ML20083D026

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Intervenor Exhibit I-MOSBA-43,consisting of Info Re Diesel Testing
ML20083D026
Person / Time
Site: Vogtle  Southern Nuclear icon.png
Issue date: 04/21/1995
From:
AFFILIATION NOT ASSIGNED
To:
References
OLA-3-I-MOS-043, OLA-3-I-MOS-43, NUDOCS 9505230314
Download: ML20083D026 (17)


Text

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X-Mw3R 43 oss DIESEL TESTING 00CMETED USHRC

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  • NORMAL 36 MONTH OVERHAUL AND INSPECTION
  • SPECIAL TESTING $bEr$[{jylfi[

SRANCH E 1.B_

3/20 EVENT IN OVERHAUL 5 STARTS, TROUBLESHOOTING SENSOR CALIBRATION LOGIC IESTING E-RUN BUBBLE IESTING MULTIPLE STARTS (14)

UV RUN IEST 6 MONTH RUN SURVE!LLANCE DIESEL OPERABLE UV RUN TEST O se"soa c^'rea^'io" LOGIC IESTING E-RUN BUBBLE IESTING LUBE OIL DCP RUN MULTIPLE STARTS (5) DCP UV RUN FUNCTIONAL UV RUN IEST 6 MONTH SURVEILLANCE DIESEL OPERABLE Hi JACKET WATER RUNS (3)

DCP UV RuN TEST 18 SUCCESSFUL STARTS 19 SUCCESSFUL STARTS NUCLEAR REGULATORY COMMISSION

.f 9 2 4 o ' ^ -1 Docket No To- 42T-cL9 -10t!,cciExh. No. b 4- 'l 3 4 )r u rs (*1 la t$c r13tter et Veg ON

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{X b- k @g7 Intervmcr / REJECTED 7-204y g Contg 0ffr Contractor DATE 5 9 '2 l- 4 C wi: ness W eJc,t k Other Re;xxter 3. 2 :l ta Ic : 9505230314 950421 DR ADOCK0500g4

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WV UNIT 2 Exhibit ,page of _

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o UNIT 2 TRIP

- Unit 2 RAT 8 Trip / Primary Differential Trip

- Turbine Trip / Reactor Trip

- Safety System Response Proper o CAUSE

- Differential Relay CT Set 3000/5 vice 2000/5 o CORRECTIVE ACTIONS

- Test the Remaining Relays on Unit 2

- Update Switchyard Drawings based on audit

- Clartfy existing polfcies for Swftchyard O

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.o UNIT 2 TRIP i

- Unit 2' RAT B Trip / Primary Offrerential Trip

- Turbine Trip / Reactor Trip

- Safety System Response Proper o CAUSE

- Differential Relay CT Set 3000/5 vice 2000/5 o CORRECTIVE ACTIONS

- Test the Remaining Relays on Unit 2

- Update Switchyard Drawings based on audit

- Clarify existing policies for Switchyard O

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DATE: April 6, 1990 RE: Accountability During Emergencies O

V Log: NOV-00426 Exhibit ,page of FROM: G. Bockhold, Jr.

TO: All Emergency Directors and Site Personnel In the event of site emergency conditions, we will implement the following revised procedures. These changes will enhance personnel accountability and safe'ty and ensure better information flow for employees. They will also provide flexibility to the plant when responding to emergency situations.

When the Emergency Director (ED) makes an emergency classification, he will make the appropriate tone and page announcement on the plant PA system. He will direct site personnel to the appropriate locations.

If you can not hear the page, report to your supervisor. He or she will direct you appropriately. Normally non-essential personnel will report to the Admin. Building auditorium or parking lot. David Phillips, the Financial Services Supervisor, has authority to coordinate with the ED and control the disposition of non-essential personnel.

In his absence, the senior person present will contact the Security Captain for additional assistance.

Emergency Response Organization (ERO) personnel should report immediately to the appropriate facility. Other shift personnel, supervisors, and managers on-site should report initially to the f]

(, OSC. Overflow personnel will assemble in the maintenance machine shop area.

When directed by the ED, the security department will initiate accountability. The security department cannot account for personnel who fail to log into the appropriate ERF (e.g., control roce. TSC, or OSC) so it is essential we comply with the ED's instructions as soon as possible.

Your assistance implementing these instructions will ensure we manage emergencies better and provide plant personnel with sufficient information to keep them infomed of abnormal plant activities.

Thank you for your assistance.

GB/ erd xc: Department Heads NORMS

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QUARANTINE COMPONENTS t")

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TEMPERATURE SWITCHES o 1A PROBABLE IRIP CAUSE JACKET WATER TEMPERATURE (2/3 logic) 1 INTERMITTENT 1 POST CALIBRATION Low (186*F & VENTING) o 1A OTHER TEMPERATURE COMPONENTS 1 LUBE Ort TEMPERATURE (SLUGGISH) o IB TEMPERATURE COMPONENTS .

4 JACKET WATER IEMP (VENTING) 2 LUBE OIL TEMP (VENTING & CALIB.)

l PRESSURE SWITCHES o 1A 1 LUBE OIL PRESSURE (TRIPPED) 2 LUBE 0!L PRESSURE (CONSERVATIVELY REPLACED) o 1B 2 LOGIC (WOULD NOT TRIP ENGINE) 92 PlostcT 05S901 Q

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EMERGENCY PLAN IMPLEMENTATl0thibit ,page of m

). DURING THE EMERGENCY,:0FF-SITE NOTIFICATIONS WERE LATE AND/OR DELAYED BEYOND THE 15 MINUTE TIME LIMIT.

O DIRECT CAUSES .

POWER TO THE PRIMARY ENN (IE EMERGENCY POWER) WAS LOST.

ALL EMERGENCY AGENCIES WERE NOT INCLUDED ON THE BACKUP ENN. (BURKE COUNTY AND GEMA ADDED 4/6/90) o CONTRIBUTING CAUSES CONTROL ROOM COMMUNICATORS AND SUPERVISORS WERE NOT FULLY KNOWLEDGEABLE OF THE COMMUNICATIONS SYSTEM CAPABILITIES. (PRIMARY ENN IN TSC HAD POWER FROM THE SECURITY SYSTEM DIESEL.)

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IHE SERIES METHOD OF NOTIFICATION CONTAINED UNSATISFACTORY DELAYS.

EMERGENCY DIRECTOR DID NOT ENSURE PROMPT NOTIFICATION OF OFF-SITE AGENCIES.

AMPLIFYING INFORMATION WAS NOT PROVIDED TO LOCAL GOVERNMENT OFFICIALS.

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003 INITIATING EVENT Exhibit ,page' of I l

D l V

FUELING TRUCK STRUCK INSULATOR SUPPORT INSIDE s

THE LOW VOLTAGE SWITCHYARD CAUSING A FAULT TO THE 1A RESERVE AUXILIARY IRANSFORMER.

o DIRECT CAUSE TRUCK DRIVER AND ESCORT WERE INATTENT!YE' TO SAFE OPERATION OF THE TRUCK.

o CONTRIBUTING CAUSES CONTROL OF VEHICLES NEAR VULNERABLE AND SENSITIVE AREAS NOT ESTABLISHED.

MAINTENANCE EQUIPMENT STAGED INAPPROPRIATELY. l THE USE OF GROUND-GUIDES INSIDE THE PROTECTED AREA WAS NOT CLEAR. l O

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00 1 EMERGENCY PLAN IMPLEMENTATI0gxhibit ,page of COMMUNICATION BETWEEN CORPORATE AND ISC NEEDS.

- TO BE IMPROVED.

O DIRECT CAUSES THE STATUS LOOP TELEPHONE BRIDGE WAS NOT OPERABLE AT THE BEGINNING OF THE ENERGENCY BECAUSE OF THE LOSS OF POWER.

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E -,page l EMERGENCY PLAN IMPLEMENTAT10N xh. bit Of

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DURING THE EMERGENCY, SITE PERSONNEL ACCOUNTABILITY NEEDED IMPROVEMENT. j o DIRECT CAUSE ACCOUNTABILITY PROCEDURES DID NOT PROVIDE FOR'THE SITUATION OF NOT EVACUATING THE SITE. (GENERAL MANAGER'S MEMO OF 4/6/90)

O CONTRIBUTING CAUSES i l

THE INITIAL PAGE ANNOUNCEMENT WAS DELAYED APPROXIMATELY 20 MINUTES.

- PERSONNEL WERE ALLOWED TO RE-ENTER THE PROTECTED AREA.

PAGE ANNOUNCEMENTS ARE DIFFICULT TO HEAR IN SOME PLANT AREAS.

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O ALLOW QUICK IDENTIFICATION OF PERSONNEL.

THE EMERGENCY DIRECTOR FAILED TO PROVIDE GUIDANCE AFTER DECIDING NOT TO EVACUATE PERSONNEL.

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'Lua i DIESEL GENERATOR AVAILABILITpxhibit ,page of n

k). THE 1A DIESEL GENERATOR FAILED TO PROVIDE EMERGENCY ,

POWER TO 1E LOADS UNDER LOSP CONDITIONS.

o DIRECT CAUSE  !

DIESEL TRIP SIGNALS WERE PRESENT DURING UNDER VOLTAGE INITIATED START CONDITIONS. l o CONTRIBUTING CAUSES l

POST MAINTENANCE FUNCTIONAL TESTING FOR l I

AIR LEAKAGE IN THE CONTROL SYSTEM WAS INADEQUATE.

PROCEDURES FOR TIGHTENING FITTINGS IN THE .i AIR LOGIC SYSTEM NEED IMPROVEMENT. l CALIBRATION PROCEDURES OF TEMPERATURE SWITCHES DID NOT GUARANTEE CONSISTENT SETTINGS.

DIESEL GENERATOR TRIPS DURING LOSP WERE NOT CONSISTENT WITH TRIPS DURING A SAFETY INJECTION SITUATION.

DIESEL GENERATOR START LOGIC DID NOT ALLOW MULTIPLE STARTS ON AN UNDERVOLTAGE CONDITION WITH THE DIESEL RUNNING.

OPERATO'RS DID NOT FULLY UNDERSTAND THE DIESEL START LOGIC AND SEQUENCER INTERFACE ON AN LOSP.

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' P89' I MID-LOOP OPERATIONS ACTIONS TO RESPOND TO LOSS OF CORE COOLING AT -

MID-LOOP SHOULD BE IMPROVED.

l o DIRECT CAUSE i THE " LOSS OF RESIDUAL HEAT REMOVAL" PROCEDURE SHOULD PROVIDE IMPROVED GUTDANCE FOR A LOSP CONDITION.

o CONTRIBUTING CAUSES THE " LOSS OF RHR" PROCEDURES ARE TOO NARROWLY FOCUSED FOR MODE 5 & 6 CONDITIONS.

DIRECTIONS FROM THE EMERGENCY DIRECTOR WERE NOT ALWAYS EXPLICIT. ,

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Cct PRESENTATION TO REGION II

-NUCLEAR RE6ULATORY COMMISS10ftxhibit .page Of s,

V ON V0GTLE SITE AREA EERGENCY MARCH 20, 1990 AGENDA 0 OPENING REMARKS C. K. MCC0Y 0 EVENT REVIEW TEAM CRITIQUE G. BOCKHOLD 0 TRUCK / SWITCHYARD 0 0FF-SITE NOTIFICATIONS 0 PERSONNEL ACCOUNTABILITY 0 COMMUNICATIONS CORPORATE / SITE O MID-LOOP OPERATIONS

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O 0 QUARANTINE COMPONENTS G. BOCKHOLD 0 UNIT 2 G. BOCKHOLD l

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UNIT 1 Exhibit-,page OL f^ '

'u DATE TIME COMTS 02/24/90 1425 Started for 24 Hour Run 02/25/90 2206 Secured from 24 Hour Run 2336 Started for ESFAS Testing 2348 Secured for ESFAS 02/27/90 0312 Started for ESFAS

. 0424 Secured for ESFAS 0605 Started for ESFAS 0642 Secured for ESFAS 03/13/90 1518 Start for liaint. Test 03/14/90 0146 Stopped 03/21/90 2149 Failed to start due to insufficient fuel in fuel lines after maintenance.

2156 Failed to Start Again 2202 Started and Governor Vented 2217 Stopped N 2259 Started for Overspeed Trip Test 2301 Stopped Manually due to Low Lube Oil Pressure and High 011 Filter DP 2314 Started 2318 Stopped 03/22/90 0017 Started 0023 Stopped for Maintenance 0428 Started for Testing 0429 Stopped 0714 Locally Started for Maintenance and Engineering Testing 03/22/90 1030 Locally Shutdown 03/22/90 1106 Started from CR 1243 Tripped on D/G High Lube Oil Temp.

03/23/90 0509 Started for Maintenance Run 1202 Stopped 92 Norect 05U909

UNIT 1 DIESEL GENERAwx 18 (CONT'D) ,page of Exhibit DATE TIE COPMENTS 03/23/90 1730 ~

Started for 4 Hour Run 1731 . Tripped on Low Jacket Water Pressure / Turbo Lube Oil Pressure Low 1744 Started for 4 Hour Run 2222 Stopped 03/24/90 0048 Started for Maintenance 0049 "Hi Jacket Water Temp" Alarm in. Temp Verified to be Normal.

0121 Normal Stop 03/27/90 1649 Emergency Start Test 1822 Normal Shutdown 1909 Normal Start 1948 Stopped. Simulated Hi Temp Lube Oil Trip 1951 Started. Simulated LOSP at Engine Panel 1954 Stopped. Simulated Hi Vibration Trip 1957 Nonnal Start 1959 Stopped. Simulated Hi Crankcase Pressure Trip  !

O J V 2004 Started. Simulated SI at Engine Panel Stopped. Simulated to Lube Oil Pressure Trip 4

2010 2220 Started. Simulated Bus UY Signal 2317 Normal Shutdown 03/28/90 0403 Started. Surveillance 14980-1 0537 Normal Shutdown 1350 Start to Perform Functional Test for MWO 1-89-03281 (Lo Lube Oil Pressure Trip Flow Orifices) 1355 Nonnal Shutdown 1 1356 Started. Simulated UV for functional on MWO 1-89-03281 1400 Normal Shutdown I

04/01/90 1623 Normal Start  !

1744 Normal Shutdown 04/04/90 1632 Started for Maintenance 1744 Stopped N E M CT O osasso

' UNIT 1 DIESEL GENE N 1B (CONT'D)-

Exhibit ,page of-O DATE TIE COMENTS 04/05/90 0030 Started. T-ENG-90-17 0035 Stopped 0307 Started. 14980 0509 Stopped O

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~ UNIT 1 DIESEL lllENER TOR 1A Exhibit ,page Of DATE TIE COMENTS 02/26/90 1509 Started. 24 Hour Run for ESFAS 02/28/90 0226 Secured from 24 Hour Run 02/28/90 0945 Started for ESFAS Testing 1210 Secured for ESFAS Testing 02/28/90 1700 Started 3 Times in Series During ESFAS Testing

. 02/29/90 0218 Secured for ESFAS Testing 03/01/90 0128 Started for ESFAS '

03/02/90 0215 Secured for ESFAS

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0912 Started for Maintenance 1944 Secured for Maintenance 03/12/90 1306 Started 2137 Stopped 03/13/90 0009 Started 0506 Stopped 03/20/90 0820 LOSP Occurred - Lost "A" RAT - DG1A Tied and Tripped (Several Alarins came in - not noted in thelog.)

0841 Auto Started after Sequencer Reset and Tripped on Low Jacket Water Pressure 0856 Emergency Break Glass Start locally to Recover from Station Blackout.

1029 RAT "8" Energized 1040 1BA03 Energized from "B" RAT l 1326 Shutdown 2119 Started for Troubleshooting 2206 Shutdown 2223 Started for Troubleshooting 2228 Secured 2233 Started for Troubleshooting 2254 Secured 03/23/90 0254 Started for Maintenance Troubleshooting 0450 Secured 91 P47Ec.T 05U912 v) l t _

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. UNIT 1

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DIESEL M TOR 1A Exhibit ,page _ Of

'DATE TIPE COMENTS 03/23/90 1724 Started and Manually Stopped from CR 03/29/90 1109 Started. UV Test. Tied to 1AA02 1158 Normal Shutdown 03/30/90 1920 Emergency Start 2115 Stopped 2235 Local Start 2241 Trip Hi Temp Lube 011 l 2254 Local 2300 Trip High Vibration 2313 Normal Start 1 2316 Stopped. Hi Crank Case Pressure 2328 SI 2334 Low Lube Oil Pressure 2343 Normal Start 2347 Nonnal Stop

. 2348 Normal Start 2358 Stop 03/31/90 0012 Normal Start 0014 Normal Stop 0016 SI 0019 CR 1827 Start Local 1837 Local Stop 1846 Local Start 1847 Stop 1856 Local Start 1857 Local Stop .

1904 Local Start ,

1906 Local Stop

- 1921 Local Start  :

1922 Local Stop 9A PROJECT O '

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-UNIT 1 DIESEL EDERT0R 1A Exhibit b,page I l of Il O

DATE TIE COMENTS 03/31/90 1955 Local Start 2012 Local Stop 2254 Started. UV Test. Tied to 1AA02-2320 Normal Shutdown 04/01/90 0423 Started. Surveillance 14980-1

. 0556 Normal Shutdown 04/06/90 1345 Start. T-ENG-90-16 1346 Stop 1404 Start. T-ENG-90-16 1405 Stop 1419 Start. T-ENG-90-16 1430 Stop i

2347 Start. T-ENG-90-11 04/07/90 0213 Stop O

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