ML20092D591

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Submits Daily Highlights.Major Steam Generator Tube Leak Occurred When Returning Reactor to Svc After Refueling Outage.Max Leakage Approx 112 Gpm Based on Steam Generator Level Measurements & Charging Flow
ML20092D591
Person / Time
Site: Fort Calhoun 
Issue date: 05/17/1984
From: Tourigny E
Office of Nuclear Reactor Regulation
To: Case E, Harold Denton, Edison D
NRC
Shared Package
ML20092D569 List:
References
NUDOCS 8406220064
Download: ML20092D591 (2)


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UNITED sTATEW NUCLEA'R REGULATORY COMMISSION t-a wasmmorow, o.c.2ones i

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MAY 171984 MEMORANDUM FOR:

H. Denton I

E. Case G. Edison D. Eisenhut

.R. Purple DL Assistant Directors OR Branch Chiefs i

T. Speis R. Mattson

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R. Vollmer H. Thompson G. Holahan

8. Snyder

-James R. Miller, Chief [#I /

l THRU:

Operating Reactors Branch #1 DL FROM:

E. G. Tourigny, Project Manager Operating Reactors Rranch #3, DL l

SUBJECT:

DAILY HIGHLIGHT 4

Fort Calhoun Station. Unit No. 1 The Fort Calhoun Station was in the process of returning to service after a refueling outage when a' major steam generator tube leak occurred in steam generator B during the primary system hydrostatic pressure test.

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The primary system pressure was approximately 1800 pounds and the secondary system pressure was approximately 200 pounds. The maximum leakage was estimated at approximately II2 gallons per minute based i

on SG level measurements and charging flow; the maximum charging rate for the plant is 120 gallons per minute.

The operators noticed water level and radioactivity level in the generator rising and isolated the steam generator. The plant was cooled down using steam generator _A.

It was estimated that 7500 gallons was transferred

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from the reactor coolant system to steam generator R.

Approximately 15,000 gallons of water is currently in steam generator B; its capacity is about 22,000 gallons. No water was introduced through the main steam line and no measurable radiological release was detected.

The licensee pians to drain the steam generator and find the leak.

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Two factors' must be evaluated in determining the cause of the leak.

Prior to' refueling, the' licensee detected minor leakage estimated to be less than r

one gallon per day. Extensive work was performed durino the outage to

. attempt to find this leak. This included eddy current testing, helium t

testing, and dye testing. The leak could not be found.

In addition both l

steam generators had rim cut operations performed during the outage.

8406220064 840614 PDR ADOCK 05000285 G

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  • 2-It is not known at this time if the major leak was a further dearadation of the previous leakage problem or whether it was a result of the rim cut operation.

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E. G. Tourigny roje t Manager Operating Reaators B nch #3 4

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