ML20081M492
| ML20081M492 | |
| Person / Time | |
|---|---|
| Site: | Indian Point |
| Issue date: | 09/30/1983 |
| From: | Blatt M, Otoole J CONSOLIDATED EDISON CO. OF NEW YORK, INC. |
| To: | Mcdonald W NRC OFFICE OF RESOURCE MANAGEMENT (ORM) |
| References | |
| NUDOCS 8311170276 | |
| Download: ML20081M492 (7) | |
Text
.
I.
OPERATING DATA REPORT DOCKET NO.
DATE in-4-n1 COMPLETED DY M.
BLATT_
TELEPHONE 914 ; X -9127 OPERATING STATUS Indian Point Unit 2' Notes -
~
. 2. Reporting Period:
September 1983
- 3. Licensed Thermal Power (MWtI:
279R
- 4. Nameplate Ra.fing (Gross SIWE):
inil
- 5. Design Electrical Ratin;;(Net alWe): A71 005
- 6. Maximum Dependab!c Capacity (Grou MWe):
Ao
- 7. Maximum Dependable Capacity (Net MWc):
.8, if Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
None I
None
- 9. Power Level To Which Restricted.lf Any (Net MWe):
one
- 10. Reasons For Restrictions,if Ai.;:
'Ihis Month Yr.-to Dr.re Ct:mulative 720 6551 81096
-II. Hours in Reporting Period
- 12. Number Of Hour 5 Reactor Was Critical 720
'6091.78
-54249.46
- 33. Reactor Resene Shutdown llours 0
ll R9 161? 16
- 14. Hours Generator On-Line 720 5755.95 52595.25
+
- 15. Unit Resene Shutdown Hours 0
0 0
- 16. Gross Thermal Energy Generated (MWH) 1942432 15268768 136705464 598610 4780360 42283086
- 17. Gross Electrical Energy Generated (MWH)
- 18. Net Electrical Energy Generated (MWH) 575357 4579243 40311300
~IS. ' nit Service Factor 100 87.9
,64.9 U
- 20. Unit Availability Factor 100 87.9 64.9'
-21. Unit Capacity Factor (Using MDC Net) 94.I
_ 81.7 57.8
'.22. Unit Capacity Factor (Using DER Net) 91.5 80.1 56.9 0
5.2 9.4
- 23. Unit Forced Outage Rate
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date.and Duration of Each):
None i
- 25. If Shtt Down At End Of Report Period. Estimated Date of Startup:
- 26. Units in Test Status (Prior to Conn.wrcial Operation):
Forecast Achieved
~
- INITIAL CRITICALITY C
INITIAL ELECTilICITY NA
/
/
t
- COMMERCIAL Ol'ERATION
~
...a 8311170276 830930 gDRADOCK 05000247 pp7)
~
o
~
AVERAGE DAILY UNIT POWER ' LEVEL 50-247 DOCKET NO.
I..P. Unit 2 UNIT 10-5-83 DATE
, COMPLETED BY M. BLATT I
TELEPilONE 91_4 526-5127 MONTH SEPTEMBER 1983 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net)
I 774 763 17 824 723 2
18 824 3
I' 799 4
20 817 775 3
21 807 7 19 812 6
22 744 809 23 785 s
24 814 824 770 9
25 828 10 26 814 820 783 13 27
'825 814 12 28 828 814 13 29 834 803 14 30 15 806 31 16 823 INSTRUCTIONS
-1:$1 g da# unit ptmer lesel fri Mwe. Net Ihr each day in the reporting inienth. Ctirnpute eo e near :
i (9/77I
i,i 14 i.ll I
O e
e Emm,g.
uO1N&a i
c2qm3C 8T2">3
- kmn nmCCQOZm t
c.2 Mz>dm
.
- 1.
asHtI N C,wm O1miww oOg,FM#
z<=
12.*
q
.l 3mh,H gO2d..
- mod, pec:
)
i a.
(
HmFQ oZm MyLp'N I-f o
t r
n n) ogt e
FnSg*
m4 n5 0*Cg$0;?=2 n c l
ios m
di a e e o e p
t u
s ott e t
r d
d p
>es= ;-
s y
r o a
h uR m!-
?.-
Ou s
s o
yo Wo) #
SC mC 7a*,3" xnc.5;s2 T
ul e
t h n D(
R e
o l
S M
w C
oD
- 2OD, w
b e
mx07= c5n: g 5*
m.
C.T.c. =
z "e.e=.
E27=L-e " 1 q E = :,'q -
- m. mL.c.C Eu3cE.
>. c.=5. a n:. ~ E Ea ~ mM Z E r
1.
o Ea c.
s m3 =V m=e2* e~ 'po=nn m.Eu==n=ug, k H3.
WEu3cE p S men 3 x,::
- X m~;::zCM *
>c~5sEE @*5o~
o.xnye. 5"~
rr a
FC.==2 ~ m4~ 3 -
om.
c.xe.sEueQ %3 =E c3 m.Can0 :, i,S3::n > nLn2E ?E5cEn n
i.>cz5 r,.L.En r.
r m;, %7=.. my=* m E*
e O.o~ c. e 5.
4; m's..E3-
- g..
d
. t
- iu-
=.o a3 ^ m 4._* 5.
2
- I
!l
SUMMARY
OF OPERTING' EXPERIENCE Docket No. 50-247 Completed by: M. Bl'att Telephone No.: (914) 526-5127 With the exception of several load reductions averaging 20% reactor power) to repair condenser tube leaks on September 4, 6, 18, 25 and 27 and a brief load reduction to approximately 74% reactor power on September 7 due to trip of No. 22 heater drain tank pump, Unit 2 operated at full power through September 29.
On September 30, reduced performance of the main turbine moisture separator reheaters necessitated isolation of reheat steam to these units resulting in a derating of Unit 2 of approximately 20 MWe.
4 k
e
e Docket No: 50-247 Date: 10/9/83 September, 1983
~
I Mechanical and Electrical Maintenance 1
MWR SYSTEM COMPONENT DESCRIPTION DATE 4702 APW Valve BFD 71 Replaced Valve 6/21/83 5469 ACS 22 Component Overhauled Pump (PM) 6/17/83 cooling Pump 7630 SW 22 SW Pump Replaced Pump 6/17/83 8058 MRS MSl/MS2 Greased Valves 6/22/83 Valves 8734 APW Valve FCV Repaired Valve 6/3/83 406A 8932
- CVCS 21 Charging Replaced Seals 6/16/83 Pump 8984 HVAC 22 CRDM Replaced Fan Motors 6/29/83 Fan Motor 9011 CVCS
- 22 BA Changed Mechanical Seal 6/25/83 Transfer 8567 HT Boric Acid Replaced Controller 6/7/83 Beat Trace and Defective TRIAC Circuit No.
44B 8569 HT BA Heat Trace Replaced Defective 6/7/83 Circuit No.
TRIAC 46B-8566 HT BA Heat Trace Repaired Controller.
6/28/83 Circuit No.
44A
s MWR SYSTEM COMPONENT DESCRIPTION DATE 8571 IIT BA Heat Trace Replaced Alarm 6/7/83 Circuit No.
Unit 46A 8784 PPI Bod Insertion Adjusted Bistable 6/7/83 Timit Alarm YC-431 A/B Alarm Point 8809 UP Mo. 21 Steam Replaced Defective 6/8/83 Generator High Capacitor and Ievel Bistable Bistable Board LC417E 7133 HT BA Heat Trace Repaired Controller 6/1/83 Circuit No. 19 5500 HT BA Heat Trace Replaced TRIAC 6/7/83' Circuit No. 47 8594
'RCS Leakage Spare Reactor Defective Weld on 6/24/83 Detection Cavity Level Sealed Capillary Instrument Tubing Rewelded.
Leg Refilled by Manufacturer.
7554 RPI Rod Insertion On Pulse to Snalog 3/28/83 Alarm Converter, Reset Clutch and Adjusted Potentiometers.
7434 RCS Reactor Cavity Transmitter Rezeroed 3/27/83 Leakage Level LT3302 Detection 8030 RCS Reactor Cavity Transmitter Rezeroed 5/8/83 Leakage Level LT 3302 Detection 8317 CVCS No. 21 Replaced Current 4/4/83 Charging Pump to Pressure Converter
' f;' : *, _
John D.O'Toole -
- ~ '
. ves Prescnt Consoldated Edison Con'pany of New York, Inc.
4 Irving Place. New York, NY 10003 Telephone (212) 460-2533 October 15, 1983 Re:
Indian Point Unit No. 2 Docket No. 50-247 Mr. William G. Mcdonald, Director Office of Management Information and Program Control c/o Distribution Services Branch, DDC, ADM U. S. Nuclear Regulatory Commission Washington, D.
C. 20555
Dear Mr. Mcdonald:
Enclosed you will find.two copies of the Monthly Operating Report related to Indian Point Unit No. 2 for the month of September 1983.
Very truly yours, e
p
- f. 6' / SY Encl.
cc:
Mr. Richard DeYoung, Director (40 copies)
Office of Inspection and Enforcement c/o Distribution Services Branch, DDC, ADM U. S. Nuclear Regulatory Commission Washington, D. L.
20555 Dr. Thomas E. Murley, Regional Administrator Region I U.
S.~ Nuclear Regulatory Commission 631 Park Avenue King of Prussia, Pa..19406 Mr. Thomas Foley, Senior Resident Inspector U.
S.' Nuclear Regulatory Commission P. O. Box 38 Buchanan, New York 10511 4,y