ML20091H983

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Intervenor Exhibit I-MOSBA-43,consisting of Diesel Testing
ML20091H983
Person / Time
Site: Vogtle  Southern Nuclear icon.png
Issue date: 05/17/1995
From:
AFFILIATION NOT ASSIGNED
To:
References
OLA-3-I-MOSBA43, NUDOCS 9508160371
Download: ML20091H983 (17)


Text

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DIESEL TESTING DOCKETED USHRC

% a 27 M0 NORMAL 36 MONTH OVERHAUL AND INSPECTION OFFICE OF SECRETARY SPECIAL TESTING 00cKETING & SERV!CE ERANCH M

N 3/20 EVENT IN OVERHAUL 5 STARTS, TROUBLESHOOTING SENSOR CALIBRATION LOGIC TESTING E-RUN BUBBLE TESTING MULTIPLE STARTS (lll)

UV RUN TEST 6 MONTH RUN SURVEILLANCE DIESEL OPERABLE UV RUN TEST SENSOR CALIBRATION LOGIC TESTING E-RUN BUBBLE TESTING LUBE OIL DCP RUN MULTIPLE STARTS (5)

DCP UV RUN FUNCTIONAL UV RUN TEST 6 MONTH SURVEILLANCE DIESEL OPERABLE HI JACKET WATER RUNS (3)

DCP UV RuN TEST 18 SUCCESSFUL STARTS 19 SUCCESSFUL STARTS I

NUCLEAR REGULATORY COMMISSION Docket No. 50 424/425-OLA 3 EXHIBIT NO.

Ie #N 3 O Staff O Applicar.t M lntervenor O Othe, ER vefyg

$Mc7 in the matter of Georola Power Co. et al, Vontie Units t & 2 QLtdent fied O Received O Rejected Reporter Cd hy g' 8 Date 05- / 7 -6 Witness It # w l4*t 055%7 7~204V 9508160371 950517 PDR ADOCK 05000424 0

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Cloo UNIT 2 i

l o UNIT 2 TRIP Unit 2 RAT B Trip / Primary Differential Trip 4

4 Turbine Trip / Reactor Trip Safety System Response Proper E

o CAUSE Differential Relay CT Set 3000/5 vice 2000/5 o CORRECTIVE ACTIONS Test the Remaining Relays on Unit 2 Update Switchyard Drawings based on audit Clarify existing policies for Switchyard i

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93. PROJECT l

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DATE: April 6, 1990 RE:

Accountability During Emergencies Log:- NOV-00426 FROM:' G. Bockhold. Jr.

All Emergency Directors TO:

and Site Personnel 1

In the event of site emergency conditions, we will implement the following revised procedures. These changes will enhance personnel.

accountability and safety and ensure better information flow for i

employees. -They will also provide flexibility to the plant when responding to emergency situations.

When the Emergency Director (ED) makes an emergency classification, he will make the appropriate tone and page announcement on the plant PA system. He will direct site personnel to the appropriate locations.

LIf,you can not hear the page, report to your supervisor. He or she will direct'you appropriately.

Normally non-essential personnel

' will: report to the Admin. Building auditorium or parking lot.

David Phillips, the Financial Services Supervisor, has authority to coordinate with.the ED and control the disposition of non-essential personnel.

In his absence, the senior person present will contact the Security 1

Captain-for additional assistance.

Emergency Response' Organization (ERO) personnel should report 4

immediately to_ the appropriate facility.

Other shift personnel.

supervisors, and managers on-site should report initially to the OSC.

Overflow personnel will assemble in the maintenance machine shop area.

When directed by the ED, the security department will initiate accountability.

The security department cannot account for personnel who fail to log into the appropriate ERF (e.g., control room, TSC, or OSC) so it is essential we comply with the ED's instructions as i

soon as possible.

l Your assistance implementing these instructions will ensure we manage emergencies better and provide plant personnel with sufficient information to keep them informed of abnormal plant activities.

Thank you for your assistance.

6 L

CB/ erd.

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Department Heads NORMS 92 PRomy 055900

OCA QUARANTINE COMPONENTS TEMPERATURE SWITCHES o

1A-PROBABLE IRIP CAUSE JACKET WATER TEMPERATURE (2/3 LOGIC) 1 INTERMITTENT i

1 POST CALIBRATION L0w (186*F & VENTING) o lA OTHER IEMPERATURE COMPONENTS 1 Lube OIL TEMPERATURE (SLUGGISH) l o

1B TEMPERATURE COMPONENTS 4 JACKET WATER TEMP (VENTING) 2 LUBE OIL TEMP (VENTING & CALIB.)

i PRESSURE SWITCHES i

o 1A 1 LUBE OIL PRESSURE (TRIPPED) 2 LUBE OIL PRESSURE (CONSERVATIVELY REPLACED) o 1B 2 logic (WOULD NoT TRIP ENGINE) i d

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EMERGENCY PLAN IMPLEMENTATION DURING THE EMERGENCY, OFF-SITE NOTIFICATIONS WERE LATE AND/0R DELAYED BEYOND THE 15 MINUTE TIME LIMIT.

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O DIRECT CAUSES POWER TO THE PRIMARY ENN (IE EMERGENCY POWER) WAS LOST.

ALL EMERGENCY AGENCIES WERE NOT INCLUDED ON THE BACKUP ENN.

(BURKE COUNTY AND GEMA ADDED 4/6/90)

}

O ' CONTRIBUTING CAUSES CONTROL ROOM COMMUNICATORS AND SUPERVISORS WERE NOT FULLY. KNOWLEDGEABLE OF THE COMMUNICATIONS l

SYSTEM CAPABILITIES.

(PRIMARY ENN IN TSC HAD POWER FROM THE SECURITY SYSTEM DIESEL.)

THE SERIES METHOD OF NOTIFICATION CONTAINED UNSATISFACTORY DELAYS.

EMERGENCY DIRECTOR DID NOT ENSURE PROMPT NOTIFICATION OF OFF-SITE AGENCIES.

AMPLIFYING INFORMATION WAS NOT PROVIDED TO LOCAL GOVERNMENT OFFICIALS.

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l 9A PAorccr 055902 r

DDb INITIATING EVENT 1

FUELING TRUCK STRUCK INSULATOR SUPPORT INSIDE THE LOW VOLTAGE SWITCHYARD CAUSING A FAULT TO THE-1A RESERVE AUXILIARY TRANSFORMER, o

DIRECT CAUSE IRUCK DRIVER AND ESCORT WERE INATTENTIVE TO SAFE OPERATION OF THE TRUCK.

o CONTRIBUTING CAUSES J

CONTROL OF VEHICLES NEAR VULNERABLE AND SENSITIVE AREAS NOT ESTABLISHED, MAINTENANCE EQUIPMENT STAGED INAPPROPRIATELY.

THE USE OF GROUND-GUIDES INSIDE THE PROTECTED ARri WAS NOT CLEAR.

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0 55903

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EMERGENCY PLAN IMPLEMENTATION COMMUNICATION BETWEEN CORPORATE AND TSC NEEDS TO BE IMPROVED.

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DIRECT CAUSES 4

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THE STATUS LOOP TELEPHONE BRIDGE WAS NOT OPERABLE AT THE BEGINNING OF THE EMERGENCY BECAUSE OF THE LOSS OF POWER.

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C{>.3 EMERGENCY PLAN IMPLEMENTATION DURING THE EMERGENCY, SITE PERSONNEL ACCOUNTABILITY I

NEEDED IMPROVEMENT.

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DIRECT CAUSE ACCOUNTABILITY PROCEDURES DID NOT PROVIDE FOR THE SITUATION OF NOT EVACUATING THE SITE.

(GENERAL MANAGER'S MEMO OF 4/6/90) r o

CONTRIBUTING CAUSES THE INITIAL PAGE ANNOUNCEMENT WAS DELAYED APPROXIMATELY 20 MINUTES.

PERSONNEL WERE ALLOWED TO RE-ENTER THE PROTECTED AREA.

i PAGE ANNOUNCEMENTS ARE DIFFICULT TO HEAR IN SOME PLANT AREAS.

THE COMPUTER GENERATED PRINTOUT DID NOT ALLOW QUICK IDENTIFICATION OF PERSONNEL.

THE EMERGENCY DIRECTOR FAILED TO PROVIDE I

GUIDANCE AFTER DECIDING NOT TO EVACUATE 7

PERSONNEL.

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91 Pe.oreer 053905 A

Cc3 DIESEL GENERATOR AVAILABILITY THE 1A DIESEL GENERATOR FAILED TO PROVIDE EMERGENCY POWER TO 1E LOADS UNDER LOSP CONDITIONS.

0 DIRECT CAUSE DIESEL TRIP SIGNALS WERE PRESENT DURING UNDER VOLTAGE INITIATED START CONDITIONS.

1 0

CONTRIBUTING CAUSES POST MAINTENANCE FUNCTIONAL TESTING FOR AIR LEAKAGE IN THE CONTROL SYSTEM WAS INADEQUATE.

PROCEDURES FOR TIGHTENING FITTINGS IN THE

.b AIR LOGIC SYSTEM NEED IMPROVEMENT.

l CALIBRATION PROCEDURES OF TEMPERATURE SWITCHES DID NOT GUARANTEE CONSISTENT SETTINGS.

4 DIESEL GENERATOR TRIPS DURING LOSP WERE NOT CONSISTENT WITH TRIPS DURING A SAFETY i

INJECTION SITUATION.

DIESEL GENERATOR START LOGIC DID NOT ALLOW MULTIPLE STARTS ON AN UNDERVOLTAGE CONDITION WITH THE DIESEL RUNNING.

OPERATORS DID NOT FULLY UNDERSTAND THE DIESEL START LOGIC AND SEQUENCER INTERFACE l

ON AN LOSP.

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% PRosEcr 0 55906 I

OCS MID-LOOP OPERATIONS i

ACTIONS TO RESPOND TO LOSS OF CORE COOLING AT

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MID-LOOP SHOULD BE IMPROVED.

o DIRECT CAUSE THE " LOSS OF RESIDUAL HEAT REMOVAL" PROCEDURE i

SHOULD PROVIDE IMPROYED GUIDANCE FOR A LOSP CONDITION.

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CONTRIBUTING CAUSES 1

1 IHE " LOSS OF RHR" PROCEDURES ARE TOO NARROWLY FOCUSED FOR MODE S & 6 CONDITIONS.

DIRECTIONS FROM THE EMERGENCY DIRECTOR WERE NOT ALWAYS EXPLICIT.

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PRESENTATION TO REGION II NUCLEAR RE6ULATORY COMMISSION ON V0GRE SITE AREA EERGENCY MARCH 20, 1990 AGENDA 0

OPENING REMARKS C. K. McC0Y 0

EVENT REVIEW TEAM CRITIQUE G. BOCKHOLD 0

TRUCK / SWITCHYARD O

0FF-SITE NOTIFICATIONS O

PERSONNEL ACCOUNTABILITY 0

COMMUNICATIONS CORPORATE / SITE O

MID-LOOP OPERATIONS 0

DIESEL TESTING /0PERABILITY G. BOCKHOLD O

QUARANTINE COMPONENTS G. 80CKHOLD 0

UNIT 2 G. BOCKHOLD 1

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9A Pko7ECT O5GS08

UNIT 1 DIESEL GENERATOR 18

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DATE TIME COMENTS 02/24/90 1425 Started for 24 Hour Run 02/25/90 2206 Secured from 24 Hour Run 2336 Started for ESFAS Testing 2348 Secured for ESFAS 02/27/90 0312 Started for ESFAS 0424 Secured for ESFAS

-0605 Started for ESFAS 0642 Secured for ESFAS 03/13/90 1518 Start for itaint. Test 03/14/90 0146 Stopped

~03/21/90 2149 Failed to start due to insufficient fuel in fuel lines after maintenance.

2156 Failed to Start Again 2202 Started and Governor Vented 2217 Stopped 2259 Started for Overspeed Trip Test 2301 Stopped Manually due to Low Lube Oil Pressure and High 011 Filter DP 2314 Started 2318 Stopped 03/22/90 0017 Started 0023 Stopped for Maintenance 0428 Started for Testing 0429 Stopped 0714 Locally Started for Maintenance and Engineering Testing 03/22/90 1030 Locally Shutdown 03/22/90 1106 Started from CR 1243 Tripped on D/G High Lube 011 Temp.

03/23/90 0509 Started for Maintenance Run 1202 Stopped 92 % 7ect 05fiSOS

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UNIT 1 i

DIESEL GENERAIDK 18 (CONT'D)

DATE TIE COMENTS 03/23/90 1730 Started for 4 Hour Run 1731 Tripped.on Low Jacket Water Pressure / Turbo Lube Oil Pressure Low 1744 Started for 4 Hour Run 2222 Stopped 03/24/90 0048 Started for Maintenance 0049 "Hi Jacket Water Temp" Alarm In, Temp Verified to be Normal.

0121 Normal Stop 03/27/90 1649 Emergency Start Test 1822 Normal Shutdown 1909 Normal Start 1948 Stopped.

Simulated Hi Temp Lube Oil Trip 1951 Started.

Simulated LOSP at Engine Panel 1954 Stopped.

Simulated Hi Vibration Trip 1957 Normal Start 1959 Stopped.

Simulated Hi Crankcase Pressure Trip 2004 Started.

Simulated SI at Engine Panel 2010 Stopped.

Simulated Lo Lube Oil Pressure Trip 2220 Started.

Simulated Bus UY Signal 2317 Normal Shutdown 03/28/90 0403 Started.

Surveillance 14980-1 0537 Normal Shutdown 1350 '

Start to Perform Functional Test for MWO 1-89-03281 (Lo Lube Oil Pressure Trip Flow Orifices) 1355 Normal Shutdown 1356 Started.

Simulated UV for Functional on MWO 1-89-03281 1400 Normal Shutdown

.04/01/90 1623 Normal Start 1744 Normal Shutdown 04/04/90 1632 Started for Maintenance 1744 Stopped i

9a Pearcr 0 55910

UNIT 1 DIESEL GENE N 1B (CONT'D)

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DATE

' TIE COMENTS i

04/05/90 0030 Started. T-ENG-90-17 0035 Stopped 0307 Started.

14980 0509 Stopped l-J.

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UNIT 1 DIESEL M TOR 1A

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-DATE.

- TIE CO M NTS L

02/26/90

. 1509-Started. 24 Hour' Run for ESFAS i

02/28/90-0226 Secured from 24 Hour Run h

02/28/90

.0945'

. Started for ESFAS Testing 4

1210 Secured for ESFAS Testing i

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02/28/90 1700.

Started 3 Times in Series During ESFAS Testing I

'02/29/90 0218.-

Secured for_ ESFAS' Testing -

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03/01/90-0128~

. Started for ESFAS j

.03/02/90

- 0215.

Secured for ESFAS

-0912-Started for Maintenance

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. 1944 Secured for Maintenance

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03/12/90

- 1306 Started i

i; 2137 Stopped i

03/13/90-0009 Started 0506 Stopped i

I 03/20/90 0820 LOSP Occurred - Lost "A" RAT - DGIA Tied and Tripped (Several Alarms came in - not noted in i

thelog.)

0841 Auto Started after Sequencer Reset and Tripped 4-on Low Jacket Water Pressure I

0856 Emergency Break Glass Start Locally to Recover from Station 81ackout.

i 1029 RAT "B" Energized j

IBA03 Energized from "B" RAT 1040 1326 Shutdown l

2119 Started for Troubleshooting l-2206 Shutdown j

2223 Started for Troubleshooting 2228 Secured 2233-Started for Troubleshooting 2254 Secured 5

03/23/90 0254 Started for Maintenance Troubleshooting 0450 Secured 4

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CCk UNIT 1 DIESEL M TOR 1A DATE TIE COMENTS 03/23/90 1724 Started and Manually Stopped from CR 03/29/90 1109 Started. UV Test, Tied to 1AA02 1158 Normal Shutdown l

03/30/90 1920 Emergency Start 2115 Stopped 2235 Local Start.

2241 Trip Hi Temp Lube Oil 2254 Local 2300 Trip High Vibration 2313 Normal Start 2316 Stopped. Hi Crank Case Pressure 2328 SI 2334 Low Lube Oil Pressure 2343 Nonnal Start 2347 Normal Stop 2348 Normal Start 2358 Stop 03/31/90 0012 Nonnal St6rt 0014 Normal Stop 0016 SI 0019 CR 1827 Start Local 1837 Local Stop 1846 Local Start 1847 Stop 1856 Local Start 1857 Local Stop i

1904 Local Start 1906 Local Stop 1921 Local Start 1922 Local Stop 9A PRorect 053913

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DATE TIE C0f0ENTS 4

- 03/31/90 1955 Local Start 2012 Local Stop 2254 Started. UV Test Tied to 1AA02 2320 Nonnal Shutdown 04/01/90 0423 Started. Surveillance 14980-1 0556 Normal Shutdown 04/06/90 1345 Start. T-ENG-90-16 1346 Stop 1404 Start. T-ENG-90-16

-1405 Stop 1419 Start. T-ENG-90-16

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1430 Stop 2347 Start. T-ENG-90-11 04/07/90 0213 Stop 4

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