ML20092F059

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Monthly Operating Rept for Jan 1992 for Clinton Power Station Unit 1
ML20092F059
Person / Time
Site: Clinton Constellation icon.png
Issue date: 01/31/1992
From: Spangenberg F
ILLINOIS POWER CO.
To:
Shared Package
ML20092F051 List:
References
NUDOCS 9202190067
Download: ML20092F059 (4)


Text

-

to U 601933 Page 1 of 4 CllALLENCES TO MAIN STEAM SAFETY / RELIEF VALVES 4

Month January 1992 None r-4 d

9202190067 920222 gDR ADOCK 05000461

.PDR

to U -601933--

Page 2 of 4..

AVERACE DAILY UNIT POWER LEVEL-DOCKET NO.

50-461~

~

-UNIT _Clinton 1' DATE- 01/31/92 COMPLETED BY F. A.

S pan e.enbt r e.. III TELEPHONE (217F 935-8881 X3400 MONTH January 1992 DAY AVERACE DAILY POWER LEVEL DAY AVERACE DAILY POWER LEVEL (MWe-Net)

(MWe-Net) 1 928

-17 539 2

927 18 728 3

924 19 873 4

66 20.

835 5

0 21 887 6

0 22 875 7

0 23 871 8

0 24 876 9

0 25 877 10 0

26 876 11-0 27 878 12 0

28 877 13 0

29 877 14 0

30 878 15 0

31 878 16 126

4 to U 601933 Page 3 of 4 OPERATING DATA REPORT 1

1 DOCKET NO.

50-461-4 UNIT 311nton 1 DATE 01/31/92 COMPLETED BY F. A.

Snantenbern. III TELEPHONE (217) 935-8881 X3400 OPERATING STATUS 1.

REPORTING PERIOD: January 1992 GROSS HOUP.S IN REPORTING PERIOD: 744 2.

CURRENTLY AUTHORIZED POWER LEVEL (MWt): 2894 MAX DEPEND. CAPACITY (MDC) (MWe-Net): 930 DESlv*1 ELECTRICAL RATING (MWe-Net): 933 3.

POWER LEVEL TO WHICH RESTRICTED (IF ANY) (MWe-Net):

None 4

REASONS FOR RESTRICTION (IF ANY):

N/A THIS MONTH YR TO DATE CUMUIATIVE 5.

NUMBER OF HOURS REACTOR WA3 CRITICAL..,

470.8 470.8-24.919.1 6.

REACTOR RESERVE SHUTDOWN HOURS.........

0.0; 0.0 0.0 7.

HOURS GENERATOR ON LINE.,

450.9 450.9 24.080.0 8.

UNIT RESERVE SHUTDOWN HOURS............

0.0 0.0 0.0' 9.

GROSS THERMAL ENERGY GENERATED (MWH)... 1.180.614 1;180.614 61.939.347 10.

GROSS ELECTRICAL ENERGY GENERATED (MVH) 391.720-391.720 20.468 81Q 11.

NET ELECTRICAL ENERGY GENERATED (MWH)..

368.273 368.273-19.419.650 12.

REACTOR SERVICE FACTOR.................

6 3 '. " %

63.3%

67.9%

13.

REACTOR AVAILABILITY FACTOR...

63.36,

-63.31-67.9t 14.

UNIT SERVICE FACTOR.

60.6%

-60.6%

65.6%

15.

UNIT AVAILABILITY FACTOR...............

60.6%

-60.6%

- 65.6%

16.

UNIT CAPACITY FACTOR (Using MDC).......

53.2%

53.2%

55.9%

17.

UNIT' CAPACITY FACTOR (Using Design MWe) 53.1%

53.1%-

56.7%-

18.

UNIT FORCED OUTAGE RATE................

39.4%

39.4%'

14.6%

19.

SHUTDOWNS SCHEDULED OVER NEXT SIX MONTHS (TYPE, DATE, DURATION OF EACH):

The third refueling outageSis-currently scheduled to begin March 1, 1992_and last approximately 70 days.

20.

IF SHUT DOWN AT' END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:

N/A l

4 i

w

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MF to U-601933 '

Page 4. of 4 }

UNIT SHUTDOWNS AND POWER REDUCTIONS POCKET NO. 50-461 UNIT Clinton 1 DATE 01/31/92 COMPLETED BY-F. A.

Spannenberc. III TELEPHONE (217) 935-8881 X3400 REPORT MONTH January 1992 METHOD OF TYPE SHUTTING DOWN F:

FORCED DURATION THE REACTOR OR CORRECT 1tE ACTIONS NO.

DATE S:

SCHEDULED (HOURS)

REASON (1)

REDUCING-POWER (2) / COMMENTS 92-01 920104 F 293.1 A: An internal fault occurred 3: An automatic The "B" Main Power in the "B" Main Power scram signal Transformer was Transformer causing was generated replaced.with a the sudden pressure relay as a result spare transformer.

to actuate. This actuation of the main (See LER 92-001).

caused a main generator. trip turbine trip.

The forced outage and subsequently a main was extended due to turbine trip and, reactor scram.

the clean up'of an unrelated Electrohydraulic Control (EHC) fluid spill in the suppression pool.

Upon completion of I

cleanup, the plant was returned to power i

operation (1) Reason l

A-Equipment Failure'(explain).'B-Maintenance or Test, C-Refueling, D-Regulatory Restriction,

E-Operator._ Training 6 License-Examination, F-Administrative, G-Operational Error,(explain),

l H-Other (S < plain)

(2)~ Method 1-Manual, 2-Manual Scram,.3-Automatic Scram, 4-Other (explain) l

- = -. - - - -.

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