ML20079L297
| ML20079L297 | |
| Person / Time | |
|---|---|
| Site: | FitzPatrick |
| Issue date: | 02/03/1983 |
| From: | Mcneil C, Corbin McNeil POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK |
| To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| References | |
| RO-83-008, RO-83-029, RO-83-29, RO-83-8, NUDOCS 8302230224 | |
| Download: ML20079L297 (1) | |
Text
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bih)(k O ha NAEIJ TELECOPY MESSAGE Certified By hg/
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TO:
Prus1 dent and Chief Operating Officer T0:
Director of Regulatory Operation Chairman SRC USNRC Region 1 Senior Vice-President. Nuclear Generation 631 Park Avenue King of Prussia, Pennsylvania 19406 Date/ Time: Jd/f3 AS : s'3 m.
Date/ Time: M6I4
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FROM:
Power Authority of the State of New York James A. fitzPatrick Nuclear Power Plant P. O. Box 41 Lycoming. New York 13093 EBJECT:
PROMPT REPORTABLE OCCURRENCE DOCKET NO.
50-333 LICENSE NO.
OPR-59 ASSIGNED OR NO.83-029 LER NO.
_83-008 EVENT DATE:
2/2/83 REPORT DATE:
2/3/83 EVENT DESCRIPTION: The licensee was informed by telephone con-versation that an error had been made in the ODYN base deck for Reload 4 Cycle 5 analysis.
This error led to ACPR values for pressurization transients non-conservative with respect to the Supplemental Reload Licensing submittal (Y1003J01A25) values.
The limiting value of CPR used throughout the cycle has been correct since a non-pressurization event has been the mosc limiting.
COMPONENTS INVOLVED: N/A CAUSE and REMEDIAL ACTION:
A personnel error in performing the licensing analysis for Reload 4.
The remedial action:
Technical Specification change i
r FNIgogagg the recalculated ACPR geA POWER 100 Routine Startup Shutdown Routine Shutdown Refueling Steady State Pcver x
Other Load Change Not Applicaole A written follcw-up raport will be submitted within t*,vo weeks.
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' CORBIN A. McNEILL. JR.
8302230224 830203 PDR ADOCK 05000333 RESIDENT MANAGER S
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