ML20092F074
| ML20092F074 | |
| Person / Time | |
|---|---|
| Site: | Clinton |
| Issue date: | 12/31/1992 |
| From: | Spangenberg F ILLINOIS POWER CO. |
| To: | |
| Shared Package | |
| ML20092F051 | List: |
| References | |
| NUDOCS 9202190073 | |
| Download: ML20092F074 (1) | |
Text
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to U-601933
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- 0T4 Page 1 of 1 UNIT SHU'rDOWNS'AND POWER REDUCTIONS M
DOCKET NO. 50-461 j
>c UNIT Clinton 1-oh DATE 01/31/92 l
Qy COMPLETED BY F. A.
Spannenberz. III TELEPHONE (217) 935-8881 X3400 Of REPORT MONTH December 1991 00 OM 10*
ND METHOD OF TYPE SHUTTING DOWN F:
FORCED DURATION THE REACTOR OR CORRECTIVE ACTIONS NO.
DATE S:
SCHEDULED [ HOURS)
REASON (1)
REDUCING POWER (2) / COMMENTS t
i j
91-06 911222 F 111.4 A: During a scheduled 2: Upon entering Repaired / replaced reduction in power 1(
the restricted valve position the "B" Reactor Recirc zone of.the and velocity ulation Flow Control Valve power-flow feedback sensors (FCV) position feedback operating map, for the "A" and "B" loop failed, resulting in a manual scram Reactor Recircul-l erratic FCV movement and a was inserted ation FCVs. -Follow -
+
decrease in reactor as required ing repairs, the core flow. The decrease by plant plant was returned in core flow placed the procedures.
to power operation.
reactor in the restricted (See LER 91-008).
zone of the power-flow operating map.
As a result, a manual reactor i
scram'was inserted as f
required by plant j
procedures.
(1) Reason j
A-Equipment Failure (explain), B-Maintenance or Test. C-Refueling D-Regulatory Restriction, E-Operator Training & License Examination, F-Administrative, G-Operational Error (explain),
H-Other (explain)
(2) Methodf 1-Manual, 2-Manual Scram, 3-Automatic Scram, 4-Other (explain)
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