVEL LEVEL (MWe-Net)
LEVEL (MWe-Net) 1 0
17 0
2 0
18 0
3 0
19 0
4 0
20 0
5 0
21 0
6 0
22 0
7 0
23 0
8 0
24 0
9 0
25 0
10 0
26 0
11 0
27 0
12 0
28 0
13 0
29 9
14 0
30 0
15 0
31 0
16 0
Instructionst On this format, list the average daily unit power level in MWe-Not for each day in the reporting month.
Compute to the nearest whole megawatt.
i I
Pago 1_ o f __1 UNIT SHUTDOWN AND POWER REDUCTIOND Explanation Sheet Docket No.1 _ EDr_338 Report Month 2Anuary Unit Namut NA-1 Yuart,_1,912_.
Dates Egbruary 3, 1912 Completed by:
Cathio Mladen
/91-10 December 23, 1991 Commenced unit ramp-down and initiated "Hotification of Unusual Event" at 1632 hours0.0189 days <br />0.453 hours <br />0.0027 weeks <br />6.20976e-4 months <br />.
Main Generator taken off-lino at 2059 hours0.0238 days <br />0.572 hours <br />0.0034 weeks <br />7.834495e-4 months <br />.
Main Turbino manually tripped at 2106 hours0.0244 days <br />0.585 hours <br />0.00348 weeks <br />8.01333e-4 months <br />.
Unit ontored Hodo 3 at 2149 hours0.0249 days <br />0.597 hours <br />0.00355 weeks <br />8.176945e-4 months <br />.
December 24, 1991 Unit entered Mode 4 at 0230 hours0.00266 days <br />0.0639 hours <br />3.80291e-4 weeks <br />8.7515e-5 months <br />.
Unit ontored Modo 5 at 0718 hours0.00831 days <br />0.199 hours <br />0.00119 weeks <br />2.73199e-4 months <br />.
Terminated "Hotification of Unusual Event
- at 0730 hours0.00845 days <br />0.203 hours <br />0.00121 weeks <br />2.77765e-4 months <br />.
- 92-01 January 10, 1392 Unit in Mode 5 for planned inspection and maintenance of Steam Generators.
(
l l
l
~
UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.:
50-338 UNIT NAME:
NA-1 DATE: February 3, 1992 REPORT MONTH: January 1992 COMPLETED BY:
C. Mladen PHONE:
(703) 894-2774 1
2 3
4 5
No.
Date Type Duration Reason Method of Licensee System Component Cause & Corrective (hrs)
Shatting Event Code Code Action to Down Reactor Report #
Prevent Recarrence 91-10 911223 F
216.0 A
4 N/A SB SG Unit shutdown required l
by T.S.
3.0.3 due to j
declaring all three steam generators inoperable.
92-01 920110 S
528.0 B
4 N/A SB SG S/G inspections and maintenance planned.
3: Method 4:
1: Type 2: Reason F= Forced A= Equipment Failure (explain) 1= Manual Exhibit F - Instructions S= Scheduled B= Maintenance or Test 2= Manual Scra=
for preparation of Data 3= Automatic Scram Entry Sheets for Licensee C= Refueling 4= Continuations Event Report (LER) File D= Regulatory Restriction E= Operator Training & License Examination 5= Load Reduction (NUREG-Ol61)
F= Administrative 9=Other 5:
G= Operational Error Exhibit H - Same Source H=Other (explain)
o NORTH ANNA POWER STATION UNIT NO.
1 NONTHI J Jiuary HVMMARLQLDEIRATIN9_XXPERIZILCR Listed below in chronological sequence is a
summary of operating experiencon for this month which required load reductions or resulted in significant non-load related incidents.
D419 TlMt D41A f
January 01, 1992 0000 Bogan month with unit in Hodo 5.
January 31, 1992 2400 Ended month with unit in Mode 5.
o
I e
OPtRAtlko DAfa ttPORT Docitt me.:
50 339 DA1( February 3, 1992 i
COMPttitD Bt C. Mladen FNONf (703) 894 2774 OPERAtlWQ $1ATUS 1.
Uni t k ame s................................ W or t h Ama 2 2.
R epor t i ng P e r i od s......................... J arua r y 1992 3.
Licensed thermet Power ( Wt):.............
2893 4.
Nameptete Reting (Gross W e):.............
947 5.
Design Itectrical Reting (Net W e).......
907 6.
Mastma DepeMable Capacity (Gross We)..
957 7.
Me:Imm Deperdable Capacity (het We)....
909 8.
If changes occur in Capacity Ratings (items No. 3 thru 7) since test report, give reasons W/A 9.
Power levet to which restricted, if any (Net We): _ /A W
- 10. Peesons for restrictions, if any:
N/A this Month YtD Cumulative
- 11. Cour s i n R epor t I ng P er i od................................
744.0 744.0 97,584.0
- 12. Nader of Hours t ract or was Cr i t ica t.....................
732.1 732.1 80,468.0
- 13. R eac t or R ese rve shut down H our s...........................
11.9 11.9 6,069.3
- 10. b. 's Generator 0n Line..................................
717.0 717.0 79,491.4
- 15. Unit Reserve shutdown Hours..............................
0.0 0.0 0.0
- 16. Gross Therme t E ner gy Genera t ed (WW )..................... 1,984,061.2 1,984,061.2 213,801,194.3
- 17. Gross t iec t rical E nergy Generat ed (MWM)..................
647,575.0 647,575.0 70.027,701.0
- 18. Ne t t i ec t r i cal Ener gy Genera t ed (WW)....................
615,306.0 615,306.0 67,115.039.0
- 19. Uni t se rvi c e f ac t or......................................
96.4%
96.4%
81.5%
- 20. Unit Aveliability factor.................................
96.4%
96.4%
81.5%
- 21. Unit Capacity factor (using MDC Net)..................,..
91.0%
91.0%
76.4%
- 22. Uni t Capac i t y f ac t or (us ing DE R We t ).....................
91.2%
91.2%
75.8%
- 23. f orc ed Out a ge R a t e.......................................
3.6%
3.6%
6.0%
- 26. $hutdowns schedul'ed Over Went 6 Months (Type, Date, and Duration of tech):_ Refueling / Maintenance Outage,
_ Scheduled to Corner.ce 02/26/92; Estimeted Duration of 60 Days
- 25. If shutdown at end of Report Period, estimated time of startup N/A
. 26. Unite in fest Status (Prior to Ctenercist Operation):
forecast Achieved IWlilAt CRiflCALITY INITIAL tttCTRICl1Y
' COMMERCIAL OPERAil0N
UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.:
50-339 UNIT NAME:
NA-2 DATE: February 3, 1992 REPORT MONTH: January 1992 COMPLETED BY:
C. Mladen PHONE:
(703) 894-2774 i
t i
1 2
3 4
5
- No.
Date Type Duration Reason Method of Licensee System Component Cause & Corrective
]
(hrs)
Shutting Event Code Code Action to Down Reactor Report #
Prevent Recurrence 92-02 920129 F
27.0 A
3 92-001 SJ FCV Reactor trip due to "C" j
Main Feedwater Regulating Valve closure due to d
failed driver card.
4 Replaced card.
i 4
4 4
1 1: Type 2: Reason 3: Method 4:
F= Forced A= Equipment Failure (explain) 1= Manual Exhibit F - Instructions S= Scheduled B= Maintenance or Test 2= Manual Scram for preparation of Data C= Refueling 3= Automatic Scram Entry Sheets for Licensee D= Regulatory Restriction 4= Continuations Event Report (LER) File i
E= Operator Training & License Examination 5= Load Reduction (NUREG-0161) 4 F= Administrative 9=Other G-Operational Error 5:
,l H=Other (explain)
Exhibit H - Same Source i
1-
{
t i
i 4
t e
AVERAGE DAILY UNIY POWER LEVEL l
t
[
Docket No.4 50-339 Unitt NA-2
[
Dates February _3.
1992 i
completed byl. c. Mladan l
Phonet (703) 894-2774 i
e I
f i
. MONTE:
January 1992 i
i t
DAY AVERAGE DAILY POWER DAY AVERAGE DAILY LEVEL LEVEL (NWa-Met)
LEVEL (NWe-Met)
-(
I 1
903 17 889' 2
903 18 874
-3 903 19 864
'I
-4 902 20 861 5
902 21 858 l
6 901 22 855 7
903 23 853 8
901 24 835 9-903 25 833 6
10 898 26 830 11-903 27 827 12 902 28.
824 13 902 29 114 i
14 900 30 188-i 15 898 31 715 l
16 894
[
v i
i-
- Instructions 8 on this format, list the average daily unit power level in MWe '
Net--for each day in the reporting month.
Compute to the nearest whole megawatt.
t l-I
+
t l'
-,-.,._,.~,.-..,__,,+,.__,,i.,._.,,___-.m.-_,,,,,,..
.. m
,w
-..,~_m
...-~m,.
CORTH ANNA P02ER STATION UNIT NO,t 2
l MONTH 8 a2ADunty_
RUMMARLAZ_QEIRATIEQ JXFIRIINCE Listed below in chronological sequence is a
summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
Dals Tint Data January 01, 1992 0000 Bogan month with unit at 100% power, 953MWo.
January 10, 1992 0928 Commenced unit ramp-down to BbOMWo for TVPT.
0955 Unit stable at 880MWo.
1050 TVTT completed satisfactorily.
3058 Commenced unit ramp-up to 100%
power.
1124 Unit stable at 100% power, 942MWo.
January 13, 1992 0143 Unit RCS boron concentration less than 1
- ppm, commenced power coastdown for refueling outage.
January 29, 1992 0325 Roactor trip as a result of "C" Main Feedwater Regulating valve failing closed.
1517 Unit ontored Modo 2.
January 30, 1992 0510 Unit entered Modo 1.
0628 Main generator placed on-line.
1004 Unit stable at 30%
power for Chemistry hold.
1703 Commenced unit ramp-up to 48% power.
1747 Unit stable at 48% power, 343MWo.
2057 Commenced unit ramp-up.
2231 Suspended power increase for QPTR datormination.
January 31, 1992 0101 Commenced unit ramp-up.
2400 Ended month with unit at 86% power, 815MWo.
s Pago 1
o f
_1 UNIT SHUTDOWN AND POWER REDUCTIONS Explanation sheet Dookat No.:
50-339 Report Month January Unit Name NA-2 Yeart _1992 Dates Eebruary_3, 19J2 Completed by: __Cathic Mladen
- 92-02 January 29, 1992 Reactor trip as a result of "C" Main Foodwater Regulating Valvo clonure at 0325 hours0.00376 days <br />0.0903 hours <br />5.373677e-4 weeks <br />1.236625e-4 months <br />.
Unit ontored Modo 2 at 1517 hours0.0176 days <br />0.421 hours <br />0.00251 weeks <br />5.772185e-4 months <br />.
January 30, 1992 Unit ontored Modo 1 at 0510 hours0.0059 days <br />0.142 hours <br />8.43254e-4 weeks <br />1.94055e-4 months <br />.
Main generator on-line at 0628 hours0.00727 days <br />0.174 hours <br />0.00104 weeks <br />2.38954e-4 months <br />.
Unit stable at 30% power for Chemistry hold at 1004 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.82022e-4 months <br />.
Commenced unit ramp-up to 48% power at 1703.
Unit stable at 48% power at 1747 hours0.0202 days <br />0.485 hours <br />0.00289 weeks <br />6.647335e-4 months <br />.
Commenced unit ramp-up at-2057 hours.
Suspended unit ramp-up for QPTR datormination at 2231 hours0.0258 days <br />0.62 hours <br />0.00369 weeks <br />8.488955e-4 months <br />.
January 31, 1992 Commenced unit ramp-up at 0101 hours0.00117 days <br />0.0281 hours <br />1.669974e-4 weeks <br />3.84305e-5 months <br />.
Ended month with unit at 86% power in power coastdown.
.