ML20086L517

From kanterella
Jump to navigation Jump to search
AO 74-11:on 740318,main Steam Line Drain Valve MO-2-77 Failed to Close.Caused by Malfunction of Group I Isolation Circuitry.Valve Operated Correctly During Group I Logic Sys Functional Surveillance Test
ML20086L517
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 03/26/1974
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: Giambusso A
US ATOMIC ENERGY COMMISSION (AEC)
References
AO-74-11, NUDOCS 8402080281
Download: ML20086L517 (2)


Text

. _ _ _ _ . - - - . - - - - - - - - - - - -

n l

U PHILADELPHIA ELECTRIC COMPANY ,?

/

2301 MARKET STREET s/S

  • Rm, . o PHILADELPHI A. PA.19101 -*

h7g:R 281974.. ql-(2isi e494o00 (g1 '

ra, Q

,Q /

. i ,w yy . .a March 26, 1974 . V,gg";p'

~WW Mr. A. Giambusso Deputy Director of Reactor Projects United Sta tes Atomic Energy Conrnission Directorate of Licensing Washington, D.C. 20545

Dear Mr. Giambusso:

Subject:

Abnormal Occurrence The following occurrence was reported to Mr. D. Caphton, A.E.C. Region I Regulatory Opera tions Office on March 19, 1974 Written notification was made to Mr. James P. O'Reilly, Region I Regulatory Operations Office on March 19, 1974. In accordance with Section 6.7.2.A of the Technical Specifications, Appendix A of DPR-44 for Unit 2 Peach Bottom Atomic Power Station, the following report is being submitted to the Directorate of Licensing as an Abnormal Occurrence.

Reference:

License Number DPR-44, Amendment No.1 Technical Specification Table 3.7.4 Report No.: 50-277-74-11 Report Date: Ma rch 19, 1974 Occurrence Date: March 18, 1974 '

Faci li ty: Peach Bottom Atomic Power Station - Unit 2 R.D. 1, Delta, Pennsylvania 17314 Identi fication of Occurrence:

Following a Group I isolation caused by instrument sur-veillance testing, it was determined that the main steam line drain valve M0-2-77 failed to close.

Conditions Prior to Occurrence:

Plant stable at approximately 48% power. -

P Description of Occurrence: /

3 During instrument surveillance testing a Group I isolation

~

qI J/ch

'\ 644 was initiated due to valving an inscrument into service. Main steam s402080281 740326 /M

. PDR ADOCK 05000277 COPY SENT REGION

i. . . - .S PDR _

~

l Mr. A. Gitmbusso March 26, 1974 Page 2

~

line drain valve M0-2-77 failed to close as required by Group I isolation. The valve was manually closed by the operator immediately following the occurrence.

Designation of Apparent Cause of Occurrence:

Since the valve was manually operable immediately af ter this

occurrence, the Group I isolation circuitry apparently malfunctioned and did not request a valve closure.

Analysis of Occurrence:

This valve, MO-2-77, is in series with another isolation valve M0-2-74, which did close correctly as a result of the isolation.

Because the line was isolated, there was no safety implicatio.,.

Corrective Action:

, The valve was operated numerous times following this occur-rence from the test pushbutton in the automatic isolation circuitry.

The valve also operated correctly during the Group I logic system functional surveillance test which was performed to ensure proper relay

, and valve operation. No specific cause for the failure of this valve to close on the Group I isolation was identified as a result of this i nves ti ga ti on.

Very truly yours, i 1, i

/ / /l'f . ay/

M.,J. Cooney Asst. Gent. Supt.

Generation Division cc: Mr. J. P. O' Rei l ly Director, Region I United States Atomic Energy Commiasion 631 Park Avenue King of Prussia, PA 19406 -

l l

g 0

' __ .