ML20076F410

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Monthly Operating Repts for May 1983
ML20076F410
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 06/01/1983
From: Schroeder B, Scott D
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
References
83-542, NUDOCS 8306140086
Download: ML20076F410 (18)


Text

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r OPERATING DATA REPORT DOCKET NO. 050-237 DATE June 1, 1983 I

COMPLETED BY B. A. Schrceder l TELEPHONE (815) 942-2920 OPERATING STATUS NOTES 1.

Unit Name:

Dresden II 2.

Reporting Period:

May, 1983 3

Licensed Thermal Power (MWt):

2,527

.4.

Nameplate Rating (Gross MWe):

828 5

Design Electrical Rating (Net MWe): 794 6.

Maximum Dependable Capacity (Gross MWe):

812 7.

Maximum Dependable Capacity (Net MWe):

772 8.

If Changes Occur in Capacity Ratings (Items 3 Through 7) Since Last Report, Give Reasons:

N/A 9

Power Level to Which Restricted, if Any (Net MWe):

N/A 10.

Reasons For Restrictions, If Any: n/A This Month Yr-to-Date Cumulative.

11.

Hours in Reporting Period 744 3623 114,383 12.

Number of Hours Reactor Was Critical 714.17 1009.95 87,868.80 13 Reactor Reserve Shutdown Hours 0

0 0

14.

Hours Generator On-Line 699.52 974.48 83,794.55 15 Unit Reserve Shutdown Hours 0

0 0

16.

Gross Thermal Energy Generated (MWH) 1,549,660 1.881.404 167,362,913 17 Gross Elect.-ical Energy Generated (MWH) 501.274 600,979 53,489,245 18.

Net Electrical Energy Generated. (MWH) 478.006 558,177 50,555,367 19 Unit Service Factor 94.02 26.90 73.26 20.

Unit Availability Factor 94.02 26.90 73.26 21.

Unit Capacity Factor (Using MDC Net) 83.22 19.96 57.25 22.

Unit Capacity Factor (Using DER Net) 80.92 19.40 55.67 23 Unit Forced Outage Rate 6.02 4.37 11.59 24.

Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

N/A 25 If Shut Down At End Of Report Period, Estimated Date of Startup:

N/A l

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8306140086 830601 PDR ADOCK 05000237 R

PDR

i OPERATING DATA REPORT DOCKET NO.

050-249 DATE June 1, 1983 COMPLETED BY B. A. Schroeder rgq 947 79h TELEPHONE OPERATING STATUS NOTES 1.

Unit Name:

Dresden III 2.

Reporting Period:

May, 1983 3

Licensed Thermal Power (MWt):

2,527 4.

Nameplate Rating (Gross MWe):

828 5.

Design Electrical Rating (Net MWe): 794 6.

Maximum Dependable Capacity (Gross MWe): 812 7.

Maximum Dependable Capacity (Net MWe):

773 8.

If Changes Occur in Capacity Ratings (items 3 Through 7) Since Last Report, Give Reasons:

N/A 9

Power Level to Which Festricted, If Any (Net MWe): N/A 10.

Reasons For Restricticens, if Any:

N/A This Month Yr-to-Date Cumulbtive.

11.

Hours in Reporting Period 744 3623 103,968 12.

Number of Hours Reactor Was Critical 744 2827.77 78,555.47 13 Reactor Reserve Shutdown Hours 0

0 0

14.

Hours Generator On-Line 744 3557.75 77,015.72 15.

Unit Reserve Shutdown Hours 0

0 0

16.

Gross Thermal Energy Generated (MWM) 1.770.999 8,373,135 154,634,865 17 Gross Electrical Energy Generated (MWH) 565,786 2.723.350 51.37s.414 l

18.

Net Electrical Energy Generated.(MWH) 539,434 2.599.253 47.681.898 19 Unit Service Factor 100.0 98.20 74.08

, 20.

Unit Availability Factor 100.0 98.20 74.08 21.

Unit Capacity Factor (Using MDC Net) 93.80 92.81 59.33 22.

Unit Capacity Factor (Using DER Net) 91.32 90.36 57.76 23 Unit Forced Outage Rate 0.0 1.8 12.99 24.

Shutdowns. Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

Rn fueli ne outnen enmmencine the latter Dart of October 1983.

l 25.

If Shut Down At End Of Report Period, Estimated Date of Startup:

N/A l

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DOCKET NO. 050-237 UNIT NAME Drerfden II UNIT SHUTDOWNS AND POWER REDUCTIONS DATE June 1, 1983' COMPLETED BY B. A. Schroeder TELEPHONE M ) 942-2920 k

REPORT MONTH May, 1983 METHOD OF LICENSEE CAUSE & CORRICTIVE NO.

DATE TYPEl DURATION REASON 2 SHUTTING EVENT SYSTEM COMPONENT ACTION TO I

(HOURS)

DOWN REACTOR 3 REPORT f CODE 4 CODES PREVENT RECUl:RENCE l01 Bonnet gasket on "B" feedwater 2

83-5-3 F

44.5 A

1 check valve leaking. Repaired.

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1 2

3 4

Method:

Exhibit G-Instructions for p

F:

Forced Reason:

S:

Scheduled

.A-Equipment Failure (Explain) 1-Manual Preparation of Data B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (

) File D-Regulatory Restriction 4-Other (Explain)

(NUREG-0161)

E-Operator Training & License Examination.

F-Administrative i

G-Operational Error i

j:

H-Other (Explain) j i

een e.

DOCKET NO. m _2Ao r

UNIT NAME Dresden III UNIT SHUTDOWNS AND POWER REDUCTIONS DATE June 1.

1983 COMPLETED BY B. A. Schroeder-TELEPHONE (815) 942-2920 i

REPORT MONTH MAY, 1983 METHOD OF LICENSEE CAUSE & CORPJ:CTIVE No.

DATE TYPEl DURATION REASON 2 SHUTTING EVENT SYSTEM COMPONENT ACTION To (HOURS)

DOWN REACTOR 3 REPORT #

CODE 4 CODES PREVENT RECURRENCE i

None o

I!

1 r

p

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I.

1 2

3 4

F:

Forced Reason:

Method:

Exhibit G-Instructions for S:

Scheduled

.A-Equipment Failure (Explain) 1-Manuci Preparation of Data B-Maintenance or Test 2-Manual Scram Entry Sheets'for Licensee l

C-Refueling

.3--Automatic Scram Event Report (

) File D-Regulatory Restriction 4-Other (Explain)

(NUREG-0161)

E-Operator Training & License Examination.,

F-Administrative

)

G-Operational Error i

l H-Other (Explain) i g

)

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AVERAGE DAILY UNIT POWER LEVEd DOCKET NO. 050-237

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UNIT II DATE June 1, 1983 i

COMPLETED BY B. A. Schroeder TELEPHONE (815) 942-2920 I

MONTH MAY, 1983 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Net) 1 568 17 782 2

571 18 761 3

35 19 786 4

0 20 737 5

350 21 772

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6 274 22 779 779 7

507 23

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8 658 24 781 9

697 25 781 10 680 26 782 11 721 27 776 12 774 28 635 13 748 29 699 742 30 679 14 15 729 31 707 16 774 1

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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 050-249 UNIT III DATE June 1, 1983 COMPLETED BY B. A. Schroeder a

~ TELEPHONE (815) 942-2920 J.

I I

MONTH MAY, 1983 I

DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Net)

)

l 1

746 17 746 2

777 18 742 3

775 19 742 4

780 20 734

~

5 775 21 370

~~ ~

479 6

775 22 769 623 7

23 752 8

24 749 l

9 783 25 761 10 769 26 751

])

767 27 747 12 28 745 762 737 719 13 29 712 14 30 748 15 31 740 16 l

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DRESDEN UNIT 2 SAFETY RELATED MAINTENANCE - MAY, 1983 NATURE OF LER OR OUTAGE MALFUNCTION EQUIPMENT MAINTENANCE NUMBER CAUSE RESULT CORRECTIVE ACTION U-2 Ea:t Torus Preventive W.R. #26681 N/A N/A Opened East Torus'mainway door per Mainwr.y request.

2-2301-4 M0 Preventive W.R. #25238 N/A N/A Lubed valve stem and tightened packing.

Valve Bus 24 to Bus Preventive W.R. #26579 N/A N/A Tested out ok.

24-1 Circuit Breaker on Bu; 24-1 Pip 3 Clamps -

Preventive W.R. #26867 N/A N/A Trimmed snubber brackets.

Main Steamline Snubber 2-1501-26A Preventive W.R. #25573 N/A N/A Took-up on packing and lubed stem.

Safety Valve Preventive W.R. #26735 N/A N/A Tightened flange bolts.

Main Steam IB Inboard MSIV Preventive W.R. #26549 N/A N/A Removed MSIV pilot block and replaced "0"

ring.

Vacuum Breaker Preventive W.R. #26784 N/A N/A Adjusted disc for proper seating Michanical Preventive W.R. #27114 N/A N/A Performed functional test on snubbers Snubber Nos. 4 7, 48, 30 and 31.

1501-3B Preventive W.R. #25513 N/A N/A Removed and replaced the conduit.

2-1501-26B Preventive W.R. #25544 N/A N/A Adjusted packing and lube stem.

M02-2301-9 Preventive W.R. #24692 N/A N/A Adjusted packing.

Torus to Rx Preventive W.R. #26042 N/A N/A Replaced air hose.

Bldg. Vacuom Break r

DRESDEN UNIT 2 SAFETY RELATED MAINTENANCE - MAY. 1983 MALFUNCTION NATURE OF LER OR OUTAGE EQUIPMENT MAINTENANCE NUMBER CAUSE RESULT CORRECTIVE ACTION D.W. Torus Preventive W.R. #20168 N/A N/A Greased both inboard and outboard shaft Vicuum Breaker housing.

U-2 MSIV Preventive W.R. #21950 N/A N/A Removed packing. Removed lantern ring and repacked valve. Lubricated guides l

and stem.

1-B MSIV Preventive W.R. #22062 N/A N/A Replaced pilot "s1ve.

I U-2 Target Rock Preventive W.R. #22019 N/A N/A Removed, tested and reinstalled Target Solenoid Rock.

l U-2 D.W. Equip-Preventive W.R. #21656 N/A N/A Inspected doors and gaskets, ment U-2 Drywell Preventive W.R. #21952 N/A N/A Reinstalled drywell cover.

j Cover l

'25 V.

U-2 TB Preventive W.R. #26758 N/A N/A Cleaned 125 volts V.D.C. ground.

R ccrve Bus-CK+6 D.W. Torus Preventive W.R. #20170 N/A N/A Repaired Torus vacuum breaker seals.

Vacuum Breaker

)HPCI Room Preventive W.R. #25302 N/A N/A Replaced packing HPCI valve 3933-502.

Cooler Inlet Valve 2

N to D.W.

Preventive W.R. 26725 N/A N/A Repaired air hose to N2 to 2-4720 valve.

2-4720 Torus to Dry-Preventive W.R. 24823 N/A N/A Removed and reinstalled vacuum breaker wall Vacuum (2-1601-33A) top cover and disc.

Breakers ID MSIV Preventive W.R. i/27217 N/A N/A Removed, tested and replaced ID MSIV pilot assembly.

DRESDEN UNIT 2 s

SAFETY RELATED MAINTENANCE - MAY, 1983 NATURE OF LER OR OUTAGE MALFUNCTION EQUIPMENT MAINTENANCE NUMBER CAUSE RESULT CORRECTIVE ACTION MOV 202-6B Preventive W.R. #25800 N/A N/A Reset breaker setting.

6 ShuYg}cwn Preventive W.R. #21865 N/A

.N/A Installed motor (2-1001-5A).

Cooling Dis-charge Valve D.W. Vent Preventive W.R. #26471 N/A N/A Removed and installed valve ( 1601-24).

Icoletion Valve D.W. Torus Vent Preventive W.R. #25993 N/A N/A Installed valve, end Purge Valve 2-1601-60 4

2B SBLC PP Preventive W.R. #26806 N/A N/A Tightened bolts.

2-1501-38A Preventive W.R. #25250 N/A N/A Reinstalled pushbutton sration.

Locr_1 P.B. Sta.

U-2 Torus D.W.

Preventive W.R. #26708 N/A N/A Replaced switch. (2-1601-33B).

Vacuum Breakers D-2-B SBLC R.V.

Preventive W.R. #21846 N/A N/A Removed, repaired and remounted valve.

Inatr. Check Preventive W.R. #26747 N/A N/A Removed, repaired and tested flow check.

Valve 2-263-31M HPCI Cooling Preventive W.R. #26756 N/A N/A Repaired and repacked valve.

Water Valve MO 2-2301-48 S.D. Cooling A Preventive W.R. #23920 N/A N/A Replaced motor (2-1001-1A).

Loop Suction Icol. Valve 2 "B" Shutdown Preventive W.R. #26462 N/A N/A Reversed auxiliary contacts in breaker.

Cooling P.P.

Discharge Valve 2-1001-4B

j DRESDEN UNIT 2

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SAFETY RELATED MAINTENANCE - MAY, 1983 l

l MALFUNCTION l

NATURE OF LER OR OUTAGE EQUIPMENT MAINTENANCE NUMBER CAUSE RESULT CORRECTIVE ACTION Accum. Rod Preventive W.R. #26154 N/A N/A Jumper removed and cleared from jumper log.

Block l

SRM and IRM Preventive W.R. #25507 N/A N/A Removed and installed SRM's and IRM.

Mr.in Steamline Preventive W.R. #21889 N/A N/A Installed and removed steamline plugs.

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Plugs U-2 MOV 1402-4A Preventive W.R. #25127 N/A N/A Repaired set limit switch.

2 MOV 1402-38A Preventive W.R. #25126 N/A N/A Reconnected wiring.

j D2 Electromatic Preventive W.R. #25952 N/A N/A Removed and replaced actuator arms (2-203,B,C,D&E).

2-2305-500 Preventive W.R. #24690 N/A N/A Installed new valve and pipe cap.

U-2 Torus /Rx Preventive W.R. #24659 N/A N/A Performed lift force test.

Bldg. Vacuum Braaksrs l

Torus to Dry-Preventive W.R. #24822 N/A N/A Opened vacuum breakers, wall Vacuum i

Breakers Torus to Dry-Preventive W.R. #24821 N/A N/A Opened vacuum breakers.

well Vacuum Breakars ECCS System Preventive W.R.

N/A N/A Installed packing, follower and nuts.

Jockey Pump 2-1501-25B Preventive W.R. #26971 N/A N/A Removed solenoid and bench tested.

  1. 2 Diesel Preventive W.R. #26619 N/A N/A Completed quarterly inspection.

Gen:rator 1

DRESDEN UNIT 2

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SAFETY RELATED MAINTENANCE - MAY,'1983 NATURE OF LER OR OUTAGE MALFUNCTION EQUIPMENT MAINTENANCE NUMBCR CAUSE RESULT CORRECTIVE ACTION LPRM 48-33A Preventive W.R. #18242 N/A N/A Investigated computer printout section Group 1 and repaired as requested.

250V Battery Preventive W.R. #25879 N/A N/A Charge cell.

N2B Recire.

Preventive W.R. #25655 N/A N/A Ground-out indication.

Inist N2H Recire.

Preventive W.R. #25777 N/A N/A Ground-out indication.

Ricer Elbow Weld LPCI Line Preventive W.R. #26132 i

N/A N/A Adjusted U-bolt.

U-Bolt Safety Valve Preventive W.R. #26734

.N/A N/A Tightened flange bolts.(SV-2-203-4B),

Main Steam CRD Sys.

Preventive W.R. #26325 N/A N/A Repaired leaking valve _(2-203-13A).

Stabilizing Valve CRD F-4 (22-15)

Preventive W.R. #26414 N/A N/A Lenghtened stroke on scram inlet valve.

Also tightened coupling on scram outlet valve.

2A LPCI Heat Preventive W.R. #25611 N/A N/A '

Tightened union, removed valves and Exchanger cleaned seats. Reinstalled valves.

2-202-7A Valve Preventive W.R. #26689 N/A N/A Opened valve and installed handwheel assembly.

D-2 SBLC A R.V.

Preventive W.R. #21845 N/A N/A Disassembled and lapped seats.

Reassembled and tested.

SRM/IRM Preventive W.R. #26116 N/A N/A Removed jumpers and installed shorting links.

DRESDEN UNIT 2 SAFETY RELATED MAINTENANCE - MAY, 1983 NATURE OF LER OR OUTAGE MALFUNCTION EQUIPMENT MAINTENANCE NUMBER CAUSE RESULT CORRECTIVE ACTION CRD 06-19 (BS)

Preventive W.R. #26411 N/A N/A Adjusted scram inlet valve 1/2 turn.

Shutdown Preventive W.R. #26840 N/A N/A Adjusted packing and lubed valve ste.n Cooling Dis-(2-1001-5B).

chstge Isola-tion Vcive Shutdown Preventive W.R. #26839 N/A N/A Adjusted packing and lubed valve stem Cooling Dis-(2-1001-4A).

chtrg: Isola-tion Valve LPCI Icolatio'n Preventive W.R. #26838 N/A N/A Adjusted packing and lubed valve stem Valve (2-1501-22A).

2B LPCI Heat

. Preventive W.R.

15723 N/A N/A Reset valve to 375.

Exchtnger Class 1 Weld Preventive W.R. 25291 N/A N/A Ground and prepped all welds.

Grinding HPCI Line Preventive W.R. #26757 N/A N/A Connected line as requested.

2318-2 Lx Equipment Hatch Preventive W.R. #26683 N/A N/A Opened D.W. equipment hatch.

2-2301-8 Preventive W.R. #23572 N/A N/A Repaired valve.

Equipment Hatch Preventive W.R. #26682 N/A N/A Closed equipment hatch.

1501-28A Preventive W.R. #26061 N/A N/A Removed spool piece and reinstalled, and 1501-27A AO's 220-44, Preventive W.R. #21148 N/A N/A Removed and replaced ASCO valve.

220-46 and 220-47

DRESDEN UNIT 2 SAFETY RELATED MAINTENANCE - MAY, 1983 NATURE OF LER OR OUTAGE MALFUNCTION EQUlPMENT MAINTENANCE NUMBER CAUSE RESULT CORRECTIVE ACTION RPS Relays Preventive W.R. 626488 N/A N/A Repaired RPS relays for the ECCS under-590-ll2A,B,C,D voltage test.

2 "B" Shutdown Preventive W.R. #26462 N/A N/A Reversed auxiliary contacts in breaker.

Cooling P.P.

Di: charge Valve 2-1001-4B RPS Rnlays Preventive W.R. #26488 N/A N/A Repaired RPS relays for the ECCS under-590-ll2A,B,C,D voltage test.

Core Spray Valve Preventive W.R. #26930 N/A N/A Investigate and repair core spray valve MO 2-1402-25B '

motor operator.

A0 1601-61 2" Preventive W.R. #25276 N/A N/A Removed, dismantled and repaired valve.

2 N

Purge Bypass MO 2-1501-3A Preventive W.R. #24166 N/A N/A Replaced valve operator with an environ'-

mentally qualified operator.

D.W. Torus Preventive W.R. #20171 N/A N/A Repaired leak.

Vacuum Breaker 1601-32D e

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DRESDEN UNIT 3 SAFETY RELATED MAINTENANCE - MAY, 1983 NATURE OF LER OR OUTAGE MALFUNCTION EQUIPMENT MAINTENANCE NUMBER CAUSE RESULT CORRECTIVE ACTION CRD #26-23 (G-6)

Preventive W.R. #27078 N/A N/A Adjusted scram outlet valve.

M3in Stcamline Preventive W.R. #26631 N/A N/A Replaced movement and recalibrated High Flow Switch (261-2L).

APRM CH #4 Preventive W.R.

11749 N/A N/A Replaced plug on 5 volt power supply.

U-3 "B" Standby Preventive W.R. #26863 N/A N/A Adjusted packing.

Liquid Control Pump LPRM 24-09-D Preventive W.R. #26250 N/A N/A Investigated and repaired as necessary.

APRM CH #2 LPRM 40-25C Preventive W.R. #26721 N/A N/A Investigated and repaired as necessary.LPRM 08-41D Preventive W.R. #26644 N/A N/A Investigated and repaired as necessary.

LPRM 40-41-A Preventive W.R. #26228 N/A N/A Investigated and repaired as necessary.

APRM (CH-1) 3D Main Steam-Preventive W.R. #25595 N/A N/A Removed and replaced 3D rad. monitor.

lina Rad. Moni-tor G.E. Main Steam-Preventive W.R. #22170 N/A N/A Repaired main steamline spare rad.

line Spare Rad.

monitor.

Monitor APRM #1 Preventive W.R. #26002 N/A N/A Investigated and repaired as necessary.

Accumulator Preventive W.R. #26564 N/A N/A Investigated and repaired the alarm.

(10-19)

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DRESDEN UNIT 3 SAFETY RELATED MAINTENANCE - MAY, 1983 NATURE OF LER OR OUTAGE MALFUNCTION EQUIPMENT MAINTENANCE NUMBER CAUSE RESULT CORRECTIVE ACTION MS Log Rad. Mon.

Preventive W.R. #26143 N/A N/A Inspected and repaired log rad, monitor.

5, 809, 356 1501-5A Valve Preventive W.R. #26466 N/A N/A Removed and reinstalled limit switch.

h

SUMMARY

OF OPERATING EXPERIENCE UNIT TWO MAY, 1983 5-1 to 5-3 Unit Two entered the. month operating at a power level of 543 MWe but shortly thereafter the "B" feedwater check valve developed a gasket leak' causing'the unit to be shutdown.

5-4 to 5-31 Following repair of the leaking gasket, the unit was returned to power and operated continuously the remainder of the month (with normal power reductions on weekends for surveillances),

reaching a power level of 826 MWe with a capacity factor of 80.79% and an availability of 94.02%.

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SUMMARY

OF OPERATING EXPERIENCE UNIT THREE MAY, 1983 5-) to 5-31 Unit Three entered the month operating at a power level of 756 MWe and operated continuously throughout the entire month (with normal power reductions on weekends for surveil-lances), reaching a power level of 820 MWe with a capacity factor of 91.40% and an availability of 100%.

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Commonwealth Edison Dmsden Nuc zr Power St; tion R.R. #1 Morris, Illinois Ml450 Telephone 815/942-2920

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June 1, 1983 DJS LTR: 83-542 Director, Office of Inspection and Enforcement United States Nuclear Regulatory Commission Washington, DC 20555 Attention: Document Control Desk

Dear Sir:

Enclosed please find Dresden Station's operating data for last month. This information is supplied to your office per the instruc-tions set forth in Regulatory Guide 1.16.

Sin re 7,

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D.

. Scott Station Superintendent Dresden Nuclear Power Station DJS: BAS:hjb Enclosure cc: Region III, Regulatory Operations, U.S. NRC Chief, Division Nuclear Safety, State of IL U.S. NRC, Document Management Branch Nuclear Licensing Administrator Nuc. Sta. Div. Vice Pres.

Statistical Research Manager, Tech. Serv. Nuc. Sta.

Tech. Staff EA On-Site NRC Inspector Sta. Nuc. Eng. Dept.

PIP Coordinator - Sta. Nuc.

Comptroller's Office INPO Records Center File /NRC Op. Data File / Numerical

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