ML20071C846
| ML20071C846 | |
| Person / Time | |
|---|---|
| Site: | Kewaunee |
| Issue date: | 01/05/1983 |
| From: | Ruiter G WISCONSIN PUBLIC SERVICE CORP. |
| To: | |
| Shared Package | |
| ML20071C843 | List: |
| References | |
| NUDOCS 8303080166 | |
| Download: ML20071C846 (4) | |
Text
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DOCKET 50-305 KEWAUNEE NUCLEAR POWEB PLANT
SUMMARY
OF OPERATING EXPERIENCE December, 1982 GPER A TIO NS:
On December 6, load was decreased to 50% to remove FWP 1A from service to inspect a noisy speed
- increaser.
The monthly turbine stop valve operability test was also completed.
FWP 1A was returned to service on December 8, and generation was increased to 100%.
On Monday, December 27, a leak in an elbow on the drain line from MSR 1B1 to the Heater Drain Tank forced a manual trip of the turbine..The unit was returned to service on December 28.
l On Thursday, December 30, a leak in an elbow on l
!( M M $iM3fA M @ 2N5$the HSR 1B1 drain to FWH 15B forced a reduction to 50% power to remove the F WH from service..Later the same day, the unit was returned to 100% power and FWH 15B was put back in service.
l M AINT EN A NCE:
Replaced
- a defective Holdup Tank level transmitter.
Replaced a defective Shield Building Vent damper controller.
Overhauled a Service Water Pump motor.
Overhauled a Charging Pump.
8303080166 830110
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AV ER AGE DAIL Y UNIT POW ER LEY EL DOCKET No-50-305 UNIT-KEWAUNEE COMPLETED BY-G.
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RUITER T EL EP HO NE-414-388-2560 X225 REPOET MONTH DECEMEER, 1982 AVERAGE DAILY DAY POWER LEVEL (5 W E-N ET) 1 313 2
513 3
513 4
513 5
518 6
370 7
235 8
292 9
509 10 513 11 513 12 513 13 518 14 514 15 514 16 514 17 513
?YYYEE&Ylkl*Wh55$4SEb!5Nb~$N:<CANI 18 514 19 514 20 509 21 514 22 514 23 509 l
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25 435 l
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.a as D'N I T S H U T D Or N'/ N S AND PO9ER f-REDUCTION 5
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DOCKET NO: 50-305 5
UNIT NAME: Ke ua unee L
- 6 DATE: January 3, 1983 j
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Puiter TELEPHONE: 414-388-2560 x225 o n.
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REPORT MONTH - DECEMDER, 1982 g,
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'l NO. l DATE } TYPE }DURATIONIREASONl METHOD l LER NUMBER lSYS I CORPONENT l COMMENTS l
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3 1 7 112/ 6/821 S'
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7.
A load reduction to 50% power was taken for I I
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i repair of Feedvater Pump la speed increaser 1 b
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The reactor and turbine were manually tripped I b
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due to a stream leak is a line tetween a i g
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moisture separator and the heater drain tank.
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9.
A load reduction to 525 power was taken for i g
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repair of a leak in a 4-inch steam line at i I
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I Feedvater Heater 15B..
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TYPE S E AS ON HETHOD SYSTEM & COMPONENT CODES g
F: Forced A-Equipment Failure (Explain) 1-Manual From NUREG-0161
.l V S: Scheduled E-Maintenance or Test 2-Manual Scras g
C-Re f ueling 3-Automat ic Scran D-Regulatory Restriction 4-Continuatisns V
E-Operator Training & License Examination S-toad Reductions j
F-Administrative 9-Other G-Operational Error (Explain) v li-Ot h e r (Explain)
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DOCKET No-50-305
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v' COMPLETED BY-G.
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RUITER L
0PER ATING STATUS kf?
TELEPHONE-414-388-2560 1225
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1 UNIT NAMR FEWAUNEE ye TA
- 2 REPORTING PERIOC DECEMBER, 1982
$* NOTES L
3 LICENSED THERM AL POW ER (MWT) 1650
.Y
- The unit outage described in the Unit i* Shutdown Report ended a run of b
4 NAMIPLATE RATING (CROSS MWE) 560
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continuous operation at 216 days.,
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5 DESIGN ELECTRICAL RATING (WET FWE) 535 9*
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e 6 MAIIMUM DEPEND AELE CAPACITY (GROSS MWE) 542 s*
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b 7 MAIIMUM DEPLif DAELE CAPACITY (N ET M E E) 514
(**********************************************
3 8 IF CHANGES OCCUR IN CAP ACITY PATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS V
MDC(net) an d MDC (gross) were updated based on the winter capacity test.,
j V
9 POWER LEVEL To tiHICH RESTRICTED, IF ANY (NET MWE) None g
10 REASCNS FOR B ESTRICTIONS, IF ANI G
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V TH MON 1H YR-TO-DATE COMULATIYE g
i 11 HOURS IN REPOETING PERIOD 744 8760
- 74905 L
4 g
12 NU MBER OF HOURS REACTOR WAS CRITICAL 733.3 7749.7 63751.6 L
13 REACTOR RESERVE SHUTDOWN BOURS
- 0. 0
- 0. 0 2330.5 g
14 HOU RS G ENER ATOR ON-LINE 710.3 7669.8 62476.6 15 UNIT RESERVE SUTDOWN HOURS
- 0. 0
- 0. 0 10.0 y
16 GROSS THERM AL ENERGY GENERATED (MWH) 1077471 12293067 97100001 J
17 GROSS ELECTRICAL ENERGY GENER ATED (Mus) 350800 4015200 31967600 18 NET ELECTPICAL ENERGY GENERATED (M W R) 334042 3824851 30425108 y
19 UNIT SERVICE FACTOR 95.5 87.6 83.4 g
20 UNIT AVAILABILITY F ACTOR 95.5 87.6 83.4 21 UNIT CAPACITY FACTOR (ft,ING MDC WET) 87.4 84.9 7 7.'J V
22 UNIT CAPACITY FACTOR (U:.ING DER NET) 83.9 81.6 75.9 g
23 UNIT F3RCED OUTAGE RATE
- 4. 5
- 0. 5
- 4. 3 24 SHUTDOWNS SCPEDULED OVEI: NEXT 6 MONTHS (TYPE, DATE, AND DUR ATION OF EACH)
Eefueling shutdown of 8-week duration is scheduled to start on March 20, 1983..
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25 IF SHUT DOWN AT END.0F REPORT PERIOD, ESTIM ATED DATE OF STARTUP - N/A i
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