ML20086M129
| ML20086M129 | |
| Person / Time | |
|---|---|
| Site: | Vogtle |
| Issue date: | 11/30/1991 |
| From: | Hooper G GEORGIA POWER CO. |
| To: | |
| Shared Package | |
| ML20086M127 | List: |
| References | |
| NUDOCS 9112170230 | |
| Download: ML20086M129 (12) | |
Text
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i ENCLOSURE-1.
.V0GTLE ELECTRIC GENERATING PLANT - UNIT 1
-MONTHLY OPERATING REPORT FOR NOVEMBER 1991-IglE OF CONTENTS r;~
. NARRATIVE REPORT Page VI-1 OPERATING DATA-REPOR1-:
Page VI-2
~ AVERAGE. DAILY POWER LEVEL Page VI -
UNIT-SHUTDOWNS AND POWER' REDUCTIONS Page VI-4 i
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g, - l NARRATIVE REPORT DOCKET NO. 424 UNIT 1 DATE:
DECEMBER S,1991 COMPLETED BY: G. L HOOPER TELEPHONE:
(404) 826 -4104
- NOVEMBER 01- 00:00 UNIT 1 IN MODE 5, PREPARATIONS FOR Flu. AND VENT iN PROGRESS.
NO'KMBER 12 04:27 _ UNIT 1 EfCERED MODE 4.
NOVEMBER - 13 17:00 - lNITIATED RCS COOLDOWN TO MODE 5 TO IMPLEMENT DESIGN CHANGE ON LEAKING BORON INJECTION PYPASS VALVE.
' NOVEMBER 13 19:12_- UNIT 1 ENTERED MODE 5.
NOVEMBER 15 15:54 ' UNIT 1 ENTERED MODE 4.
NOVEMBER 16 01:58 UN!T 1 ENTERED MODE 3.
~ NOVEMBER.19 09:57 ' UNIT 1 ENTER 1D MODE 2.
- NOVEMBER.19 - 14:14 UNIT 1 REACTOR CRITICAL NOVEMBER 20 18:27 - UNIT 1 ENTERED MODE 1.
' NOVEMBER 23 09:22 INITIATED POWER REDUCTION FROM 8% TO 1% TO REPAIR TURBINE TURNING GEAR.
NOVEMBER 23 10:36 UNIT 1 ENTERED MODE 2.
NOVEMBER 24 ' C4:16 UNIT 1 ENTERED MODE 1.
' NOVEMBER 24 20:56 UNIT 1 GENERATOR TIED TO GRID.
NOVEMBER 25 ? 12:53 UNIT 1 COMMENCED REDUCING TURBINE LOAD FOR TURBINE OVERSPEED
. TESTING AND MAINTENANCE.
NOVEMBER 25 16:10 - UNIT 1 TURBINE TRIPPED FROM 00 MWe.
- NOVEMBER 26 00:49 - UNIT 1 ENTERED MODE 2 IN PREPARATION FOR TURBINE BALANCE SHOT.
NOVEMBER 27 02:07 UNIT 1 ENTERED MODE 1.-
t NOVEMBER 27 : 10:10 UNIT 1 GENERATOR 11ED TO GRID.
- NOVEMBER 30 23
- 59 UNIT 1 AT 76% POWER, 80% PLATEAU POWER ASCENSION TESTING IN PROGRESS WITH NO OPERATIONAL PROBLEMS.
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V1-1
OPERATING DATA REPORT DOCKET NO. 50-424 OATE:
DECEMBER 5,1991 COMPETED BY: G. L HOOPER TELEPHONE:
(404) 826 -4104 OPERATING ST?.10S
- 1. UNIT NAME:
VEGP UNIT 1
- 2. REPORT PERIOD:
NOVEMBER 1991
- 3. UCENSED THERMAL POWER (MWt):
3411
- 4. N AMEPLATE RATING (GROSS MWe):
1215
- 5. DESIGN ELECTHCAL RATING (NET MWe):
1101
- 6. MAXIMUM DEPENDABLE CAPACITY (GROSS MWe):
1154
- 7. MAXIMUM DEPENDABLE CAPACITY (NET MWe):
1100
- 8. IF CHANGES OCCUR IN CAPACITY RATINGS N/A (ITEMS 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS:
- 9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWe):
NO RESTRCTIONS
- 10. REASONS FOR RESmlCTION,IF ANY:
N/A THIS MONTH YR.TO DATE CUMULATIVE
- 11. HOURS IN REPORTING PERIOD:
720 8016 39457
- 12. NUMBER OF HOURS REACTOR WAS CRITICAL:
268.8 6436.4 32894.9
- 13. REACTOR RESERVE SHUTDOWN HOURS:
0.0 0.0 0.0
- 14. HOURS GENERATOR ON-UNE:
105.1 6272.7 32027.0
- 15. UNIT RESERVE SHUTDOWN HOURS:
0.0 0.0 0.0
- 16. GHOSS THERMAL ENER3Y GENERATED (MWH):
215953 20927762 106121373
- 17. GROSS ELEC. ENERGY GENERATED (MWH):
56879 7035769 35330219 18.' NET ELEC. ENERGY GENERATED (MWH):
34399 6692259-33454169
- 19. REACTOR SERVICE FACTOR 37.3 %
80.3 %
83.4 %
- 20. REACTOR AVAILABluTY FACTOR 37.3 %
80.3" 83.4 %
-21. UNIT SERVICE FACTOR:
14.6 %
78.3%
81.2%
- 22. UNIT AVAILABluTY FACTOR:
14.6%
78.3%
81.2 %
- 23. UNIT CAPACl1Y FACTOR (USING MDC NET):
4.3%
75.9 %
78.2%
- 24. UNIT CAPACITY FACTOR (USING DER NET):
4.3%
-75.8%
77.0 %
- 25. UNIT FORCED OUTAGE RATE:
0.0%
0.0%
7.3%
- 26. SHUTDOWNS SCHEDULED OVER THE NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH):
NONE
- 27. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
N/A y
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- UNIT 1. AVERAGE DAILY DOCKET NO. ' 50-424
. POWER LEVEL
_ DATE:
DECEMBER S,1991 COMPLETED BY: G. L HOOPER TELEPHONE:
(404) 826 -4104
'- d, __
DAY Net MW 1
0 2
0 3
0 4
0
.5 0
6 0
7 0
~,
8-0 9
0 10 0
0 i
11 12 0
13 0
14
'O 15 0
-16 0
-17 0
'18 0.
-19 0
20.
0
-~ 21 -
0 22 0
23 0
24 86-25 100-N.
0
-27
-150.
28 -
450'
-F
-545 30
-768' o
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VI-3
UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50 - 424 DATE:
DECEMBER 5,1991 UNIT NAME:
VEGP UNIT 1 COMPLETED BY: G. L HOOPER TELEPHONE:
(404) 826 - 4104 REPORT MONTH NOVEMBER 1991 R
M S
E E
Y T
A T
UCENSEE SC Y
S H
EVENT TO COMPONENT CAUSE & COh.dCTNE P
DURATION O
O REPORT ED CODE ACTION TO NO.
DATE E
(HOURS)
N D
NUMBER ME (SUBCODE)
PREVENT RECURFENCE 91-1 9 -15 S
572.9 C
4 NA ZZ n7777 SEE BELOW 91 - 2 11 - 25 S
42 B
1 NA TA 777777 SEE BELOW F: FORCED REASON:
METHOD:
EVENTS REPORTED INVOLVE S: SCHEDUWD A-EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL A GREATER THAN 20%
(
B-MAINTENANCE OR TEST 2 - MANUAL SCRAM REDUCTIONIN AVERAGE C-REFUEUNG 3 - AUTO. SCRAM DA!LY POWER WVEL FOR D-REGULATORY RESTRICTION 4 - CONTINUATIONS THE PRECEDING 24 HOURS.
E-OPERATOR TRAINING & UCENSE 5 - LOAD REDUCTION F-ADMINISTRATIVE 9 - OTHER (EXPLAIN)
G-OPERATIONAL ERROR (E'APLAIN)
H-OTHER (EXPLAIN)
EVENT 91-1 CAUSE: SCHEDULED REFUEUNG OUTAGE CORPECTNE ACTION: MAJOR SAFETY RELATED CORRECTIVE MAINTENANCE INCLUDED COMPLETING MA!N1ENANCE ON CENTRIFUGAL CHARGING PUMP A AND THE IMPWMENTATION J.F A DESIGN CHAT'3E ON A LEAKING BORON INJECTION BYPASS VAL'K.
CRITICAL PATH WAS:
CCP A PUMP MA!NTENANCE, RESTORE AND DECON REFUEUNG CAVITY HEATUP, PREPARE FOR MODE 4, MODE 4 ENTRY HEATUP, PREPARE FOR MODE 3, MODE 3 ENTRY HEATUP, PREPARE FOR MODE 2, MODE 2 ENTRY LOW POWER PHYSICS TESTING, PREPARATION FOR MODE 1 ENTRY MODE 1 ENTRY SYNCHRONIZE GENERATOR TURBINE TESTING EVENT 91-2 CAUSE: SCHEDUGO OUTAGE FOR TURBINE OVERSPEED TESTING, EXTENDED TO ALSO INCLUDE TURSINE BALANCE SHOT.
CORRECTTE ACTION:
PERFORMED OVERSPEED TEST AND ADJUSTED OVERSPEED TRIP.
PERFORMED TURB:NE BALANCE SHOT.
V1-4
9 9
ENCLOSURE 2 V0GTLE ELECTRIC GENERATING plt" - UNIT 2 MONTHLY OPERATING REPORT FOR N IMBER 1991 TABLE OF CONTENTS NARRATIVE REPORT Page V2-1 OPERATING DATA REPORT Page V2-2 AVERAGE DAILY POWER LEVEL Page V2-3 UNIT SHUTDOWNS AND POWER REDUCTIONS Page V2-4 i
9
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NARRATIVE REPORT DOCKET NO. 50 -425 UNIT 2 DATE:
DECEMBER 5,1991 COMPETED BY: G. L HOOPER TEEPHONE:
(404) 826 - 4104 NOVEMBER 01 00:00 UNIT 2 AT 100% POWER WITH NO OPERATIONAL PROBLEMS.
NOVEMBER 17 17:51 UNIT 2 BEGAN POWER REDUCTION TO 72% FOR MFP B POYER SUPPLY REFLACEMENT, NO'vEMBER 18 18:15 UNIT 2 BEGAN ASCENT FROM 78% TO 100% POWER.
NOVEMBER 19 03.00 UNIT 2 RETURNED TO 100% POWER.
NOVEMBER 30 23:59 UNIT 2 AT 100% POWER WITH NO OPERATIONAL PROBEMS.
V2-1
~
OPERATING DATA REPORT DOCKET NO. 50 425 DATE:
DECEMBER 5.1991 COMPLETED BY: G. L HOOPER TELEPHONE:
(404) 820 -4104 OPEPATING STATUS
- 1. UNIT NOAE:
VEGP UNIT 2 2 REPORT PERIOD:
NOVEMBER 1991
- 3. UCENSED THERMAL POWER (MWt):
3411
- 4. NAM 6PLAIE FtATING (GROSS MWe):
1215
- 5. DESIGN ELECTT1 CAL RATING (NET MWe):
1101
- 6. MAX! MUM DEPENDASU2 CAPACITY ('3ROSS MWe):
1151
- 7. MAXIMUM DEPENDAF i' CAPACITY (NET MWe):
1097 8.lF CHANGES OCCUR IN CAPACITY RATINGS N/A GTEMS 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS:
- 9. POWIM lEVELTO WHICH RESTRICTED IF ANY (NET MWe)
NO RESTRICTIONS
- 10. REASONS FOR RESTRICTION,IF ANY:
N/A THIS MONTH YR. TO DATE CUMJLATIVE i
- 11. HOURS IN REPOR11NG PERIOD:
720 8010 22201
- 12. NUMBER OF HOURS REACTOR WAS CRITICAL:
720.0 7711.0 20248.4 1J. REACTOR RESERVE SHUTD0%N HOURS:
0.0 0.0 0.0 s
- 14. HOUR) GENERATOR ON-UN:.i:
720.0 7632.5 19867.4
- 15. UNIT RESERVE SHUTDOWN HOURS:
0.0 0.0 0.0
- 16. GROSS THERMAL ENERGY GENERATED (MWH):
2433457 25025520 G3924765
- 17. GROS 3 ELEC. ENERGY GENERATED (MWH):
834819 847G373 21534811
- 18. NET ELEC. ENERGY GENERATED (MWH):
796779 8064383 2046G471
- 19. REACTOR SERVICE FACTOR 100.0 %
90.2%
91.2%
- 20. REAC70R AVAJLABlWTY FACTOR 100.0 %
C6.2%
91.2%
- 21. UNIT SERVICE FACTOR:
100.0 %
95.2%
09.5%
- 22. UNIT AVAILAD:UTY FACTOR:
100.0 %
05.2%
89.5%
100.9 %
91.7 %
B3.9%
- 24. UNIT CAPACITY FACTOR (USING der"..t!T)-
100.5 %
91.4 %
83.7 %
- 25. UNIT FORCED OUTAGE RATE:
0.0%
2.3%
2.3%
- 26. SHUTDOWNS SCHEr0 LED CV7RTHE NEXT 6 MONTHS (TYPE, DATE. AND DURAT10N OF EACH):
PEFUEUNG - MARCH 13,1992 - 58 DAYS
- 27. !F SHUTDOWN AT END OF REPORT PERIOD, EST1 MATED DATE OF STARTUP:
N/A a
V2-2 E
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4 UNIT 2 AVEFMGE DAILY DOCKET NO. 50 -425 POWERITVEL DATE:
DECEMBER 5,1991 r OMPLETED BY: G. L HOOPER TELEPHONE:
(404) 826-4104 DAY Not MW 1
1111*
2 1115
- 3-1121
- 4-1122
- 5 1122
- 6 1121
- 7 1121
- 8 -
1121
- 9 1121
- 10 1121
- 11 1120
- 12 1120
- 13-1120
- 14 -
1114
- 15 1113
- 16 _ _
1110*
17 1050 18 881 10.
1103
- 20 1100
- 21 1104*
22 -
1111 *--
23 1116
- 24 1122
- 25 -
1123*
26 1122
- 27 1122 *
- 28 t123
- 29 -
1115*
30 1110 *
+-
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UNIT SHUTDOWNS AND POWER REDUCTION,
DOCKL~T NO, 50 -425 DATE:
DECEMBER 5,1991 UNIT NAME VEGP UNIT 2 COMPLETED BY: G. l HOOPCR TELEPHONE:
(404) 826 - 4104 REPORT MONTH.
NOVEMBER 1991 R
M S
E E
Y T
A T
UCENSEE SC Y
S H
EVENT TO COMPONENT CAUSE & CORRECTNE P
DURATION O
O REPORT ED CODE ACTION TO NO.
DATE E
(HOURS)
N D
NUMBER ME (SUBCODE)
PREVENT RECURP5NCE NA NA NA NA NA NA NA NA NA NA I
F: FORCED REASON.
ME7 ICD; EVE.WTS REPOkiED INW>LVE 8: SCHEDL.T A-ECUIPVENT FAlLURE (EXPLA N) 1 - MANUAL A ORr.\\TER Tl MN 20%
B-MAINTENANCE OR TEST 2 - MAffJAL SCMM REDUCTON IN AVEMGE C-REFUCUNG 3 - AUTO. SCMM DAILY POWER FVEL FOR D-DEGULATORY RESTRICTON 4 - CON 11NUATKWS THE PRECEDINO 24 HOURS.
E-OPERATOR TRAINING & UCENSE S - LOAD REDUCTON F-ADMINISTRATIVE 9 - OTHER ' EXPLAIN) 0-OPrMTONAL ERFOR (EXPLAIN)
H-01HER (EXPLAIN) l I
V2-4 i
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I ENCLOSURE 3 V0GTLE ELECTRIC GENERATING PLANT - UNITS 1 AND 2 MONTHLY OPERATING REPORT FOR NOVEMBER 1991 CHALLENGES TO PORY OR SAFETY VALVES e
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(ENCLOSURE 3)
DOCKET NOS. 50-424,50 -425 i
VEGP UNfTS 1 & 2 DATE:
DECEMBER 5,1991 COMPETED BY: G. L HOOPER t
TELEPHONE:
(404) 826 -4104 i
EVENT DATE TAG NO.
TYPE DESCRIPTION E
THERE WERE NO CHALENGES TO POh / OR SAFETY VALVES.
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