ML20066D229

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Monthly Operating Rept for Sept 1982.Narrative Summary Encl
ML20066D229
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 10/06/1982
From: Eich E
CONSOLIDATED EDISON CO. OF NEW YORK, INC.
To:
Shared Package
ML20066D221 List:
References
NUDOCS 8211110239
Download: ML20066D229 (4)


Text

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1 OPERATING DATA REPORT DOCKET NO. 50-24 7 j DATE 1 n-6-99 COMPLETED 11Y /r _ ri +

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TELEPl!ONE 91 d c "-5155 OPERATING STATUS ,

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I. Unit Name: Indian Point Unit No. 7 Unit removed from service

2. Reporting Period:

Septem!'er 1982 __

27ga n 9/18/82 for the Cycle

3. Licenwd Thermal Power (MWt). 5/6 refueling and 1013

! 4. Nameplate Rating (Gross MWe): ### ~ ** " "^" #9'

( 5. Design Electrical Rating (Net MWe):

6. Maximum Dependable Capacity (Gross MWe):
7. Masimum Dependable Capacity (Net MWe):

I S. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Gise Reasons:

9. Power Lesel To hhich Restricted.lf Any (Net MWel:
10. Reawms For Restrictions.If Any:

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' This Month Yr. to-Date Cumulative 720 6551 .72336

11. Ilours in Reporting Period AR P .19 76.92 5773.65
12. Number Of Hours Reactor Was Critical 0 51.08 1578.51
13. Reactor Resene Shutdown Hours ,g g , g , ,
14. Hours Generator On Line 0 0 -

0

15. Unit Pesene Sht.tdown Hours
16. Gross Thermal Energy Generated (MWH) 617493 15177101 1?)416676 .

180610 466. W 37502726 17 Gross Electrical Energy Generated (MWH) ,_

1hJ 445F513 34743169

18. Net Electrical Energy Generated (MWH) '#*
19. Unit Senice Factor 87.4 64.8 37.6
20. Unit Availabili:s Factor 57.5 26.8 79.6

! 21. Unit Capacitv Factor IUsing MDC Net 1 78.n 56.6 26.1

22. Unit Capacity FactorIUning DER Net)
  • *3
23. Unit Forced Outage Rate
24. Shutdowns Scheduled Oser Next 6 Months (Type. Date,and Duration of Each :

I Unit presently shut down for refueling and maintenance

25. If Shut Down At End Of Report Period. Estimated Date of Startup: 12/23/82 2ti. Units in Test Status IPrior to Commercial Operationi: Forecast Achiesed l

INillT L CRITICALITY INill \1. FLI C1RICIIY \

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COsnit'RCIAL OPFR \l~lON \ N A*

i l 8211110239 821015 c6 4 PDR ADOCK 05000249 R PDR t -

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' AVERAGE DAILY UNIT POWER I.EVEL s

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DOCKET NO.

I.D. r'??TT 2 I~ 2 DATE COMPLETED BY 914-526-5155 TELEPlf0NE f

MONn! RPpTEMBER 1982

  • I DAY AVER AGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net) (MWe Net)

, 630 594

,7 393 o 2 18

, 0 3 19 0

0 4 20 0

0 t 5 21 o 0

6 22 0 7

0 0 f .

As 3 1Ao 24 0 524

, 25 0 1

' 10 26 0 663 1I 27 0 701 0 28 699 0 3

13 29 712 g l

14 30 l-708

\' l5 3I O 704 16 _

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INSTRUCTIONS l

i On this l'ormat.hst the ascrage dai!y unit power leselin MWe Net tior each da> in the repor m.c month. Compute to i

the nearest whole mepwatt.

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! (9I77) 4 1

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I UNil SHUlDOWNS AND POWER REDUCllONS I d K I I I M l- 50-247 i UNIINAME I.P. 11 nit 2 i D Al f 10-6-R2 1982 COMPLETEI) HY P _ Fie h ,

REPORT MONT![F T.

TELEPHONE 914-926-5155 h

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= re '": en 2 C l'ic#"s # C""'# A I"'" #

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I' x',' Da'#

h 3.I $ 5ix Event Report #

G mO Ation le l OO E yEjO . U o Present Recurrence O

, I 7 9/2/R2 F 137.03 A 1 82-038-03L SB Blower. Fan Cooler Unit Fan and Coupling Repairs

  • i 8 9/18/82 S 311.93 C 1 None XX XXXXXXX Refueling and Maintenance Out-

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i I 2 3 4 F: F uced Reason: Method: Exhibit G Instruttiaan S: Scheduled A l'quipment Failure (Esplain) 1 -Manual for Perparation ut Data B-Maintenance of Test 2-Manual Scram. Entry Shtets for I,isen.ee C Refuehng 1 Automatic Scram. Event Rep.nl 111 R t I !.-(Nt:RI G D-Regulatory Restriction 4-Other (Explain) 0161)

E-Operator Traming & Ucense Examinati m F-Admmist rative e 5 G-Operation.d Eirar (Explain) / Exhibis 1 - Same Sourse Pt!77) Il-Othec (Explain) ,  ;

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SUMMARY

OF OPERATING EXPERIENCE Docket No. 50-247 Date: 10/7/82 Completed By: J. Curry Telephone: (914) 526-5235 Indian Point Unit No. 2 began the month at 85% power. On Thursday, September 2 an inspection of No. 24 fan cooler unit (FCU) revealed damage to the motor / fan coupling and the fan shaf t bearings. A controlled plant shut-down was initiated at 12:00 noon, ard the unit was renoved frcen service at 6:10 P.M. that same day. On Friday, Septenber 3,1982 the Company requested and was granted a temporary change to the facility Technical Specifications by the NRC. This change extended the time limit for operation at hot shutdown conditions until 11:59 P.M. Tuesday, September 7 while repairs to No. 24 FCU were being made. Unit No. 2 was returned to service at 11:12 A.M. on Wednesday, September 8 following completion of maintenance on Nos. 21 and 24 fan cooler units.

Reactor power was maintained at 70% until September 16 when a load reduction was initiated while boron concentration was adjusted in the No. 22 Boric Acid Storage Tank. The load reduction was terminated in one hour.

From September 10 until September 17 the unit remained at approximately 90% power. It was removed from service at 12:04 A.M. on Saturday, September 18 for the Cycle 5/6 refueling and maintenance outage. System cooldown was initiated Saturday and cold shutdown conditions were reached on Monday, September 20, 1982.

On September 24 the RCS was borated to the refueling concentration. Reactor coolant cleanup was completed on September 29. The system was then depressurized and drained in preparation for reactor vessel head removal and steam generator eddy current inspections.

All three low pressure turbine spindles were removed from their respective inner cylinders and grit blasted in preparation for inspection of the blading and discs. Work was initiated on the replacement of all six moisture separator reheater tube bundles.

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