ML20086J485

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AP 74-5:on 750910,emergency Shutdown Panel RCIC Static Inverter Tripped from Operation of Barometric Condenser Condensate Pump.Caused by Failure in Trip Circuitry of Inverter Unit.Inverter Unit Replaced
ML20086J485
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 09/20/1974
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: Anthony Giambusso
US ATOMIC ENERGY COMMISSION (AEC)
Shared Package
ML20086J487 List:
References
AO-74-5, NUDOCS 8401240036
Download: ML20086J485 (2)


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September 20, 1974 Mr. A. Giambusso Deputy Director of Reactor Projects

. United States Atomic Energy Commission Directorate of Licensing Washington, DC 20545

Dear Mr. Giambusso:

Subject:

Abnormal Occurrence The following occurrence was reported to Mr. W. Baunack, A.E.C. Region 1 Regulatory Operations Office on September 11, 1974.

Written notification was made to Mr. James P. O'Reilly, Region 1 Regulatory Operations Office on September 11, 1974.

In accordance with Section 6.7 2.A of the Technical Specifications, Appendix A of DPR-56 for Unit 3 Peach Bottom Atomic Power Station, the following report is being submitted to the Directorate of Licensing as an Abnormal Occurrence.

Reference:

License Number DPR-56, Amendment Number 1 Technical Specification 3 5 0 Report No.:

50-278-74-5 Report Date:

September 20, 1974 Occurrence Date: September 10, 1974 Facility:

Peach Bottom Atomic Power Station R. D. 1, Delta, Pennsylvania 17314 Identification of Occurrence:

Unit 3 Emergency Shutdown Panel RCIC static inverter tripping from operation of the Barometric Condenser Condensate Pump.

Conditions Prior to Occurrence:

The reactor was operating at approximately 22% power with the RCIC in test at the Emergency Shutdown Panc1.

8401240036 740920 9860 PDR ADDCK 05000278

.' COPY SENT REGION __

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Mr. A. Giambusso Szptember 20, 1974

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Page 2 s-Description of Occurrence:

During the test run of the RCIC from the Emergency Shutdown Panel, the static inverter feeding the RCIC flow controller at the Emer-gency Shutdown Panel tripped repeatedly upon automatic starting of the RCIC Barometric Condenser Condensate Pump. Each time, it was immediately reset.

Designation of Apparent Cause of Occurrence:

Investigation points to a failure in the trip circuitry of the particular inverter unit.

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Analysis of Occurrence:

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At the time of the inverter trippings, all other Unit 3 Emer-gency Core Cooling Systems were operable. Due to this, and the short time intervals that the inverter was in a tripped condition, this occurrence has minimal safety significance.

Corrective Action:

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The inverter unit was replaced with a spare. A storage oscilloscope was installed to monitor inverter input and output during i

the testing. This spare inverter did not trip throughout the remainder of the RCIC testing at the Emergency Shutdown Panel.

The input filter network as outlined in A0-50-277-74-40 is

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in progress, in that two'of six filters have been installed.

Failure Data:

Five other trippings of RCIC inverters have been reported as:

A0-50-277-74-14, 20, 37, 39, and 40.

Very truly yours,

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f'tYL4 M.

. Cooney f

Ass' t Gen' t Supe'rintendent Generation Division cc:

Mr. J. P. O'Reilly Director, Region !

United States Atomic Energy Commission 631 Park Avenue King of Prus'sia, PA 19406 e

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