ML20086J111

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AO 74-39:on 741221,drywell Equipment Drain Sump Isolation Valve AO-3-20-74 Failed to Close on Primary Containment Isolation Sys Isolation.Caused by Solenoid Valve Stuck in Energized Position,Preventing Valve Closure
ML20086J111
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 12/31/1974
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: Anthony Giambusso
US ATOMIC ENERGY COMMISSION (AEC)
Shared Package
ML20086J115 List:
References
AO-74-39, NUDOCS 8401230187
Download: ML20086J111 (2)


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PHILADELPHIA ELECTRIC COMPANY hA

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December 31, 1974 6:s/

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'O Hr. A. Giambusso Deputy Director of Reactor Projects United States Atomic Energy Commission Directorate of Licensing Washington, D.C.

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Dear Mr. Giambusso:

Subject:

Abnormal Occurrence The following occurrence was reported to Mr. Walt Baunack, A.E.C. Region 1 Regulatory Operations Of fice on December 21, 1974.

L Written notification was made to Mr. James P. O'Reilly, Region 1 Regulatory Operations Office on December 23, 1974 In accordance with Section 6.7.2.A of the Technical Speci fications, Appendix A of DPR-56 for Uni t 3 Peach Bottom Atomic Power Station, the following report is being submi tted to the Di rectorate of Licensing as an Abnormal Occurrence.

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Reference:

License Number DPR-56 Technical Specification

Reference:

3.7.0 c

Report No.:

50-278-74-39 Report Date:

December 31, 1974 Occurrence Date: December 21, 1974 Faci li ty:

Peach Bottom Atomic Power Station R.D. #1, Delta, Pennsylvania 17314 Identification of Occurrence:

Drywell equipment drain sump isolation valve A0-3-20-74

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failed to close on a PCIS isolation.

Conditions Prior to Occurrence:

Unit 3 operating at 3182 MWT, 96.6% power.

Startup Test 27, Turbine Trip had just been performed causing reactor scram and group 2 and 3 PCIS isolation.

Description of Occurrence:

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During the PCIS isolation, A0-3-20-94 failed to isolate.

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The valve also failed to isolate on a manual closure signal.

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Mr. A. Giambusso December 31, 1974 Page 2 Designation of Apparent Cause of Occurrence:

The solenoid valve which de-energizes to bleed the air off the diaphram stuck in the energized position preventing valve closure.

Analysis of Occurrence:

The other isolation valve in this line, A0-3-20-95, did close to isolate the line. Therefore, there is minimal safety im-pli ca tion.

Corrective Action:

The solenoid valve was rebuilt and satisfactory operation was veri fied wi thin 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> of the occurrence.

Failure Data:

Similar occurrences were reported as Abnormal Occurrence Report Numbers A0-50-277-74-7 and A0-50-278-74-26.

Very truly yours, h-f>LC M. J. Cooney Asst. Gent. Supt.

Genera tion Division cc: Mr. James P. O'Reilly Director, Region 1 l-United States Atomic Energy Commission -

631 Park Avenue King of Prussia, PA

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