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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20216J9251999-09-30030 September 1999 Suppl to Special Rept:On 990621,11 Containment Hydrogen Monitoring Sys Chart Recorder Was Indicating Below Normal Operating Range.Caused by Excessive Wear on Valve Body & Discs of Bypass Pump.Sample Pump Replaced ML20212F7301999-09-21021 September 1999 Special Rept:On 990907,CR Operators Declared 12 Containment Hydrogen Monitoring Sys Inoperable for Planned Maint.Cause of Low Flow Condition Was Determined to Be Foreign Matl. Replaced Sample Pump Valve Discs ML20212B9081999-09-14014 September 1999 Special Rept:On 990901, 12 Containment Hydrogen Monitoring Sys Was Declared Inoperable for Planned Maint.Caused by Planned Maint Being Performed as Corrective Action.Check Valves with O Rings Were Replaced ML20209D0291999-07-0202 July 1999 Special Rept:On 990621,operator Identified That Number 11 Hydrogen Monitoring Sys (Hms) Chart Recorder Was Indicating Below Normal Operating Range.Cause Indeterminate.Licensee Will Complete Troubleshooting of Subject Hms by 990709 ML20207G2671999-03-0101 March 1999 Special Rept:On 990315,Nine Mile Point,Unit 1 Declared Number 12 Containment Hydrogen Monitoring Sys Inoperable. Caused by Degraded Encapsulated Reed Switch within Flow Switch FS-201.2-1495.Technicians Replaced Flow Switch ML20206P2391998-12-31031 December 1998 Special Rept:On 981222,operators Removed non-TS Channel 12 Drywell Pressure Recorder & Associated TS Pressure Indicator from Svc.Caused by Intermittent Measuring Cable Connection in non-TS Recorder Circuitry.Replaced Cable ML20206P2421998-12-30030 December 1998 Special Rept:On 981219,number 12 Hydrogen Monitoring Sys (Hms) Was Declared Inoperable When Operators Closed Valve 201.2-601.Caused by Indeterminate Failure of Valve 201.2-71. Supplemental Rept Will Be Submitted After Valve Is Repaired ML20198M3571998-12-23023 December 1998 Special Rept:On 981210,operators Declared Number 11 Inoperable,Due to Failure of CR Chart Recorder.Caused by Inverter Board in Power Supply Circuitry of Recorder Due to Component Aging.Maint Personnel Replaced Failed Inverter ML20196H0111997-07-11011 July 1997 Special Rept 97-001:on 970620,removed High Range Radioactive Noble Gas Effluent Monitor (Stack Ragems) from Service to Allow Secondary Calibr IAW Master Surveillance Schedule. Completed Calibr on 970628 & Returned Stack Ragems to Svc ML20129A3401996-10-15015 October 1996 Special Rept 96-001,rev 1:on 960806,stack Ragems High Range Monitor Was Removed from Svc & Not Restored to Svc in Seven Days.Caused by Malfunction of Interlock on Source. Interlock Components Replaced ML20117K5931996-09-0505 September 1996 Special Rept SR 96-001:on 960806,declared Stack Ragems High Range Monitor Inoperable.Caused by Difficulties Requiring Component Replacement.Developed Course of Action for Returning Stack Ragems Instrument ML20078A9311994-08-31031 August 1994 Special Rept:On 940818,inoperability of Containment Hydrogen Monitoring Unit 11 Occurred.Caused by Failure of K4 Relay in Auto Calibr Unit.Sticking Relay Released & Exercised ML20116B7521992-10-27027 October 1992 Special Rept 92-08:on 920929,Turbine Building High Radiation Noble Gas Monitor Declared Inoperable for Greater than Seven Days.Alternate Testing Performed Throughout Period of Inoperability ML20115G6461992-10-22022 October 1992 Special Rept 92-07:on 921015,determined That Stem & Disc Separated on Discharge Valve V-9-004 for Diesel Fire Pump P-9-102A.On 921021,fire Pumps Isolated.Redundant Fire Pump Secured & Valves Replaced ML20104B6081992-09-10010 September 1992 Special Rept 92-05:on 920727,condenser Bay Sprinkler Sys 2 Removed from Svc After Spurious Actuation of Sprinkler Head. Hourly Fire Watch Established While Sys Out of Svc.Sprinkler Head Replaced & Sys Returned to Svc on 920814 ML20105A5121992-09-10010 September 1992 Special Rept 92-06:on 920807,fire Diesel Pump 1 Declared Inoperable for More than 7 Days to Perform Preventive Maint.On 920811,diesel Engine Overheated.Solenoid Valve Replaced & New Cooling Water Strainers Installed ML20114C5191992-08-26026 August 1992 Special Rept 92-03:on 920705,electromatic Relief Valve C Inadvertently Opened While Testing Pressure Switch of Valve A.Caused by Personnel Error.Training Session Will Be Held & Engineering Work Request Submitted Re Switch Terminal Point ML20114A9701992-08-17017 August 1992 Special Rept 92-04:on 920724,fire Diesel Pump 2 Removed from Svc to Replace Battery Cables & Solenoid Valve.Correct 24 Volt Dc Coil Obtained from Mfg & Pump Returned to Svc on 920806 ML20096D4711992-05-0101 May 1992 Special Rept 92-02:on 920327,fire Diesel Pump 1 Out of Svc for More than 7 Days to Replace Pump Due to Marginal Discharge Pressure.Caused by Valve Seating Problem.Pump Replacement Expected to Be Completed by 920504 ML20100R7411992-04-10010 April 1992 Special Rept 92-01:on 920227,CO2 Fire Suppression Sys for 4,160-volt Switchgear Inoperable for More than 14 Days When Leaking Valve Stem Repaired on 920226.Possibly Caused by Moisture Intrusion.Corroded Components Replaced ML20087B8431992-01-0303 January 1992 Special Rept 91-09:on 911115,fire Diesel Pump 1-2 Failed to Meet Required Acceptance Criteria During Functional Test. Caused by Cloth Rag Becoming Lodged Inside Pump.Fire Diesel Pump 1-2 Rebuilt & Reinstalled on 911208 ML20076E2641991-08-13013 August 1991 Special Rept 91-08:on 910717,coolant Found Leaking from Cap on Heat Exchanger of Engine of Fire Diesel Pump 1-1.Caused by Wearing on HX Neck,Resulting in HX Failing to Hold Normal Pressure.Engine Secured & Work Request Initiated ML20076E3001991-08-12012 August 1991 Special Rept 91-07:on 910709,nonfunctional Fire Barrier Doors Between Fire Zones OB-FA-6 & TZ-FZ-11B Not Restored to Operable Status within 7 Days.Caused by Ventilation Flow Preventing Door from Closing.Fire Patrol Established ML20077K2271991-07-31031 July 1991 Special Rept 91-06 Re Nonfunctional Fire Barrier Door Not Repaired within 7 Days as Required by Tech Spec 3.12.E. Caused by Broken Door Closure Mechanism.Hourly Fire Watch Initiated.Door Mechanism Repaired on 910704 ML20082E1411991-07-23023 July 1991 Special Rept:On 910702,non-functional Fire Barrier Door Not Repaired within Seven Days as Required by Tech Specs. Caused by Faulty Door Closing Mechanisms.Util Evaluating Alternate Door Closing Mechanisms ML20073C9381991-04-18018 April 1991 Special Rept 91-04:on 910309,fire Detection Sys on Elevations 75' & 95' of Reactor Bldg Made Inoperable to Facilitate Maint Activities.Fire Watch Patrol Has Been Established to Compensate for Detection Sys ML20070T5341991-03-28028 March 1991 Special Rept:On 910222,inoperable Fire Hose Station 33 Not Restored to Operable Status within 14 Days as Required by Tech Specs.Caused by Maint to Angle Valve.Valve Reopened on 910312,restoring Hose Station 33 to Operability ML20070M5181991-03-14014 March 1991 Special Rept 91-02:on 901117,discovered That Fire Barrier Door Between 480-volt Switchgear Rooms a & B Nonfunctional Since 901110 & Not Repaired within 7 Days.Caused by Faulty Door Latching Mechanism.Fire Watch Established ML20058A7441990-10-16016 October 1990 Special Rept 90-04:on 900921,nonfunctional Fire Barrier Door Not Repaired within 7 Days.Fire Watch Established ML20245E7541989-06-0909 June 1989 Special Rept 89-02:on 890526,declared Fire Pump/Diesels 1-1 & 1-2 Inoperable.Caused by Loss of Fire Suppression Water. Pressure Switch & Associated Recorder for 1-2 Diesel Recalibrated Along W/Pump Discharge Pressure Gauge ML20247J2081989-05-22022 May 1989 Special Rept 89-01:on 890422,nonfunctional Fire Barrier Not Repaired within 7 Days as Required by Tech Spec 3.12.E. Fire Watch Established.Nonfunctional Fire Barrier Seal Plannned to Be Restored to Operable Status by 890523 ML20237C6711987-12-11011 December 1987 Special Rept 87-08:on 871112,fire Diesel Pump 1-2 Not Restored to Functional Status within 7 Days.Caused by Constraints Imposed by Increased outage-related Maint Activities.Fire Diesel Pump Restored to Functional Status ML20236S5201987-11-19019 November 1987 Special Rept 87-07:on 871020,nonfunctional Thermo Lag Fire Barrier Not Restored to Functional Status within 7 Days Per Tech Spec 3.12.E.Caused by Constraints Imposed by Increased Maint Activities.Fire Watch Established ML20236L3711987-10-29029 October 1987 Special Rept 87-06:on 870928-30,fire Barrier Penetration Seals Identified as Not Meeting Acceptance Criteria.Cause Not Stated.Fire Watch Established Immediately.Fire Barrier Seals Will Be Restored to Functional Status by 871030 ML20235B4411987-09-22022 September 1987 Ro:On 870811,spill of Reactor Bldg Closed Cooling Water Occurred.Caused by Failure to Follow Instructions on Switching & Tagging Request Form Re Valve Backseating. Procedures Will Be Revised & Training Provided ML20235G2151987-09-20020 September 1987 Ro:On 870911,w/reactor in Cold Shutdown Mode,Tech Spec Safety Limit 2.1.E Exceeded.Caused by Operator Error. Operators Received Training on Safety Limit,Applicable Procedures & Relevant Control Room Indications ML20214H9801987-05-0707 May 1987 Ro:On 870424,operator Personnel Blocked Open Two Torus to Drywell Vacuum Breaker Valves at Time When Primary Containment Integrity Was Required.Caused by Cognitive Personnel Error.Procedures Revised ML20215H3621987-04-0909 April 1987 Special Rept 87-02:on 870214,turbine Trip & Reactor Scram Occurred.Caused by Loose Wire Causing Loss of Feedwater Flow Signal.Following Reduction in Reactor Pressure All Electromatic Relief Valves Reseated Properly ML20206E3931987-04-0101 April 1987 Special Rept 87-01:on 870302,inoperable Fire Suppression Water Deluge Sys Not Restored to Functional Status within 14 Days from Time of Discovery.Caused by Long Lead Time for Procurement of Replacement Parts ML20209H2501987-01-23023 January 1987 Special Rept 86-017:on 861228,nonfunctional Fire Barrier Not Returned to Functional Status within 7 Days from Discovery.Hourly Fire Watch Established.Repairs Completed & Penetration Seal Restored to Functional Status on 870112 ML20207J2981986-12-17017 December 1986 Special Rept 86-16:on 861121,fire Barrier Door Between Monitor & Control Area Stairwell & Hallway Outside Cable Spreading Room Found Nonfunctional.Hourly Fire Watch Patrol Established.Door to Be Restored as Functional on 861222 ML20207J2821986-12-16016 December 1986 Special Rept 86-15:on 861110,penetrations Through Floor of 4160 Volt Switchgear 1D Vault & Floor of Motor Generator Set Room Found Degraded.As of 861117,penetrations Not Restored to Functional Condition.Hourly Fire Watch Patrol Initiated ML20211P6331986-11-24024 November 1986 Special Rept:On 861110,diesel Fire Pump Taken Out of Svc to Troubleshoot Lube Oil Pressure Switch.Sys Cross Tied to Unit 2 Fire Suppression Sys as Back Up.On 861026 & 28,occurrence Repts Written for Inoperable Fire Door & Pump,Respectively BECO-86-173, Partially Withheld Security Event Rept:On 861107,HVAC Duct, Penetrating Vital Area,Removed by Contracted Craft Workers Before Notifying Security.Cause Not Stated.Security Oversight of Subj Contract Work Intensified1986-11-12012 November 1986 Partially Withheld Security Event Rept:On 861107,HVAC Duct, Penetrating Vital Area,Removed by Contracted Craft Workers Before Notifying Security.Cause Not Stated.Security Oversight of Subj Contract Work Intensified BECO-86-171, Partially Withheld Security Event Rept:On 861106,temporary Vital Area Barrier Insp Found Barrier Could Be Breached. Barrier Modified & Compensatory Security Measures Released1986-11-10010 November 1986 Partially Withheld Security Event Rept:On 861106,temporary Vital Area Barrier Insp Found Barrier Could Be Breached. Barrier Modified & Compensatory Security Measures Released ML20211F4441986-10-17017 October 1986 Special Rept:On 860903 & 04,some Fire Barrier Penetrations Declared Nonfunctional & Fire Door D-107 Rubbing Against Side Jamb.Measures to Maintain Compliance W/Tech Spec Section 3.6.10.1 Implemented ML20197B1471986-10-0909 October 1986 Special Rept 86-14:on 860922 & 27,nonfunctional Fire Barrier Penetration Seals Not Restored to Functional Status within 7 Days.Hourly Fire Watch Patrol Established within 1 H. Restoration Expected by 861130 ML20211E0731986-09-26026 September 1986 Unplanned Operating Event Rept 85-6, Manual Reactor Trip Following MSIV Closure Due to Inadvertent Emergency Feedwater Actuation,851009 BECO-86-125, Partially Withheld Security Event Rept:On 860826,bomb Threat Received.Search Initiated.No Suspicious Objects Found1986-08-29029 August 1986 Partially Withheld Security Event Rept:On 860826,bomb Threat Received.Search Initiated.No Suspicious Objects Found ML20238E4601986-08-28028 August 1986 Partially Withheld Secrity Event Rept:On 860824,bomb Threat Received for Plants.Bomb Search Initiated.No Suspicious Objects Found 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G2161999-10-15015 October 1999 Errata Pages 2 & 3 for Safety Evaluation Supporting Amend 168 Issued to FOL DPR-63 Issued on 990921.New Pages Change Description of Flow Control Trip Ref Cards to Be Consistent with Application for Amend ML20216J9251999-09-30030 September 1999 Suppl to Special Rept:On 990621,11 Containment Hydrogen Monitoring Sys Chart Recorder Was Indicating Below Normal Operating Range.Caused by Excessive Wear on Valve Body & Discs of Bypass Pump.Sample Pump Replaced ML20217K4631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Nine Mile Point, Unit 1.With ML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With ML20212F7301999-09-21021 September 1999 Special Rept:On 990907,CR Operators Declared 12 Containment Hydrogen Monitoring Sys Inoperable for Planned Maint.Cause of Low Flow Condition Was Determined to Be Foreign Matl. Replaced Sample Pump Valve Discs ML20212B9081999-09-14014 September 1999 Special Rept:On 990901, 12 Containment Hydrogen Monitoring Sys Was Declared Inoperable for Planned Maint.Caused by Planned Maint Being Performed as Corrective Action.Check Valves with O Rings Were Replaced ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20212C4601999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Nine Mile Point Nuclear Station,Unit 1.With ML20210U4591999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Nine Mile Point, Unit 1.With ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With ML20209D0291999-07-0202 July 1999 Special Rept:On 990621,operator Identified That Number 11 Hydrogen Monitoring Sys (Hms) Chart Recorder Was Indicating Below Normal Operating Range.Cause Indeterminate.Licensee Will Complete Troubleshooting of Subject Hms by 990709 ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With ML20210B9081999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Nine Mile Point Unit 1.With ML20212H5491999-06-18018 June 1999 Non-proprietary Rev 4 to HI-981983, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool ML20209F8811999-06-0808 June 1999 Rev 1 to NMP Unit 1 COLR for Cycle 14 ML20207G2261999-06-0707 June 1999 SER Accepting Proposed Mod to Each of Four Core Shroud Stabilizers for Implementation During Current 1999 Refueling Outage at Plant,Unit 1 ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20196E2111999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Nmp,Unit 1.With ML20207B0241999-05-18018 May 1999 Safety Evaluation of Topical Rept TR-107285, BWR Vessel & Intervals Project,Bwr Top Guide Insp & Flaw Evaluation Guidelines (BWRVIP-26), Dtd December 1996.Rept Acceptable ML20206U5351999-05-17017 May 1999 SER Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant, Units 1 & 2 ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With ML20196L2301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Nmp,Unit 1.With ML20205L0541999-04-0101 April 1999 Nonproprietary Replacement Pages to HI-91738,consisting of Section 5.0, Thermal-Hydraulic Analysis ML20205S5701999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for NMP Unit 1.With ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207G2671999-03-0101 March 1999 Special Rept:On 990315,Nine Mile Point,Unit 1 Declared Number 12 Containment Hydrogen Monitoring Sys Inoperable. Caused by Degraded Encapsulated Reed Switch within Flow Switch FS-201.2-1495.Technicians Replaced Flow Switch ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With ML20204C9971999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Nine Mile Point,Unit 1.With ML20207E9311999-02-26026 February 1999 Part 21 Rept Re Sprague Model TE1302 Aluminum Electrolytic Capacitors with Date Code of 9322H.Caused by Aluminum Electrolytic Capacitors.Affected Capacitors Replaced ML17059C5501999-01-31031 January 1999 Rev 0 to MPR-1966(NP), NMP Unit 1 Core Shroud Vertical Weld Repair Design Rept. ML20199M0891999-01-22022 January 1999 Part 21 Rept Re Failure of Square Root Converters.Caused by Failed Aluminum Electrolytic Capacitory Spargue Electric Co (Model Number TE1302 with Mfg Date Code 9322H).Sent Square Root Converters Back to Mfg,Barker Microfarads,Inc ML20195E8321998-12-31031 December 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Sys & Procedures, for Period of June 1997 to Dec 1998.With ML20210R8441998-12-31031 December 1998 1998 Annual Rept for Energy East ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With ML20199K9331998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20206P2391998-12-31031 December 1998 Special Rept:On 981222,operators Removed non-TS Channel 12 Drywell Pressure Recorder & Associated TS Pressure Indicator from Svc.Caused by Intermittent Measuring Cable Connection in non-TS Recorder Circuitry.Replaced Cable ML20206P2421998-12-30030 December 1998 Special Rept:On 981219,number 12 Hydrogen Monitoring Sys (Hms) Was Declared Inoperable When Operators Closed Valve 201.2-601.Caused by Indeterminate Failure of Valve 201.2-71. Supplemental Rept Will Be Submitted After Valve Is Repaired ML20198M3571998-12-23023 December 1998 Special Rept:On 981210,operators Declared Number 11 Inoperable,Due to Failure of CR Chart Recorder.Caused by Inverter Board in Power Supply Circuitry of Recorder Due to Component Aging.Maint Personnel Replaced Failed Inverter ML20198D9361998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Nine Mile Point,Unit 1.With ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20155E2001998-11-0202 November 1998 Safety Evaluation Approving NMP 980227 Request for Extension of Reinspection Interval for Core Shroud Vertical Welds at NMP1 from 10,600 Hours to 14,500 Hours of Hot Operation ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With ML20195J4141998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20154R4981998-10-20020 October 1998 Core Spray Sys Insp Program - 17R ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20154D8401998-10-0505 October 1998 Safety Evaluation Accepting Proposed Changes Related to PT Limits in Plant,Unit 1 TSs 1999-09-30
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o O 1 Jers~ey Central Power & Light Company M AossoN AVENUE AT PUNCH sOWL Ro AD e MORRISToWN. N.J. o7960 e 539 6111 April 20, 1972 . . ~ .
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/N f& <?p Dr. Peter .^.. Morris, Director _.
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d Division of Reactor Licensing 5 .
\ .,, s -l United States Atomic Energy Commission Washington, D. C. 20545 j ~y * ,y /
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. % . . , , Q@ ,
Dear Dr. Morris:
Subject:
Oyster Creek Station Docket No. 50-219 Loss of Secondary Containment Integrity The purpose of this letter is to report to you a violation of a Limiting Condition for Operation in that Secondary Containment Integrity was not maintained as required by Specification 3.5.B.1.
of our Technical Specifications.
On April 11, 1972, during performance of a routine weekly surveillance test of isolation of the Reactor Building and initiation of the Standby Gas Treatment System due to simulated high radiation l levels on the Reactor Building Operating Floor and in the Reactor Building Ventilation Exhaust ducts, the supply dampers for the Reactor Building Ventilation System failed to close as required.
As a result of this failure, Secondary Containment was not in effect.
Isolation of the Reactor Building Ventilation System supply damper is initiated by "b" contacts from the Reactor Building Ventilation System supply fans, SF1-12, SF1-13, and SF1-14 wired in series. However, due to an electrical problem with supply fan 1-13, which resulted in the discovery that the motor was shorted, its supply breaker was racked-out.
Thus, the logic control circuit for the dampers was " opened", the normal situation with the fans in operation. When the remaining fans were '
tripped during the surveillance test conducted at 2:00 a.m. on April 11, 1972, the logic control circuit was still open, the damper control relays remained de-energized, and the dampers did not close.
8302280147 720425 PDR ADOCK 05000220 G PDR
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1
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1 O o Dr. Peter A. Morris Page II April 20, 1972 The logic circuit was restored by disconnecting the motor leads from the breaker and racking-in the breaker. At 9:20 a.m.
on April 11, 1972, an operability check of Reactor Building Isolation was conducted and proved to be satisfactory. A caution tag was placed at the fan control switches in the Control Room to notify operators that if a supply fan breaker is racked-oug the Reactor Building supply damper isolation control logic is defeated unless a jumper is installed in the breaker cabinet. A similar caution note is being stenciled locally on the supply fan breakers.
As noted in the FDSAR, the primary objective of the Secondary Containment System is to minimize ground level release of airborne radioactive materiale and to provide for controlled elevated release of the building atmosphere under accident conditions. The containment systems, Primary and Secondary, provide the principle mechanism for mitigation of accident consequences. The off-site accident consequences, however, are relatively insensitive to the Reactor Building in-leakage rate as long as the Standby Gas Treatment System can maintain the building at a vacuum. In this particular instance, the supply and exhaust fans tripped, the exhaust dampers closed, and the Standby Gas Treatment System was initiated. With the above situation, the i air supply to the building was not only via the various in-leakage paths but also, and no doubt primarily, via the Reactor Building supply dampers.
Any accident conditions postulated that require secondary containment in determining environmental releases would, under these conditions, have a second path permitting release of the Reactor Building air at approximately a 60-foot elevation.
In order to prevent a reoccurrence of this incident, a circuit design change will be implemented that will permit a Reactor Building supply f an breaker to be racked-out for maintenance without defeating the Reactor Building supply damper isolation logic. Until this design change can be implemented, a standing order will be issued instructing plant personnel in the appropriate practice to be followed to avoid defeating the Reactor Building supply damper isolation logic.
Very truly yours, q I0N I il Ivan R. Finf ock Jr.
Manager, Nuclear Generating Stations IRF/pk Enclosures cc: Mr. J. P. O'Reilly, Director Division of Compliance, Region I