ML20070H905

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Monthly Operating Rept for Nov 1982
ML20070H905
Person / Time
Site: Salem PSEG icon.png
Issue date: 12/10/1982
From: Miller L
Public Service Enterprise Group
To:
Shared Package
ML20070H886 List:
References
NUDOCS 8212270280
Download: ML20070H905 (19)


Text

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, AVERAGE DAILY UNIT POWER LEVEL Docket No. 50-311 Unit Name Falem # 2 Date Dec.^iO, 1982 Ccmpleted by L. K. Miller Telephone 609-935-6000 Extension 4455 Month November 1982 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 880 ___ 16 710 2 894 17 578 3 849 18 612 4 865 19 159 5 869 20 779 6 865 21 808 7 865 22 842 8 865 23 824 9 849 24 880 __

10 874 25 874 11 866 26 854 12 818 27 858 13 876 28 861 14 837 29 874 15 839 30 869

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OPERATING DATA REPORT Docket No. 50-311 Date Dec. 10, 1982 Telephone 935-6000 Completed by L. K. Miller Extension 4455 Operating Status

1. Unit Name Salem No. 2 Notes
2. Reporting Period November 1982
3. Licensed Thermal Power (MWt) 3411 4, Nameplate Rating (Gross MWe) 116'2
5. Design Electrical Rating (Net MWe) TTf5
6. Maximum Dependable Capacity (Gross MWe)1149
7. Maximum Dependable Capacity (Net MWe) 1106
8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason
9. Power Level to Which Restricted, if any (Net MWe) None
10. Reasons for Restrictions, if any N/A __

This Month Year to Date Cumulative

11. Hours in Reporting Period 720 8016 9962
12. No. of Hrs. Reactor was Critical 718 7852.3 9711.6
13. Reactor Reserve Shutdown Hrs. 0 36.5 36.6
14. Hours Generator On-Line 706.5 -~ 7775.5 9593.2
15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Thermal Energy Generated (MWH) 1916650 23535757 28643776
17. Gross Elec. Energy Generated (MWH) 612750 7709390 9418260
18. Net Elec. Energy Generated (MWH) 583022 -

7374158 9006225

19. Unit Service Factor 98.1 97.0 96.3
20. Unit Availability Factor 98.1 97.0 96.3
21. Unit Capacity Factor (using MDC Net) 73.2 83.2 81.7
22. Unit Capacity Factor (using DER Net) 72.6 82.5 81.1
23. Unit Forced Cutage Rate 1.9 3.0 3.5
24. Shutdowns scheduled over next 6 months (type, date and duration of each)

Refueling Outage, January 22, 1983, 18 weeks

25. If shutdown at end of Report Period, Estimated Date of Startup:

N/A

26. Units in Test Status (Prior to Commercial Operation) :

Forecast Achieved Initial Criticality 6/30/80 8/2/80 Initial Electricity 9/1/80 6/3/81 Commercial Operation 9/24/81 10/31/81 8-1-7.R2 Page 3 of 20

UNIT SHUTDOWN AND POWER REDUCTIONS Dockst No. 50-311 .

Page 4 of 20 REPORT MONTH November 1982 Unit Name Salem No.2 Date Dec. 10, 1982 Completed by L.K. Miller Telephone 609-935-6000 -

Extension 4455 Method of Duration Shutting License Cause and Corrective No. Date Type Hours Reason Down Event System Component Action to 1 2 Reactor Report Code 4 Code 5 Prevent Recurrence ,

Nuclear Main Steam 82-448 8/12 F 2654.7 A 5 ---

HB VALVE X Safety / Relief Valves Traveling Screens / Trash 82-741 10/30 F 63.6 A 5 ---

HF FILTER Racks /Qinal Screens

,82-742 11/02 F 42.8 A 5 ---

HF FILTER 82-743 11/02 F 21.5 A 5 ---

HF FILTER 82-744 11/03 F 626.1 A 5 ---

HJ PUMP XX 22 Htr Drain Tank Pump Traveling Screens / Trash 82-745 11/05 F 3.5 A 5 ---

HF FILTER Racks / Canal Screens62-746 11/U5 F 20.0 A 5 ---

HF FILTER 82-747 11/06 F 8.5 A 5 ---

HF FILTER 82-748 11/08 F 10.4 A 5 ---

HF FILTER Feedwater Regulating 82-749 11/08 F 1.7 A 5 ---

HH VALVE X Level Cantron Valve Traveling Screens / Trash 82-750 11/08 F 2.5 A 5 ---

HF FILTER Racks / Canal Screens82-751 11/09 F 8.6 A 5 ---

HF FILTER Condenser Tube Leak 82-752 11/10 F 10.3 A 5 ---

HC HT EXCH Inspection 82-753 11/10 F 10.3 A 5 ---

HC HT EXCH Traveling Screens / Trash 82-754 11/12 F 22.5 A 5 ---

HF FILTER Racks / Canal Screens Condenser Tube Leak 82-755 11/12 F 8.5 A 5 ---

HC HT EXCH Inspection Traveling Screens / Trash 82-756 11/12 F 93.8 A 5 ---

HF FILTER Racks / Canal Screens82-757 11/15 F 1.0 A 5 ---

HH PUMP XX Condensate /Motwell Pumps

1 Page 5 of 20 Docket No. 50-311 Unit Name Salet i 2 Rept. Month Nov. 1982 -

Page _2

~~~

Method of Shutting License System Component Cause and Corrective No. Date Type Duration Reason Down Event Code Code Action to 1 Hours 2 Reactor Report 4 5 Prevent Recurrence 82-758 11/16 F 16 " A 5 ---

HH PUMP XX Condenser Tube & Water 82-759 11/16 F 67.6 A 5 ---

HC HT EXCH Box Cleaning 82-760 11/17 F 60.4 A 5 ---

HH PUMP XX Condensate /Hetwell Pumps Condenser TuSe Leak 82-761 11/18 F 36.0 A 5 ---

HC HT EXCH Inspection

  1. 22 SGFP Trip-caused Low 82-762 11/19 F 13.5 A 3 ---

CH PUMP XX Feed Flow with Low Level on 424 SG Condenser Tube Leak 82-764 11/19 F 9.3 A 5 ---

HC HT EXCH Inspection Condenser Tube & Water 82-765 11/19 F 40.3 A 5 ---

HC HT EXCH Box Cleaning Condenser Tube Leak 82-766 11/20 F 81.9 A 5 ---

HC HT EXCH Inspection 82-767 11/21 F 24.8 A 5 --- "82-768 11/21 F 7.5 A 5 ---

A 82-769 11/23 F .2 5 --- 82-770 11/23 F 10.1 A 5 --- " " "82-771 11/24 F 18.6 A 5 ---

Traveling Screen / Trash 82-772 11/25 F 9.7 A 5 ---

HF FILTER Racks / Canal Screens _

82-773 11/25 F 8.8 A 5 ---

Condenser Tube Leak 82-774 11/25 F 15.2 A 5 ---

HC HT EXCH Inspection 82-775 11/26 F 11. :. A 5 --- 82-776 11/26 F 27.9 A 5 --- 82-777 11/27 F 5.7 A 5 ---

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1 Page 6 of 20 Docket No. 50-311 Urtit Name Salem # 2 Report Ma th Nov. 1982 Page 3 -

Method of Duration Shutting License System Component Cause and Corrective No. Date Type Hours Russon Down Event Code Code Action to 1 2 Reactor n eport 4 5 Prevent Recurrence 82-778 11/28 F 15.1 A 5 ---

Traveling Screen /Traj.-

82-77:1 11/29 F 40.2 A 5 ---

I' FILTER _ Racks / Canal Screens82-78C 11/29 F 28.0 A 5 ---

p 1 2 Reason 3 Method 4 Exhibit G 5 Exhibit 1 F: Forced A-Equipment Failure-explain 1-Manual Instructions Salen as

,
Scheduled E-Maintenance or Test 2-Manuhl Scram. for Prepara- Source

- C-Refueling 3-Automatic Scram, tion of Data E-Regulatory Restriction 4-Continuation of Entry Sheets E-Operator Training & Licensing Exam Previous Outage for Licensee F-Administrative 5-Load Reduction Event Report G-Opt. rational Error-explain 9-Other (LER) File H-Other-explain (NUREG 0161)

.5

502TED BY SALFM br%rkATING STATION DALE iP/6A/8?

DEPA3TMENT, WO*K 0" DER Nn. SAFFTY Ott af t p Futil prF N T wnog Opor9 LPG - UNIT P PAGF 0001 49IK OIDE2 NUMBE2 DEPT EQUTPMENI InENTIFTCATION EXPLANAff0N OF nnNW *ECFnRMEn I

101104 4 VALVE 24SN69 DE9COIpTTON OF PPnaLFM, 1/4 GPM PACKING LEAM. 474809 IR A2-196 .!

IER 42-070 .1 f.HdPFriTVF ArTION, ADOFn 1 RING OF PACKING aNO ADJUSTFD ,

  • 20810 l

~~~

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401919 4 CONT FAN COTL UNIT,74 l nESCDIPTinq nF PROPLEM, r0TL LFAM 1G"M M70R15 IR 47-217 LER A2-75 CnRRFrTTVF ACTION, REL70NAED LEAK 3RD COIL FROM RDTTOM ON SECONDARY sgnt, q20417 605160 8' VALVE,hMS137 )

nESCDIPiipN OF PDORLEM, OpFN AND INSPECT VALVE STNAINER FOR DEmdIS 820811 IR 82-241 LER 87-95 4

CORRECTIVE sr* inn, REMOVED THE VALVE Ahn FOUNn THE PIECE FROM l MS46 VALVE. F0HNn 9 EAT STEAM Clf T . I REINSTALLEn VALVE. 570901 906570 4 cnNT AIR LOCH EL 100 DESCRIPTION OF PRORLFM, OUTEo nonR HAS HIGH LEAK RATF. 420927 j IR 87-P91 1 CnWWErTIVF ArTinN, rHFCKED SAT. nPERATOR FRune ON LEAM TEST.

A20972 {

l 406532 M PUMP,PI SFRVICE NATER Page 7 of 20

_ _ _. a

9 SORTED BF SALFM GFNFwAylur,'IATION DATF 12/nn/sp nEPARTMENT, WOOM 00nER No. SAFrTV *EL A fr a F i)H I P uF tp woog nonpp (ng . HNIT 7 PAGF 0007 WORK ORDER NUMSER DEPT EQUTPwENT IDENTTFICATION FYPLANATION OF WORM PERFnyMFn nESCPIPTTON PF PRORLFM, LEAM TM SERVICF WATER LI'< rn MOTOR C00LFR 420921 IR 42-292 LFR 82=t11.

CnHRFCTivF AcTink, REPLACFD 6 INCM PIFCF OF 3/4 INCH PIPE DOWNSTDEAM HF 23SW13. m2n972 a06539 4 VALVE,PcSW91 DESCptoTTON OF PDnRLTM, FMCESSTVE SERVTCE WATER LEAKING U5nER VALVE TNSul ATICN. 820923 IP A2-303 CPRCECTTVF AcTinN, PAD NELDFD LFANS. REFINISHED CEMENT LINihG TNSIDE LTNF. 820929 906692 M C70LEp.?A DTESEL LHAF OTL DESCRIPT10N OF PRnRLFM, CAA DN HIPPLF nN LHHF nII. ConLER HAS FRnDED AWAY. 87092R IR SP-117 LER 82-115 CONRFCTIVF ACTinN, REPLACFD CAPS. P.2092R 4J6693 4 SFr 2R nE9ColpTTF OF P9nRLFM, ALARM POINT 7 EON'T CLFAR. 620928 CORRttTTVF erTInu, REPLACFO Faut.TY CHASSIS 1964-1001 WITH NFW CHASSIS 1964=lf.v9. TFSTEn SAT. A70928 907395 u PHMP,71 CnNT SPRAY DESCRIPTION nF PDORLFM, 12SVDC FONTNnt PWR hTLL NOT RESET nN Aur ALARM. PtWP WIL L NOT START. 8209n4 TR 87-P5% LFD A2-103 l l

Page 8 of 20

'ORTED ev SALFu GF*+FRATINC staff 0N DATE IP/06/87 OEPARTNENT, WORK ORDFR Nn. SAFFTV PEtATrn FoytodFNT kORM fl00FW Ln  ? PAGF 0003 WORN ORDEC NduglR nEPT ECHiPufMT InENT)FICAT70N F) TON nF MnRK PERFORMED CnRREC1Tv acTinN, PERACMFD 4MV HWk TO PFMAKE HL5?e ALARM RESET AND RkR IS Ft'LL Y OPRFARLF. A20904 907449 M CONT FAN COTL UNIT,P3 DE SCD I P f it.N nF Po nPLFM, COnLINC COTL SFkVICE WATFR LFAN. 820406 IR 87-P57 LER 42-091 CORRFCTTVF ArTinN, PATCHED LEAK IAW OR MD-1736 670907 100635 M PitMP,21 COMP CUOLING DESCpfPTION nF PROALFM, RFPLACF nUTHn&R0 HEARINGS. VTARATInN UP 70 1.5 MILLS. 820R10 CnRDErfiVF ACTION, REPLACFD OllTROARD PEARINGS.870913 90R860 M CDAT FtN COTL UNIT l

OFScoIPTTt1H nF PRnRLFM, REPATR THRF LEAM IN TOP PRIMARY COTL.

M21003 IR A2-3t! LFR 87-117 CORRECTIVF ACTION, plt!GGED 8 TURES,4 TN 3RD P#IMARY AND 4 [N IST PRIMARY. 371014 900999

  • CONT FAN COTL UNIT,P2 DESCRIPTTON nF PPORLFM, LEhK IN CFCU 27 IST C0!L PRIMARY 16TH TURE flP.821015 CnRpECTivF AC11nN, REMOVED RLANKS AND INSTAlLFO GASNETS.

VER{FIFO LFAN "EPAYWS. RFPAIRED REPORTED LEAM IAW MllV. R?t014 I

e Page 9 of 20

90RTED BY SAlFM GENFRATINr. STATinN DATE 12/06/87 nEPARTMENT, WORK nonrR Nn. SAFriv del.ATFS F'3HipwFNT know DRDEn lng - UNIT ? PAGF 0004 CORR ORnER NUMBER DEPT EQt1TPvENT InENT TF T C A T I' ei FIPLANATION nF mnRK PERFORM!n 900010 M CnMPRFSSOR,82 E" ERG ATR DESCRIDTTON OF FRnRLFM, COMPRESSnp OnES 40T SEFM in ME DEVELOPING ANY OUTLFT PRESSURF. 870712 TR 92-1F4 C1'RRECTiVF ACTInN, NO APPARFNT PRnH*FM. 8P0713 009092 M CONTRnLLER,HT iRACF 2610A nESCRIPTTON nF PRnRLFM, CKY F#TLED SHWVETLLANCE. CONTACinR DOEM N': T $wili WHEN CALLFD Fnd BY CONTROLLER.

8/07iT IR AP-183 LFR 87-N 9 CnRRECTIVF ACTInN, REPLACFD BROKEN WIRE TR1-8 TO 181-36. WIRE PARTIALLt DAMArED DURING INSTALLATTON.

A70721 96'094 M HT TRACF CKT Ph0AR DESCPIPTTON nF PonPLFM, CIRCllIT ORAWTNG 7ERO AMP 3 nURING TEST.

CONTACTS VERTFIEn CLOSED. A20717 1R 92-1A3 LER A2-064 CnRRECTIVE ACTinN, REPLACFD HEAT TAPF 2604Aeg, n207pg 909112 M CnNT FAN CnTL UNIT,71 nESCRIPTinu 0F PRnRLFM, REPATR COTL LEAK. 82081A IR P2-718 CnRRECTTVF AeTION, PATCHEn ConLER. 42n876 416707 M CONT FAN COTL 0417,71 nESCRIPTTON OF PRORLFM, MULTIPLE CDIL LEAKS. A7141] TR 87-120 LER 82-170 Page 10 of 20

_ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ . _ _ _ _ _ _ _ - - - - .- - .- _J

302TED BY SALFM GFNFRATINC 9TATIUM DATE IP/n6/sp OE'A#iMENT, WORK OROFR Nn. SAFFTY REI ATF n FW;IPwFNT %ORM MorF4 LUG - O*'I T 7 PAGF 000%

WO!K l 0%0E9 NUM Em nEPT E Q U T PME'J T IDENTTFTCATION FXPLANA710H OF wnRK PERFORMEC CORDECfiVF arTinN, RERAIRED LFak WITH i)E L 7DN A . A21016 916st2 M PtlMR Pl CHARGINC nESCOIPTTON nr PRORLEMe SIX INCHF" 0F WATER IN BOTTOM OF PUMP OIL DESERVnth. 871019 TR A7-173 LER A2-126 CDRDFCITVF ACTIDN, REPLACFD LUPF OIL COnLE9. 8 2 f a ? 0 _ .._ _

916910 M RilS,2F 4KV DESCRIPTitsN OF PRnRLFM, MONENTARY llNDERFRF4 ALARMS PFRIqn!CALLY COMING HP ON AtlX TYPEnRITER AND RPa.

A21011 IR M2-348 LER 82-12a l

CORRECTTVF ACT]nN, FOUND N0?PF ON 2F 4KV TN EXCESS OF 6 VOLTS l REPLACFG 50*FW SUPPLY ON 24 DIESEL PANFL ALARM RESULTING IN NntSE RT0liCTinN TO a VDLTS. R?lott 916914 M CONT FAN COIL UNIT,71 i nFSCRIPfinN OF PROPLFM, COIL LE4w. 871n0A TR A7-31R LER A2-119 CORREClivF ACTinN, REPAIWF0 MiiH RELZONA IAM M11V. 821014 916167 M CONT FAN COTL UNIT,73 OE9CRIPTTON OF PROP L F '4, SERVICE WATER PIN HulE LFaw. PP1002 IR M2-296 COWRFCTTVF ACitos, PELIONA REPATW 10 7 TURES. A21007 937897 M INCORE nETECinR THi?4RI E 9 Page 11 of 20

SODTED BY SALEM GFNF4ATIFC 9TATTON 0410 12/06/32 DEPAatEENT, '. G SM ORDEk NO. SAFFTY OFLATFD FuHIpw.Fhi wqen ODOFR LOG - UNIT 7 PAGE 0006 COXK 02DED NUMBE2 DEPT EQ U T P*AE h i InENiiFICATIGH FXPLANATION OF n0Rr PERFP%MED nESCDIPTTU4 DF PWnPLFM, ARHSH OUT FOLLOWING THtHRIESf0 RIVE LOC).

A-1,2,4 R-4,A C-1,2 n-a F e2 F- A. 821007 l C"W'ECTTVF ACT ina s, RRUSHEn 00T 6 nr 10 9LDCNED THTMRLES. FOUR l WEPE VERY DIFFICULT. 871G14 -

VALVE,73MS86 l 491052 M

DESCRIPTTON OF PRnRLEM, FLAPPER HAS AECOME DETACMF0 FROM HANGER l ARM. DISCOVFDED PY RADIOGRAPHY. REPLACE l

FLAPPER AND LOCATE MISSING NUT, WASHER AND 1 l CUTTER PIN. 421004 IR 42-333 LER 87-121 CORRECTiVF ACTION, PEPLACED VALVE INTERNALS. RETRIEVED MISSING PARTS FROM 2MS52 VALVE STRAINER.

M21005 991053 M VALVE,214946 DESCRIPTTON OF PRORLVV, RADIOGRAPHY REVIELED HANGER ARM OISTORTED. l DEPLACF HANGFR ARM. 821005 CORRECTTVF ACTinN, REPLACED HANnER ARM. 871005 491377 M RAD WASTE STOR TM FREFil PROT DESCRIPTION OF PRORLFM, TFMP IND FAILFD DORIC PT 7A8. TAC FOUND OPFN THERHOCOUPLF LEADS IN C AHL E 2VHT4 A440

  1. ERLACF CARLF. 870720 CPRPECTTVF ACTinN, REPLACFD CARLF PVHT444-AQ AND CARLE RVHT185-44 RFCAUSE ONE wn.JtD NOT COMF OUT WITonuT THF nIHER. 370A17 i

i Page 12 of 20

MORTED BY SALFM GFa'ER A T ING 9TATION 0 ATE 17/06/02 i DEPARTMENT, 90fM OpnFR NO. SAFFTY DELATFD FGHIPMFNT PORK 04DFR L OG - HNIT 2 PAGE 0007 i WORK I n:DEQ NUMsE2 DERT EDUTPaENT InENTTFICATTON etPLANATTON nF wnRM PERFORMED i

C01177 P WMS.2417A DESCRIRTION OF PRnRLFM, MONTTnp FAILEn. R20812 IR 82-211 CORRECTivF AcTinN, ALL FUNCTIONALS CHECK SAT. CONT ISOL OPERA SAT. CRT PRINTEN A NEMnTE CONTROLLER ALL SAT. RP0412 401141 P CONT FAN Coil UNIT,25 DESrpIPTinN nF FRORLFM, IN LOM SPEFD, MERVICE WATER FLOW LESS THAN 1200 GRM. M20812 IR 82-279 LFR 82-080 rnppECTIVE ACTION, ALEN DOWN INLET A DUTLET TRANS. PURGED INST LINES WTTH N2. TOOK D/P READINGS ANO CTCLFD SYS. MAINT F0HND r,RnHND PROB IN ANNUNCIATOR CMT. A70812 401212 P WMS 2R12A DESCR2RTIDH OF PRnRLFM, READING CONSTANT. 420806 IR 82-210 LER 82-076 f,0NRECTIVF ACTION, REPLACED TFST JACK IN SCALER. ADJUSTED nISCRIMINATOR. 820406 401834 P CONT FAN COTL UNIT,73 DESCRIPTION OF PROHLFM, 2200 GRM SERVICE WATER FLOW TN LOW SPEED.

820M11 TR 82-745 LFR A?-09A CnRRECTIVF 3CTInN, ALEd OHT INLFT AND OUTLET TRANSMITTERS.

EXCFRSTZED 23SW57 SEVERAL TIMES 70 GET Page 13 of 20 l

MORTED RY SALEM GFNERATINC 9TarTOM DATE IP/06/8/

nEPARTMENT, WORK OpnFR NO. SAFETY RFL AT5 0 FollipMFN1 WOOW nWDFR LC6 - UNIT ? PAGE Onne WORK ORDER 9UM8FR DEPT EDUTPuENI 10ENTIFTCATION FXPLANATTON nF WORK PERFnRMED nESIRED FLnw. 820901 904044 9 CnNT F AN C0fL UNIT,22 1

! DESCOIPITON nF PRORLFM, NO INDICATFlp FLOW TN HIGH SPFEO. LESS THAN 700 CPM IN LOW SPEED. 82n501 IR A2-107 LER 42-015 CPWRECTTvF ACTInN, FREEn llP 225W57 ITCHTENED POSITIONER AQM.

VERIFIFD FLOW. 820501 904459 P A00,20114 nESCRIPTION OF PenPLEM, FIL TER DRIVE INODERARLE. 870027 IR CT=309 LER 42-114 CORWECTTVF ArTION, F O U*!D SOLENOTO ARM WHICH .YTACHES TO PATCHFT COG DISCnNNECTFD. REASSEMBLED AND LOADFD NFW FTLTER ROLL. TESTFD SAT. A209P7 s 9044G0 P RMS,2R17R DESCDIPTTON OF PROALFM, CHANNEL FATLFO. 4E9?28 CORRECTTvF ACTION, REPLACED ACIA CHIP IN '6AI M00t:LF. REPAT9 RACMPLATF,REPLACEO DAM 4GFD PINS. REPLACFO A47 TN ANALY7ER 400UIE. RESET HV, CLEARED RAMS. CHECKEn SAT. A2100%

906696 P CnNT FAN COIL UNIT,23 nFSCRIPTTON OF PPnRLFM, t.0W SERVICE WATER FLO4 IN LOW SPEED M2n979 TR 82-314 LEP R2-IIT Page 14 of 20

50]TED gy SALFH GFhEDATING STaitDN DATF 12/06/A2 nEPA%TMENT, WORK 000FR NO. SAFFTV DEsATFn FQHipMFNT vopw OROFR lng - UNIT 7 PAGE 0009 WOIR ORDE3 l NUW2E2 nEPT EQUIPwFNT IDENTirTCATION FXPLANATION OF 40kK PERFORMFD CnRDFC1FvF ACTION, SHFLLS FOUND i t' 735457 LINF. 820930 407260 P CONT FAN COIL UNIT,ps nESCRIDiiON nF PPORLFM, WMFN PLACE 0 IN HIGH SPEEO, 5tRVICE MATER FLnw RISES TO 600 CPM THFN FALLS TO 2ERO.

I.0W SPFEn SAT. 870913 l COR9ECTTVE ACTinN, REPLACFD DFFFCTIVE CIRCUTT PDARD IN FA-3176CP. 820411 ,

1 407268 P VALVE.21SW24 l

DE9C#IpTTON OF PpnRLFM, ACTUATOR DOFS NOT APPEAR TO BE FUNCTIONING THFREFORE VAL VF ST AYS CLnSED. 820913 CORRECTTVE ACTinN, REPLACED cCFFCTIVE SnLEN010 VALVE AND P140NED COIL WITH SAME TYPE. 820915 l l

407347 P VALVES.24,25,768w24 )

nESCRIPTION nF PDnRLFM, VALVFS UNDFRW4TER. PDOVIDE SIIPPORT TO IN90RE VALVES AWE OPFN. 420917 CnRRECTIVF ACTION, REPLACFO COILS ON SV262,263,AND 764.820917 I

907338 P CnNT FAN COIL UNIY,25 nE9CRTPTTON OF POORLFM, LOW SERVICE WATE8 FLOM IN LOW SPEED.A20902 IR 82-256 LED A2-049 CnRRECTiVF ACTinN, CYCLED 23ShS7 ann 73FW723 620907 907417 P CnNT FAN COTL UNIT,22 Page 15 of 20

1 503TFD RY SALFM GFNFRATINC 9TATTON DATF 12/06/82 j DEPACTMENT, WORK 0*DFR NO. S AFETY DEL ATFn FuistpwrNT =0pm opnFR lng - UNIT 7 PAGE 0010 '

l CORK '

OIDED NUMBF# nEPT EQUIPMENT IDENi t r iC A T TD's rXPLANATION OF n0RW PERF0WHED ,

l nF9CRIPTTON OF PRnRLFu, SLRVICF WATED IS HEL0n RFQHIREFr FLOW.

320908 IR 82-264 LFR M2-105 CnPoECTIVF ACTION, CYCLEN 22S457 SEVERAL TIuES. 820108 901073 P CnNT FAN COIL UNIT,24 OESCRIPTION OF PRORLFM, ;E7EL INDICATION FOR SERVICE WATER ZERO

/OR HIAM OR LOW SPEED. 820720 IR 82-187 l I'

CnRRECTTVF ACTION, REPLACED BROMEN LINKAGE ON 245W223 91ROMEn VALVF AND VERIFIFO FLOW. 820727 4010%0 p RMS,2RttA DESCRIPTION OF PRnRLFM, FILTER TEAR ALARM. 82072P IR AP-191 CnRRECTTVF ACTION, T4MEUP SPOOL Nni MOVING WHEN MANIfALLY ADVANCED. LODSFNED TOP CLAMP 4 VERIFIED PROPER OPERATIDM. M207?2 916805 P RMS 2R414 DE9C#IPTf0N nF PRnRLFM, CHANNFL APPEARS FATLES. A7into IR A2-371 CORRECTIVF ACTION, REPLACED FTPRT STAGE Op-AMD 4 CHANGE 0 R7 FROM in 70 Ino OHMS PFo ARit4T. REPLACED RROKEN WTRF ON TFST SNITCH. a21019 I 914592 P SSPS TRA]N N nESCRIPTinM nF PRnRLFM, LOGIC R 16 A 20 FOUNO OEFECTIVE OURu?G FUNCTIONAL TFST. 821013 TR 82-352 Page 16 of 20

SQRTED BY SALFM GFNFRaytNG SsATinN DATE 12/06/87 OEPARTMENT, .TQ9M OQDFW NO. SAFFTV WELATED FCIII puF N T WDDA ODDFR LOG - UNIT 7 PAGF 0011 WORG ORDER i NUMBFR DEPT EQUIPME NT IDE N T IF T L A T TOPJ FKPLANATION nF WORT PERFnRMED CnRoECTIVF A C T I nk', REPATRFD UNIVEDSAL CARD 9/N 2962 A204 RE TE 9 f Er: SAT. P21013 9900Q3 P NTS 2N56 DESCRIPTION nF PROP,FM, T NVE9T TG A'F C Al'SF nF P6 AISTAHLE NOT TRIPPING WHF N TNSTRU4ENT PonER FHSES WERE REMOVED. 870408 _ __

CnRRECliVF ACTInN, P6 HISTARLE nq.3N'T TRIP ON LOSS OF *NST PWR ON N35 00 N3A. BTSTAPLE WIRED TO TRIF ON INCREASTNG PWR. WHEN FUSES PULLED, DWR AC?S LIKE A nECREASING PWR rnND. 620625 991174 # FEED FL,0W CH ?,24 S/G DESCRIPITON OF PRORLEH, SENSOR FOUND OUT OF CAL nORING SFNSOR CAL PROCFOURE. 870720 IR 82-183 CORRECTTVF ACTInN, TRANSMTTTER WDifLD NG'I REPE A T DUR T P'G C AL .

PEPLACED TRANSMITTER. A70721 991177 P #74 S/G PDESSI'RE CH7 nFSCDIPTTON OF P9nALEM, PRS-52944H TRIP ann RESET POINTS art THE SAME. A20721 cnRDECTTVF ACTION, REPLACFD DFFFCTIVE ISOLATOR ann COMPARATOR ADJ:ISTED SFTPOINTS AND COMPLFTLi) l FUNCTIONAL. R207P1 Page 17 of 20

SORTED BY SALFM GFNFWATTNG STATION DATE 12/06/82 DEPADTMENT, WORK ORDER NO. SAFFTv RFLATED F Q t t I P"F N T rops ORnFR LOG - UNIT 2 PAEF 0017 CORK n 0E2 NU;;FA DEPT EQUIPMENT IDENTIFICATTON FIPLANATION OF n0RK PERFnRMED i

991181 P INST Ril, ISOL A TOR Qu-909 OESCRIPTTON OF PRORLFM, INPUT TS 3.61A VDC. DUTPUT IS 8.75 VDC.

F20804 CORRECTivF ACTION, REPLACED ISOLATOR S/M 00-403 WITH S/N 00-461. 42080%

~~ ~

991187 p VALVE,2*MS10 OESCRIPTTbN OF PRORLEM, CONTROL GOES TO MANUAL WHEN INCREASING SETPOINT. 870H06 CDP'ECTIvF ACTION, REPLACED 800 MICROFARRAD CAPACITOR.ON 2HC-516B SfAvu DRIVEN SETPDINT STATION.

P20806 491190 P RC FLOW, LOOP 4 CHP DESCRIPTION MF PROALFM, CHANNEL F0tIND 007 0F CAL DH71NG FUNCTIONAL TEST. n20816 CORRECTTVE ACTION, FOU33 180LATOR 2FM-445 S/N 00-801 READINC ONF 00 TFilT WHEN OIFFERFNT INPUTS INJECTED.

REPLACED 00-401 WITH 00-473 820P16 991197 P ACCllMULATORS,73A24 l DESCRIDITON OF PP0aLFM, VERIFY PRESSIIRF ALARM SETPOINTS FOR ALL PkFSSURE CHANNFLS. 620821 COR'ECTTvF ACTION, REPLACED OLD STYLE CAPACITORS IN 2PC936C/G AND 2PC9370/H. A0JHSTED CHANNELS TO SPEC.

A20All TOTAL LINES = 000259 TOTAL A-RECS = 00h050 LAST UPDATE R21202 210307 ENTER COMMANOS FNO OF RHN Page 18 of 20 CB:KPT PRINTS

I" SALEM UNIT 2 OPERATING

SUMMARY

November 1982 l

Unit 2 continues to be limited to 82? due to a gagged safety valve.

Raactor power was reduced to 80% on November 15 due to #23 condensate pump bearing noises, and further reduced to 60% on November 16 to repair the bearing.

The reactor tripped on November 19 at 0411 hours0.00476 days <br />0.114 hours <br />6.795635e-4 weeks <br />1.563855e-4 months <br />.from 60% power {

on a Feed Flow / Steam Flow mismatch on #24 steam generator. This condition waa caused when #22 steam generator feed pump tripped due to low suction pressure. #21 condensate pump was r eturned to service after strainer cleaning and had not been completely primed. ,

An air void was consequently pumped to the fced pump causing the low suction pressure condition.

Power reductions to 73% and 75% occurred on November 21 and November 23 respectively due to three circulators being out of service for screen problems and condensor tube leaks.

l Page 19 of 20

4 REFUELING INFORMATION Docket No. 50-311 Unit Name Salem #1 Date Dec. 10, 1982 Completed by L. K. Miller Telephone 609-935-6000 Extension 4455 Month November 1982 1

1 1. Refueling information has changed from last month:

l YES X NO

2. Scheduled date of next refueling: January 22, 1983
3. Scheduled date for restart following refueling: May 29, 1983
9. A. Will Technical Specification changes or other license amendments be required?

l YES X NO l

NOT DETERMINED TO DATE B. Has the reload fuel design been reveiwed by the Station Operating Review Committee? YES NO X If no, when is it scheduled? January 1983 1

5. Scheduled date (s) for submitting proposed licensing action: f January 1983, if required
6. Important licensing considerations associated with refueling: l NONE
7. Number of Fuel Assemblies:

A. Incore 193 B. In Spent Fuel Storage 0

8. Present licensed spent fuel storage capacity: 1170 Future spent fuel storage capacity: _1170
9. Date of last refueling that can be discharged to spent fuel pool assuming the present licensed capacity: March 2000 8-1-7.R4 Page 20 of 20
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