ML20066D859

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Monthly Operating Rept for Aug 1981
ML20066D859
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 09/02/1981
From: Campbell D, Might M, Svensson B
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
Shared Package
ML20066D853 List:
References
NUDOCS 8211120317
Download: ML20066D859 (7)


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...., PERATING DATA R.EPORT O

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.s 50-315 DOC:~.IT NO.

DATE 922-81 1

COstPLETED EY M.A. Miaht TELEP.$icyg 616-m -%901 OPE?aTING STATUS Donald C. Cook 1 N#5:8 g, g,;, y,,,..

August 1981 3250 _

2. Reportug Pe. oc:
3. U:s=sedThe:=21 Power (MW:):

1089

4. Nr.. eplat R:dn;(Gross MWe): -

I"#

5. Desigs Se==i=1 R dn2(Net MWe):

IORO

6. M-4,t=: Depend:ble Capci:y (Gross MWe):

1044

7. Maxi==m Dep=dshie C:pci:y (Nec MWe):

S. If Chseges Oc: urin Capci:y F++gs (Ite=s Nu=ther 3 Through 7) Sia== Last Report. Give R: sons:

9. Power Level To Which Res:==:-,If Any (Net MWe):

4

10. Reasons For R:s=i: dens.If Any:

This Month Yeao-Date Cu=u!:dve 744 5,831 58,439

11. Hou:s != Repor:iss Period 730 4,178._1 43.699.1
12. Nue.ber of Hou:s Rector Wss C:!:f=1 0

0_

463

13. Re:c:or Rese:ve Shu:down Ho=s 65/.3 4,095.7 42,652.8
14. Hours Gene = tor on.Line 0

0 321

15. Unic R. serve Shutdown Hot =s 1,790,135 12.862,987 122.089.992
16. Cross The:=21 E=e::y Ce=ented (MWM) 579,000,_,

4,277,760 40.133,420

17. Gross Se==i=l Ese:;y Cec-rz:ed G.tWH) 555,230 4,127,275 38,586,416
18. Net E.=:i=1 E== ;y Gene =:ed C.tWE) 88.3 70.2 75.8
19. Unit Service F:c:or 88 3 70.2 75.8
20. Unit Av ilsbi!I:y F.cror 71.5 67.8 67.7
21. Unit C:pcity 7:c:or (Usi=: MDC Net) 70.8 67.2 63.9
22. Unit Capcity. :::or (Using DER Nett 1.0

.6 6.3

23. Unic Forced Cu:sge Rate
24. Shutdowns Scheduled Over Nex: 6 Mon:ts (Type. Date. :n:i Du= don of E:chl:

Maintenance shutdown scheduled for December 1981 for tw'o weeks.

25. If Sht: Dowrt At End Of Report Period. Esti=: red D:te of Sc2::np:

Foreest Achieved

. 25. Units la Tes: S::::s (Prior to Ce==e:cial Oper::ioni:

INITIA L CRIT!CA UTY INITIAL E:.ECTRIC: Y CO.*.I.*.i ERC:A:. O?ET.A TION psi ~7 s t'211120317 810914

~ l PDR ADOCK 05000315 R

PDR

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.

50-315 UNIT 1

DATE 9-2-81 COMPLETED BY Ann Might TELEPHONE 616-465-5901 MONTH August 1981 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWE-Net)

(MWe-Net) 1 0

17 1015 2

0 18 1035 3

0 19 1031 4

164 20 1035 5

430 21 1023 1011 6

430 22 7

277 23 1034 8

413 24 1032 9

436 25 1021 10 636 26 1033 11 636 27 1032 12 766 28 1031

~

13 870 29 1019 14,

920 30 1031 15 748 31 1029 16 996 l

INSTRUCTIONS On this fonnat list the average daily unit power level in MWe-Net for each day in the recorating sosth.

Cemmte to the searast whole mon 22-

UNITSilUTDOWNS AND POWER REDUC 110NS I)OCKET NO. 50-315 UNIT N AhlE D.C. Cook - Unit 1 DATE 9-14-81 REPORT hlONTil August, 198]

COhlPLETED iiY B. A. Svensson 1ELEPil0NE (616) 465-5901 PAGE 1 of 2 "t.=

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$ h"}d Licensee

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Cause & Correceive No.

Date Q

5 ij j sc Event 3,3 gU3 At. tion to fE jgg itepor: #

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Prevent Recuitence g

c5 171 810529 S

78.2 B&C 1

N.A.

ZZ ZZZZZZ The unit was removed from service at Cont'd 2259 hours0.0261 days <br />0.628 hours <br />0.00374 weeks <br />8.595495e-4 months <br /> on 810529 for scheduled Cycle V-VI refueling and maintenance outage.

Following completion of the outage work and low power physics test-ing the unit was returned to service at 0614 hours0.00711 days <br />0.171 hours <br />0.00102 weeks <br />2.33627e-4 months <br /> on 810804. The total length of the outage was 1591.2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />.

172 810804 S

1.7 B

1 N.A.

ZZ ZZZZZZ Unit removed from service for turbine overspeed testing.

173 810807 F

6.8 G

3 N.A.

ZZ ZZZZZZ Reactor / Turbine trip from 48% reactor power.

Reactor tripped from pressur-izer High Level because Channel NLP-153 was inadvertently valved out with Channel NLP-152 in trip for calibra-tion.

2/3 trip logic. The reactor was.taken critical and the unit paral-leled the same day. 48% reactor power was reached on 810808 and the power asconsinn nrnaram cnntinnori.

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3 4

1:: Fmeed Reason:

hicilmd:

linhibit G Instinctions S: Scheduleil A Equipmens Failme(Explain) 1 -klanual for Preparation of Data ll klaintenance of Test 2 hfanual Scram.

Entry Shecis fm I.icensee C. Refueling 3 Autmnatic Scram.

Event Report (i.ER) File INtiltEG-D Itegulaimy Restriction 4-Other (Explain) 0161)

'E Operator fraining & License Examinallon F Administrative 5

G. Operational linor (Explain) lishibit ! Same Somce I'l/77)

Il Other (Explain) s

DOCKET No. 50-315 UNITSiluTDOWNS AND POWER REDUCTIONS UNIT NAnlE D.C. Cook - Unit 1 DATE 9-l4-81 REPORT A10NTil August, 1981 COMPLETED HY B. A. Svensson TELEPil0NE (616) 465-5901 PAGE 2 of 2

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j.$ 3 Licensee g

f, Cause & Courecilve No.

1) ate Q

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js5 Even 3,7 gU3 Ai.liam so fE j gy, g iteportsi un U Prevent Recurrence H

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174 810814 F

0 H

4 81-033/0lT-0 EB SUP0RT Started a power reduction from 97%

power to 60% due to an engineering re-view indicating that the safety-related 4KV power busses had.not been ade-quately supported for their seismic class.

60% power was reached at 0254 hours0.00294 days <br />0.0706 hours <br />4.199735e-4 weeks <br />9.6647e-5 months <br /> on 810815. At 0825 the seismic supports were temporarily repaired and power increase to 97% started. 97%

power was reached at 0215 on 810816 and 100% power was reached for the first time in Cycle VI at 1403 hours0.0162 days <br />0.39 hours <br />0.00232 weeks <br />5.338415e-4 months <br /> on 810817, 1

2 3

4 F: Fmced Reason:

hicilmd:

Exhible G -Instructi.ms S: Scheiluleil A lialuipment Failure (lixplain) 1 -Maimal for Preparation of Data ll Maintenance of Tess 2 Manual Scram.

Entry Sheels fm 1.icensee C Refueling 3 Aulomatic Scram.

Evens Repmt (1.!!R) File iNDIll.'G-D. Regulatory Resiricilon 4-Other (Explain) 0161)

I!-Operator Training & License lixaminallon F Ailministrative 5

G. Operational linor ilixplain) lixhible I Same Somce I'l/77)

Il Olher (lixplain) i

Docket No.: 50-315 Unit Name:

D. C. Cook Unit #1 Completed By:

D. R. Campbell Telephone:

(616) 465-5901 Date: September 14, 1981 Page:

1 of 1 MONTHLY OPERATING ACTIVITIES - AUGUST, 1981 Highlights:

The Unit entered this period in Mode Three following refueling.

The reactor was made critical at 0854 hours0.00988 days <br />0.237 hours <br />0.00141 weeks <br />3.24947e-4 months <br />, August 1,1981. This was the beginning of the Physics Testing.

Unit was paralleled at 0614 hour0.00711 days <br />0.171 hours <br />0.00102 weeks <br />2.33627e-4 months <br />, August 4,1981. At 1847 hours0.0214 days <br />0.513 hours <br />0.00305 weeks <br />7.027835e-4 months <br />, August 4,1981, Unit removed from service for overspeed testing.

2028 hours0.0235 days <br />0.563 hours <br />0.00335 weeks <br />7.71654e-4 months <br />, August 4,1981 the Unit was again paralleled.

At 1517 hours0.0176 days <br />0.421 hours <br />0.00251 weeks <br />5.772185e-4 months <br />, August 7,1981 the Unit tripped from pressurizer high level because channel NLP-153 was inadvertantly valved out with NLP-152 in trip for calibration. The trip was from 48% power.'

The reactor was made critical the same day, paralleled at 2205 hour0.0255 days <br />0.613 hours <br />0.00365 weeks <br />8.390025e-4 months <br /> and power physic tests were continued.

August 14,1981 at 1800 hour0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br />, a power reduction was started due to an engineering review indicating that the safety related 4 KV power busses had not been adequately supported for their seismic class.

Sixty percent power was reached at 0254 hour0.00294 days <br />0.0706 hours <br />4.199735e-4 weeks <br />9.6647e-5 months <br />, August 15, 1981. At 0825 hours0.00955 days <br />0.229 hours <br />0.00136 weeks <br />3.139125e-4 months <br /> the seismic supports were temporarily repaired and a power increase started. Reactor power was at 100% at 1403 hours0.0162 days <br />0.39 hours <br />0.00232 weeks <br />5.338415e-4 months <br />, August 17, 1981. The Unit operated at s100% power for the remainder of the month, except for a short period of time at 90% power to test turbine valves.

Generation:

579,000 MWH.

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A, DOCKET N0.

50 - 315 UNIT NAME D. C. Cook - Unit No. 1 DATE 9-14-81 COMPLETED BY B. A. Svensson TELEPHONE (616) 465-5901 PAGE 1 of 2 MAJOR SAFETY-RELATED MAINTENANCE AUGUST, 1981 M-1 Inspected the seals on No. 4 reactor coolant pump.

Replaced the No. 3 seal and the No. 1 seal insert.

M-2 A vent valve at the top of No. 3 steam generator, MS-106-3 had a packing leak.

The leak was sealed by Furmanite injection M-3 Disassembled No.1 through No. 4 steam generator stop valves, MRV-210, 220, 230 and 240 and replaced all upper and lower disc guide studs.

Reassembled valves and had the valves tested.

M-4 No. 3 steam generator stop valve dump valve, MRV-232 was leaking by.

Replaced the valve stem and plug.

Lapped the plug to the seat.

Re-packed the valve and had it tested.

M-5 The inner door of the containment personnel airlock on the 612' elevation had a broken interlock cable.

Replaced the cable and tested the door.

M-6 The tapered pin on the 1AB diesel fuel rack assembly at the bell crank shaft was worn and bent.

Replaced the tapered pin and retested engine.

C&I-l MRV-233, steam generator No. 3 power operated relief valve would open approximately 4% when the controller was in the auto mode and not re-quired.

The controller's calibration was tested and the setpoint dial was found out of specification.

The setpoint dial was adjusted to the correct value and proper operation of the controller was verified.

C&I-2 A 4% difference was indicated on the pressurizer level protection set indication in the control room. The reference leg of NLP-151, pro-tection channel No.1 was filled. The indication returned to the cor-rect value.

C&I-3 Annunciator 11 Drop 6, 'Tavg High' was received with Tavg at approxi-mately 561.5 F.

The alarm module's calibration was tested and found to be out of specification. The module was recalibrated'and returned to service.

C&I-4 IPA-131, accumulator No. 3 control room indication failed. The instru-ment loop was tested and a fuse was found blown in the loop's power supply.

The fuse was replaced. The test point voltage was measured at 1.7 volts with the normal maximum being 0.5 VDC. The problem was iden-tified as a shorted feed-through in the penetration. The circuit was changed to a different penetration and correct operation of the instru-ment loop was verified.

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DOCKET NO.

50 - 315 UNIT NAME D. C. Cook - Unit No. 1 DATE 9-14-81 COMPLETED BY B. A. Svensson TELEPHONE (616) 465-5901 PAGE 2 of 2 MAJOR SAFETY-RELATED MAINTENANCE AUGUST, 1981 C&I-5 Annunciator.9 Drop 23, north boric acid storage tank high temperature alarm was received in the control room. The temperature transmitter, 0

0 QTC-410 indicated 170 F at the transmitter and 175 F at the control room panel.

The alarm bistable's calibration was tested and the high alarm setpoint was found to be 1.875% low. The bistable was recalibrated and returned to service.

The calibration of the transmitter was tested to detenmine the reason for the difference in indications. The process temperature point on the transmitter was found binding. The transmitter was within specifications and the pointer was freed.

Control Rods' Control Bank C Low Alarm was received with the rods at 228 C&I-6 and all associated RPI Channels indicating > 228. The insertion limit computer modules were tested.

ZY-4328 high limit was found out of spec-ification. The high limit was calibrated to the correct value and the low alarm was verified to actuate at 220 steps.

C&I-7 The 50' wind recorder paper drive was not working..The defective drive motor was replaced and all drive components checked.

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