ML20085M516

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AO BFAO-7344W:on 731130,during Startup Testing,Main Steam Line High Flow Pressure Switch PdIS-1-25D Malfunctioned. Caused by Faulty Indication.Pressure Switch Replaced
ML20085M516
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 12/07/1973
From: Eric Thomas
TENNESSEE VALLEY AUTHORITY
To: Oleary J
US ATOMIC ENERGY COMMISSION (AEC)
Shared Package
ML20085M518 List:
References
AO-BFAO-7344W, NUDOCS 8311080616
Download: ML20085M516 (2)


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Mr. John F. O' leary, Director

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Directorate of Licensing Office of Regulation y"IN U.S. Atouic Energy Co:niscion Washington, DC 20545

Dear Mr. O' Leary:

TSNIESSEE VALIEY AUTHORITY - EROWNS FERRY NUCLEAR PLANT UHIT 1 -

DOCKET NO. 50-259 - FACILITY OPERATING LICENSE DPR AENOMAL OCCURRENCE REPORT LFAO-734Mi The enclosed report is to provide details concerning n main steamline high-flow pressure switch malfunction Q ich occurred on Browns Ferry Nuclear Plant unit 1 on November 30, 1973, and is submitted in-accordance with Appendix A to Regulatory Guide 1.16, Revision 1, t

l October 1973 Very truly yours, 1

TEUNESSEE VAIlff' AUTHORITY:

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l E. F.-Thomac Director of Power Production Enclosure ~

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Mr. Norman C. Moseley, Director-

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ABNORMAL OCCURRENCE REPORT

. Report No.--BFAO-73% W Report Date--December 7,1973 Occurrence Date--Hovember 30, 1973 Facility--Browns Ferry Nuclear Plant unit 1 Identification of Occurrence Unit 1 main steamline high-flow pressure switch malfunction.

Conditions Prior to Occurrence j

Reactor was at 25-percent thermal power during startup testing.

ll Description of Occurrence During routine daily instrument checks, main steamline high-flow pressure I

switch PdIS-1-25D was found not indicating correctly.

Analysis of Occurrence One switch from each of the four steamlines is connected in a series to establish one trip logic in a one out of two taken twice trip system in the primary containment isolation control system. The other 15 switches

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were indicating correctly.

Corrective Action A replace =ent differential pressure switch, Earton Model 278, was installed, calibrated, functionally tested, and placed in. service. A bench test of the failed switch indicated that the low-pressure bellows was leakira.

Failure Data Barton Model 278; serial No. 278-2990.

Switch Date~

Failure Corrective Action 1 PdIS-1-25D 11/30/73 Faulty indication-

~ Replaced' pressure switch-e 4

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