ML20086K504

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Telecopy AO 75-8:on 750124,reactor a Low Water Level Scram/ Reactor High Water Level HPCI Turbine Trip Instrument LIS-2-2-3-101D Out of Svc.Caused by Incomplete Testing. Instrument Backfilled,Vented & Returned to Svc
ML20086K504
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 01/27/1975
From: Ullrich W
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20086K497 List:
References
AO-75-8, NUDOCS 8401270168
Download: ML20086K504 (1)


Text

. . . .. ., .... ,-. m ..m..n w wm mu i e i' s .t) :.,V. . Peach Botten Atomic PawSr Statinn Delto,Pennsylvh 17314 Mr. James P. O'Reilly, Director January 27, 1975 United States Atomic Energy Commission Directorate of Regulatory Operations 631 Park A. venue King of Prussia, Pennsylvania 19406 -

Subj ec t s-Abnormal occurrence 24-Hour Notification.

Confirming V. T. U11 rich's phone conversation with Mr. Robert Carlson, A.E.C. Regie Regulatory Operations Office on January 25, 193

Reference:

License Number DPR-44 ,.-: 7'" ~..

Technical Specification

Reference:

Tables 3.1.1 and-3.2.Bg ( ,[s, '

.c ,

Report No.: 50-277-75-8 /Y '0 ' ' x.k

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Report Date: January 25, 1975

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Occurrence Date: January 24, 1975 t --4 d) * '

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y,3 Tacility: Peach Eottom Atomic Power Station '

u.;. ,$ o'k,,/.,,h d R.D. 1. Delta, Pennsylvania 17314 -

c3 ;f a J Identifiestion of Occurrence: -

Aid.Mj!f3 N

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w fx gg reactor low vater level scram / reactor high water level HPCIc tuybijsa tip instru=ent (%15-2-2-3-101D) not in service.

Conditions Prior to Occurrence:

Unit 2 start @g. up -epproxinstely 20% power.

uescription of Occurrences Darins a r'outine plant startup inspection of plant safety instrumentation, one of the reactor low water Icvol scram /roactor high water level HPCI turbine trip instrucents. (CIS.-2-2-3-101D)uas found to not have been properly returned to service following naintenhnce on its instrutaent test valve block.

Designatio' n of Apparent Cause of Occurrence:

The testing specified to be conpleted following naintenance was incoc:pleccia in that verification of correct valve lineup was not required.

Analysis of Occurrence:

The switch was found in the equalized condition which drives it full upscale and gives one of the two needed reactor high water level turbine trips for the HPCI.

The reactor Low Water Level Scran switches are arranged in a one-of-two twice logic chus, no one switch being disabled can render this scran inoperable.

Because the other three scran switches and the other reactor high water 1cvel

HPCI turbine trip avitch were operabic, the safety implication't are mininal.

Corrective Action:

This instrunent vaa tenediately backfilled, vented and returned to rervice.

Verbal instructions have been issued to remind personnel to be more careful') in specifying verification testing following naintenance.

Failure Data s None previous. 8401270168 750203 PDR ADOCK 05000277

  • S PDR Very truly yours, 7: s 7WA W. T. Ullrich, Superintendent 9 g'!y ,

1055 Peach Bottom Atomic Power Station s

f COPY SENT REGION _

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