ML20086H609

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Telecopy AO 75-51:on 750819,core Spray 3A Full Flow Test Valve MO-3-14-26A Failed to Close.Cause Under Investigation. Corrective Action Will Be Determined Subsequent to Investigation
ML20086H609
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 08/20/1975
From: Ullrich W
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20086H608 List:
References
AO-75-51, NUDOCS 8401180159
Download: ML20086H609 (1)


Text

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Leits,.PesccylvsLia' 1731L August 20, 19~5

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O'Fiilly. Oirecter

, United 2

  • c *. e s A::=i: Ener y C.: circicn e

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Direetc.nte of F.cculatcry Operations, k**.$M h.f:/c4:q j 631 Park A. c r. a e i

Ki ng o f -Pru s al e. Pennsylvania 19 kC 6.

S u t.j e ct :

Abnerrsl Occurren e 2k-Hou r :!cti fi e n-t en

'a'.' 2. J11 rich's phene c:nversation with Mr. Va t 3sunach, l

Con firsing Region 1. United States Lucicar F.egulatory Co=cission on August 2Q, 1975

Reference:

License su=ter DPR-56 Technical Specificatica

Reference:

h.5.A 1.c Report No.:

50-278-75-51 Report Oate:

August 23, 1975 Occurrence Date:

August 19, 1975 Facility:

Peach Botton Atocic Power Station R.D.

1, Delta, Pennsylvania 1731k Identification of Occurrence:

3A Core Spray prull Flav Test valve - MO-3-1L-26A failed to clos.

Conditions Prior tg occurrence:

Reactor power - 55.2%.

Description of Occurrence:

During the performance of surveillance testing, subsequent to valve

' maintenance. MO-3-1k-26A failed to close from the vide open position during operation of both core spray "A" loop pumps at rated flow.

During single and zero pump operation the valve closed satisfactorily.

Designation of Apparent Cause of Occurrence:

Under investigation.

Analysis of Occurrence:

Because the valve is only opened for a short period of time once a month during surveillance testing, the redundant systes was opereble, and because the operator conducting the test would have bees able, l

to stop the pu=ps, close the valves, and restart the pu=ps, there is mini =al safety significance.

Corrective Action:

Will be deter =ined subsequent to investigation.

Failure Onta:

Sone.

Very truly yours.

k..M SO U W

....,en,

..per.,ntenden:

e.

Pea:n 3cttc= Atc=1: Pcver Static' jvs 8401100159 750829 PDR ADOCK 05000278 S

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