ML20071Q343

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Monthly Operating Rept for Oct 1982
ML20071Q343
Person / Time
Site: Cooper Entergy icon.png
Issue date: 11/02/1982
From: Ballinger P
NEBRASKA PUBLIC POWER DISTRICT
To:
Shared Package
ML20071Q340 List:
References
NUDOCS 8212290315
Download: ML20071Q343 (4)


Text

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OPERATING DATA REPORT DOCKET NO. 050-298 11-2-52 DATE COMPLETED BY P.L. Ballinger TELEPHONE 402-825-3811 OPERATING STATUS Notes

1. Unit Name:

Cooper Nuclear Station October 1982

2. Reporting Period:
3. Licensed Thermal Power (MWt):

2381 836

4. Nameplate Rating (Gross MWe):

778

5. Design Electrical Rating (Net MWe):

787

6. Maximum Dependable Capacity (Gross MWe):

764

7. Maximum Dependable Capacity (Net MWe):
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
9. Power Level To Which Restricted. If Any (Net MWe):
10. Reasons For Restrictions. If Any:

This Month Yr to.Date Cumulative 745.0 7,296.0 73,081.0

11. Hours in Reporting Period 714.5 6,020.5 59,906.9
12. Number Of Hours Reactor Was Critical
13. Reactor Reserve Shutdown Hours 0.0 0.0 0.0

/03.8 5,950.5 58,908.0

14. Hours Generator On.Line
15. Unit Reserve Shutdown Hours 0.0 0.0 0.0 1,561,824.0 12,941,856.0 116,630,334.0
16. Gross Thermal Energy Generated (MWH)
17. Gross Electrical EnerEy Generated (MWH) 524,454.0_

4,297,155.0 36,777,942.0

18. Net Electrical Energy Generated (MWH) 507,500.0 4,158,895.0 35,456,273.0
19. Unit Service Factor 94.5 81.6 80.6 94.5 81.6 80.6
20. Unit Availability Factor 89.2 74.6 63.5
21. Unit Capacity Factor (Using MDC Net) 87.6 73.3 62.4

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22. Unit Capacity Factor (Using DER Net) 5.5 3.4 3.9
23. Unit Forced Outage Rate
24. Shutdowns Scheduled Over Next 6 Months (Type.Date,and Duration of Each1:

s 4

25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units In Test Status (Prior to Commercial Operation):

Forecast Achiesed INITIA L CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 8212290315 821102 to/77 i PDR ADOCK 05000298 R

PDR

9 e

DOCKET NO.

050-298 UNIT SIIU1 DOWNS AND POWER REDUCTIONS UNIT N AME Connor Nucla," Statiori DATE 11-2-82 COMPLETED BY P.

L. BallinRer REPORT MONill Octnhor TELEril0NE 402-825-3811 No.

D.it e 5!

k 3 (E

=

Licensee Et

1, Cause & Corrective 50

{j Action to 5

Ivent y3 y

y g =!

Report e in V O

Prevent Recurrence H

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82-9 821005 F

41.2 A

3 N/A N/A N/A Electrical insulation for the control cable for the turbine control valves deteriorated from exposure to heat and radiation of a nearby main steam line and shorted out causing the tur-bine control valves to close. Turbine control valve fast closure initiated a reactor scram. The bad cable was replaced and the plant returned to operation.

1 2

3 4

F: Forced Reason:

Method:

Exlubit G - Instructiims S: Scheduled A-Eiluipment Failure (Explain)

I-Manual for Preparation of Data 11-Maintenance of Test 2 Manual Scram-Entry Sheets for Licensee C-Refueling

3. Automatic Scram.

Event Report ILERI Fde (NtlRI (;-

D-Regulatory Restriction 4 Other (Explain) 01611 1:. Operator Training & Iicense INamination F. Ad minist ratis e 5

(;-Operational Error IExplain t lahibit I Same Source p)/77)

Il-Other (thplain)

6 AVERAGE DAILY UNIT POWER LEVEL 050-298 DOCKET NO.

UNIT Cooper Nuclear Statio@

0 DATE t

COMPLETED BY P.L. Ballinger TELEPHONE

  • MONT}i October DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Net) 743 700 1

37 2

726 732 gg 3

716 39 753 4

727 773 20 5

571 21 777 6

0 22 778 122 778

-- 7 23 g

507 758 24 9

660 25 777 10 640 26 777 11 749 27 777 726 12 g

778 13 732 777 29 14 756 30 775 15 732 33 639 16 759 INSTRUCTIONS On this format. list the average daily unit power levelin MWe Net for each day in the reporting month. Compute to the nearest whole megawatt.

(9/77) k

4 OPERATIONS NARRATIVE Cooper Nuclear Station October 1982 During normal power operation on October 5,1982, 'a failure in the turbine control valve system caused the turbine control valves to close initiating a reactor scram. The electrical insulation for the control cable for the turbine control valves was found to have deteriorated and shorted out from the heat and radiation of a nearby main steam line.

The damaged cable was replaced and the plant returned to operation. The plant operated the remainder of the month with no other power reductions or outages.

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