ML20084K511

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AO 50-265/74-15:on 740625,standby Liquid Control Sys a Relief Valve Lifted Above Tech Spec Limit.Caused by Setpoint Drift.Investigation to Determine Cause & Corrective Action in Progress
ML20084K511
Person / Time
Site: Quad Cities 
Issue date: 07/05/1974
From: Kalivianakis N
COMMONWEALTH EDISON CO.
To: Oleary J
US ATOMIC ENERGY COMMISSION (AEC)
Shared Package
ML20084K513 List:
References
AO-50-265-74-15, NJK-74-140, NUDOCS 8305190453
Download: ML20084K511 (3)


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Quad Cities Generating Station L

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7, July 5, 1974 v

%,. s OJ 6 e' Mr. John F. O' Leary, Director

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Reference:

Quad Cities Nuclear Power Station, Unit 2 Docket No. 50-265 DPR-30 Appendix A, Sections 1.0.A.4, 4.4.A.2, 6.6.B.l.1.

Dear Mr. O' Leary:

Enclosed please find Abnormal Occurence Report No. A.O. 50-265/

74-15 for Quad Cities Nuclear Power Station.

This was previously reported to Region III, Directorate of Regulatory Operations by tn3cphnr.c on June 25. 197.* and to you and Region III Directow t.:.

of negulatory operations by telegram on oune 26, 1974.

This report is submitted to you in accordance with the requirements of Technical Specifications 6.6.B.l.a.

Very truly yours, COMMONWEALTH EDISON COMPANY QUAD-CITIES NUCLEAR POWER STATION

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Kalivianakis Station Superintendent I

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Region III, Directorate of Regulatory Operations l

J.S. Abel

Enclosure:

Abnormal Occurence Report No. A.O. 50-265/74-15 t

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REPORT NUMBER:

A.O. 50-265/74-15 f

REPORT DATE:

July 5, 1974

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OCCURENCE DATE:

June 25, 1974

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n-FACILITY:

Quad-Cities Nuclear Power Station

.Cordova, Illinois 61242

.f IDENTIFICATION OF OCCURENCE:

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Unit 2 Standby Liquid Control System "A" relief valve setpoint drift.

' CONDITIONS PRIOR TO OCCURENCE:

Unit 2 reactor critical at 530 MWE with normal water level and temperature.

DESCRIPTION OF OCCURENCE:

While performing relief valve setpoint tests for unit 2 standby liquid control system, at 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br /> on June 25, 1974, the "A" relief valve was found to lift at 1520 psig, which exceeds the Technical Specification 4.4.A.Z. limit of 1400( p 4 1490 psig7 The standby liquid control system pressure gage was re-calibrated at 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> and the A relief valve was reset to lift at 1460 psig.

Tac D relief valve was chac' rad and roundite relicyc at 1400 psig.

At 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> on June 26, 1974, the A relief valve was reset to lift at 1440 psig and D was set to lift at 1430 psig to allow for setpoint drift.

1 DESIGNATION OF APPARENT CAUSE OF OCCURENCE:

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r This Abnormal Occurence is attributed to setpoint drift of the "A" relief valve.

., a ANALYSIS OF OCCURENCE:

The impact of the 1520 psig relief valve setpoint drift is minimal on the operation of standby liquid control system.

The increase

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in SDLC relief valve set point was in a safe direction, allowins? '/

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for continued pumping sodium pentaborate solution into the reactor' in the event that the standby liquid control system would have been required.

CORRECTIVE ACTION:

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  1. 1 Action Item Record No. 4-74-57 was issued on June 13, 1974, to investigate the cause of standby liquid control relief valve setpoint drift and determine _ corrective action.

This investigation

'is presently in progress by Quad Cities Station and the Crosby Valve and Gage Company.

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'AILURE DATA:

Standby ligdid control relief valve setpoints hhhe been found to be out of specification limits twice before at Quad Cities Station.

In June of 1973', unit 1 reliefs were found to be set low.

During refueling outage tasts in May of 1974, unit 1 relief valves were found to relieve "higlier than specification limits.

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