ML20080F747

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Responds to Violations Noted in Insp Repts 50-445/94-23 & 50-446/94-23.Corrective Actions:Radiation Work Permit Covering Spent Filter Carousel Unit Was Revised
ML20080F747
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 01/23/1995
From: Terry C
TEXAS UTILITIES ELECTRIC CO. (TU ELECTRIC)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
TXX-95006, NUDOCS 9501300226
Download: ML20080F747 (10)


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Ref # 10CFR2.201 lilELECTRIC January 23. 1995 C lance Terry Gnupyirshuiden U. S. Nuclear Regulatory Con tiission Attn: Document Control Desk Washington DC' 20555

SUBJECT:

COMANCHE PEAK STEAM ELECTRIC STATION (CPSES)

DOCKET N05, 50 445 AND 50-446 NRC INSPECTION REPORT N05. 50-445/94-23; 50-446/94-23 RESPONSE TO NOTICE OF VIOLATION Gentlemen:

TV Electric has reviewed the NRC's letter dated December 8.1994, concerning the inspections conducted by Mr. A. T. Gody. Jr.. and other inspectors during the period of October 2 through November 12, 1994.

On January 6. 1995 during a telephone conversation with David Graves of your staff TU Electric requested and was granted an extension until January 23, 1995 to respond to the subject violation.

TV Electric hereby responds to the Notice of Violation in the attachment to this letter. The responses provided in the attachment are a summary of actions taken by TU Electric. The details of the root cause analyses, and the t.orrective and preventive actis 1re available at the site for your review. Please do not hesitate to contact me, or contact Obaid Bhatty at (817) 897-E839 to coordinate any additional information you may need to facilitate closure of these issues.

y, Sincer{/

t C. L. Ter >

OB:tg Attachment cc: Mr. L. J. Callan Region IV Mr. D. D. Chamberlain. Region IV Resident Inspectors I

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I 9501300226 950123 DR- ADOCK j 45 r.o. Box 1002 Glen Rose. Tex 76043

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. 1 Attachment to TXX-95006 ,

Page 1 of 9 l

REPLY TO NOTICE OF VIOLATION I

i EESIATEMENT OF VIOLATION A l (445/9423-01: 446/9423 01) '

CPSES Technical Specification 6.11.1 states that procedures for personnel radiation protection shall be prepared consistent with the requirements of 10 CFR Part 20 and shall be approved. maintained, and adhered to for all operations involving persennel radiation exposure.

10 CFR 20.1501(a)(2)(i). (ii), and (iii) states that each licensee shall make or cause to be made surveys that are reasonable under the circumstances to evaluate the extent of radiation levels, concentrations or quantities of  !

radioactive material and the potential radiological hazards that could be present.

Procedure RPI-602. " Radiological Surveillance and Posting." Section 6.1.2.

states that non routine surveys should be performed as required to ensure adequate knowledge of radiological conditions prior to, during, and/or after any evolution involving exposure or potential exposure to radiological hazards.

Radiation Work Permit 94000523. Item 4. states that Radiation Protection technicians proviaing coverage for filter carousal operations shall perform and document necessary surveys in accordance with Procedure RPI-602.

Contrary to the above, on September 26. 1994 radiation protection workers failed to perform and utilize surveys for the filter carousal transfer activities performed in the fuel building. Subsequent surveys indicated contact dose rates of 3.6 R/hr (gamma) and 24 rao/hr (beta).

RESPONSE TO VIOLATION A (445/9423-01: 446/9423-01)

TU Electric accepts the violation. While adequate surveys for the circumstances were taken to assure worker exposure could be appropriately minimized. the intent of the violation is correct in that the survey results were not adequately incorporated into the pre-job plannir g process. The information requested is provided as follows:

1. Reason for the Violation  !

On September 26. 1;94. radioactive contamination present under the filter carousal on top of the transport trailer and on the carousel plug. was inadvertently spread during initial work preparations associated with the transfer of spent filter cartridges into a storage vault.

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Attachment to TXX-95006 Page 2 of 9 TV Electric's investigation indicated the primary cause of the event -

was less than adequate planning. Although, adequate surveys were performed for the situation, the survey results were not adequately incorporated into the pre-job planning process.

2. Corrective Steos Taken and Results Achieved The spread of contamination beyond the established work boundaries was initially detected at approximately 11:30 a.m. on September 26. 1994.

Spread of contamination was detected very quickly by Radiation ,

Protection (RP) technicians and immediate corrective actions '

(e.g.. contamination control and decontamination efforts) were effective at controlling the situation and minimizing the impact on plant areas and personnel. Effected plant areas were decontaminated and returned to normal access by 2:40 p.m. on September 26.1994.

3. Corrective Steos Taken to Avoid Further Violations To preclude future incidents of this nature the following actions have been implemented:

. The radiation work parmit (RWP) covering the spent filter carousel unit was revised to provide more specific details associated with the radiological precautions to be followed when performing this task.

. Additional enhancements were incorporated into procedure changes to Radiation Protection Instruction (RPI)-206. Liquid Process Filter Control, which were effective on December 2. 1994. These enhancements define radiological control measures to be taken during the liquid process filter change out and transfer.

t should be ncted that filters have subsequently been removed from the filter carousel device utilizing the enhanced RWP and procedures with no radiological problems encountered. .

4 Date of Full Comoliance TV Electric is in full compliance t

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Attachment to TXX-95006 Page 3 of 9 RESTATEMENT OF VIOLATION B (445/9423 02: 446/9423 02)

CPSES Technical Specification 6.8.1.a states that written procedures shall be established. implemented, and maintained covering the applicable procedures recommended in Appendix A of Regulatory Guide 1.;3. Revision 2.

dated February 1978.

Regulatory Guide 1.33. Appendix A. Itcm 3. recommends procedures for startup, operation, and shutdown of safety related systems.

1. Procedure 0WI-110. Revision 3. " Operation Department Work Control and Clearance Guideline." Step 6.2.6. specifies. in part, chat the shift manager, on-shift senior reactor operator, or cognizant supervisor shall review the clearance release to ensure the desired component, subsystem, or system restoratio,1 lineup and sequence is correctly specified.

Procedure 50P-609B. Revision 0. " Diesel Generator System." Step 5.4.3 specifies the steps necessary to fill the jacket water cooling system and align it for service. Specifically. Step 5.4.3.5. states. in part. "If the jacket water rocling system requires filling, then open valves for the selected DG [ diesel generator] and allow the standpipe to fill." Step 5.4.3.7 specifies to complete the electrical lineup per Section 2.3 of Attachment 1. rhich states that the diesel generator jacket water immersion heater 2-02 feeder breaker should be "0FF" when the system is drained.

Contrary to the above, on October 27. 1994 a clearance release was approved that war not adequate to ensure the proper diesel generator jacket water cooling system lineup specified in Procedure 50P-609B.

This resulted in the auxiliary operator placing the feeder breaker for the jacket water heater in the "on" position and then placing the jacket water keep warm pump and heater handswitch in the " auto" position. This energized the jacket water heater and the pump with the jacket water cooling system drained and resulted in damage to the jacket water heater.

2. Integrated plant Operating Procedure IP0-003B. Revision 0. " Power Operations." required that power increases between 20 percent and 100 percent be limited to 3 percent per hour.

Contrary to the above. on May 15. 1993. reactor power was increased at a rate of 9.3 percent per hcar.

Attachment to TXX-95006 Page 4 of 9 RESPONSE TO VIOLATION B EXAMPLE 1 (445/9423 02: 446/9423 02)

TU Electric accepts the violation and provides the following information. as requested:

1. Reason for the Violation The cause of the event was deemed to be personnel not recognizing that the Emergency Diesel Generator (EDG) 2-02 jacket water system was drained. Additicnally, the clearar,ce "special instructions" were vague and did not adequately describe the assumptions used to generate the clearance release (i.e..the intent for use of the system operating procedure to refill the jacket water heater pric~ to startup was not evident).
2. Corrective Stens Taken and Results Achieved Immediate actions were taken to place the EDG 2-02 in the maintenance mode using the system operating procedure. The damaged heaters were replaced.
3. Corrective Steos Taken to Avoid Further Violations Energizing of the EDG jacket water immersion heater with the jacket water cooling system drained has occurred previously. Corrective actions associated with the previous occurrence included procedure enhancements for the Shift Manager (a licensed senior reactor operator) to determine the position of the immersion heater breaker depending on scope of the work / clearance. Additionally, a sight glass on the jacket water standpipe was added to aid in determining system status.

TU Electric now believes that additional actions to preclude recurrence are required as follows:

(a) Operator Component / System Status Knowledge.

(i) Clearances, when developed or released. will identify in the " note pad" section the planned or expected system / component condition (i.e.. dreined, filled.

energized. deenergized. etc.).

(ii) Clearance releases developed in work control will be reviewed and approved by an SRO. j i

(iii) A list of work control center and clearance processing center expectations will be generated.

i A' iment, to TXX-95006 Pt  ; of 9 (b) Program / Process Enhancements (1) For the Emergency Diesel Generator system, clearance tags will be removed and the EDG will be restored using the procedural steps of the system operating procedure.

(ii) The clearances that have been prepared for the upcoming Unit I refueling outage (IRF04) will be reviewed with the subject event in mind to preclude future occurrences.

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4. Date of Full Comoliance TU Electric is in full compliance. The clearance reviews will be completed prior to start of 1RF04. ,

Atta;hment to TXX-95006 Page 6 of 9 RESPONSE TO VIOLATION - EXAMPLE 2 (445/9423 02: 446/9423 02)

TU Electric wishes to point out with respect to this example that the ramp rate limitations contained in procedure IPO-003B are recommended by the fuel vendor for warranty concerns, and not for nuclear safety concerns. As such.

TU Electric does not believe that the cited references to Technical Specification 6.8.1.a and Regulatory Guide 1.33 Revision 2 are applicable to the steps in procedure IP0-003B which impose these limitations.

Additionally, on May 15. 1993 reactor power was increased at a rate of 9.3 percent during a one hour period. The details of this event, along with actions taken by TU Electric were discussed at length during a management meeting at CPSES on July 8.1993 and are summarized below.

1. Realpp for the Viola. tion On the evening of May 14, 1993, Unit 2. while in Mode 1, was prepared for power escalation activities at a 3 percent per hour camp rate.

Activities being performed by the on-shift crew were normal. The Unit Supervisor for Unit ? gave brief instructions to the Reactor Operator and Balar.ce of Plant Peactor Operator to commence power escalation.

Subsequent to shift relief on the morning of May 15, 1993, Performance and Test personnel dur;ng their review of testing data (power ascension) indicated that the procedurally prescribed 3 percent ramp rate restrictions had been exceeded.

An independent evaluation team was formed to review this event at the request of the Vice President. Nuclear Operation CPSES. The independent evaluation team ascertained the causes of the event as the following: on-shift supervision was less than adequate at all levels; communication between on-shift crew members was less than adequate:

work practices (i .e. , self-verification and procedure usage) were less than adequate and application of knowledge of integrated plant cperation on the Reactor Operator's part was less than adequate.

Based on on-shift observations by the Independent Safety Engineering Group (ISEG) dur1ng the preceding 5 months, the causes of this event were concluded to be isolated incidents.

Please refer to NRC letter dated July 13, 1993 from Mr. A. Bill Beach to Mr. W. J.

Cahill, Jr., Which describes the meeting summary.

Attachment to TXX-95006 Page 7 Of 9

2. Corrective Steos Taken and Results Achieved _

Appropriate disciplinary actions for the individuals involved were taken.

An evaluation by Reactor Engineering was performed to determine the impact of exceeding vendor recommended power ramp rates. It was concluded that exceeding vendor recommended power ramp rates has the potential for initiating leaks in the fuel cladding (one of the three primary fissicn product boundaries). The evaluation also. concluded that it is unlikely that any fuel leaks will occur in CPSES Unit 2 as a result of the power ramps experienced on May 15. 1993. The power ramp (s) for this event, although outside of vendor recommendations and administrative guidance were within the power ramps for which the plant was designed to operate.

3. Corrective Steos Taken to Avoid Further Violation Additional actions taken were to; require a power change briefing prior to power changes: utilization of a power change checklist, which defines important parameters to be verified; and reemphasis of management expectation with respect to supervisory oversight and communication.

TV Electric believes the corrective steps taken above will avoid further occurrences. Additionally, no matters of concern with the fuel have been identified through Cycle 1 of Unit 2.

4. Date of Full Comoliance TV Electric is in full compliance.

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Atta,chment to TXX-95006 Page 8 of 9 RESTATEMENT OF VIOLATION C (445/9423 03: 4A6/9423-03)

Criterion III of Appendix B to 10 CFR Part 50 requires. in part. that measures be established to assure that applicabi regulatory requirements and the design basis, as defined in Section 50.2 and as specified in the licanse application, for those structures, systems, and components to which this appendix applies are correctly translated into specifications, drawings, procedures and instructions. Furthermore. the design control measures shall provide for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program.

Final Safety Analysis Report (FSAR) Section 6.2.2. " Containment Heat Removal Systems," states. in part. that the design of the containment sump trash racks are to preclude clogging of the recirculation lines and any of the system's cc:penents. The FSAR further states that the trash rack has a fine screen opening of 0.115-inch which is designed to ensure that the 3/8-inch diameter containment spray nozzle orifices and the grid assemblies in the reactor core will not clog.

Contrary to the above. licensee design control measures did not adequately verify that Unit 1 and 2 containment sump trash racks met design requirements specified in the FSAR prior to operation of both units as evidenced by the discovery of numerous gaps and holes with dimensions that exceeded the FSAR specification ci 0.115-inch on November 2.1994.

RESPONSE TO VIOLATION C (445/9423 03: 446/9423-03)

TU Electric accepts trie violation and provides the following information as requested:

1. Reason for the Violation In response to an industry experience report, engineering personnel parformed a walkdown of CPSES Unit 2 (which was in its first refueling outage) Containment Sump. The sump screens themselves were configured per design; however several structural gaps were found in the framework and base which supports the screens. These gaps were larger than the 0.115-inch screen mesh size addressed in the FSAR. The largest gap was approximately 0.375-inch by 1.25-inch.

i Attachme'nt. to TXX-95006 Page 9 of 9 A review of the design. installation, and inspection documents was performed. It was determined that adequate emphasis was pro'lded to assure proper sump screen size; however, guidance for construction and inspection of the sump support structure did not assure that structural gaps would not exceed the 0.115 inch design requirement.

2. Corrective Steos Taken and Results Achieved An evaluation was performed by Westinghouse for the gap sizes. It was concluded that the gaps would not prevent the Unit 1 & 2 residual heat removal systems, high head safety injection or containment spray systems from performing their safety functions. Since Unit 2 was in its refueling outage, the sumps were repaired to restore the original design conservatism. The Unit 1 containment sump structures were also inspected. and similar conditions were noted.
3. Corrective Steos Taken to Avoid Further Violations Unit 2 sump structures have been repaired, and Unit 1 sump structures '

will be repaired during its up coming refueling outage. Therefore, no further actions are warranted.

4. Date of Full Comoliance CPSES Unit 2 is in full compliance. CPSES Unit 1 gaps will be repaired during its upcoming refueling outage.

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