ML20066D096

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Monthly Operating Repts for Sept 1982
ML20066D096
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 10/01/1982
From: Schmitendorf G
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
Shared Package
ML20066D086 List:
References
NUDOCS 8211110151
Download: ML20066D096 (8)


Text

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VIRGINIA ELECTRIC AND POWER COMPANY NORTH ANNA POWER STATION MONTHLY OPERATING REPORT ,

MONTH September YEAR 1982 APPROVED:

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STATIONMANAGERf 8211110151 821013 PDR ADOCK 05000338 R PDR

OPERATING DATA REPORT DOCKET NO. 50-333 DATE 10-01-82 COMPLETED BY G. D. Schmitendorf TELEPHONE (703) 894-5151 X2502 OPERATING STATUS Notes

1. Unit Name: North Anna 1
2. Reporting Period: September 1982
3. Licensed Thermal Power (MWt): 2775
4. Nameplate Rating (Gross MWe): . 947
5. Design Electrical Rating (Net MWe): 907
6. Maximum Dependable Capacity (Gross MWe): 918
7. Maximum Dependable Capacity (Net MWe): 865
8. If Changes Occur in Capacity Ratings (Items No. 3 thru 7) Since Last Report,~Give Reasons:

NA

9. Power Level To Which Restricted, If Any (Net MWe): N/A
10. Reasons For Restrictions, If Any: N/A This Month Yr.-to-Date Cumulative
11. Hours In Reporting Period 720 6,551 37,872
12. Number of Hours Reactor Was Critical 0 3,129.9 26,958.2
13. Reactor Reserve Shutdown Hours 0 21.5 256.4
14. Hours Generator On-Line 0 3,022.9 26,375.9
15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Thermal Energy Generated (MWH) 0 7,941,328 68,255,580
17. Gross Electrical Energy Generated (MWH) 0 2,537,888 21,783,410
18. Net Electrical Energy Generated (MWH) 0 2,396,973 20,519,889
19. Unit Service. Factor 0 46.1 69.6
20. Unit Availability Factor 0 46.1 69.6
21. Unit Capacity Factor (Using MDC Net) 0 42.3 62.6
22. Unit Capacity Factor (Using DER Net) 0 40.3 59.7
23. Unit Forced Outage Rate 0 7.3 5.1
24. Shutdowns Scheduled over Next 6 Months (Type, Date, and Duration of Each):
25. If Shut Down At End Of Report Period, Estimated Date of Startup: 11-09-82
26. Units In Test Status (Prior to Commercial Operation):

Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION -

UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-338

UNIT NAME North Anna 1 i DATE 10-01-82 REPORT MONTH September COMPLETED BY G. D. Schmitendorf TELEPHONE (703) 894-5151 X2502 2

No. Date Type Duration Reason Method of Licensee System Component Cause & Corrective (llours) Shutting 3

vent Code 4

Code 5

Action to Down Reactor Report # Prevent Recurrence 82-10 S 720 The scheduled refueling cutage continues 1 2 3 4 F: Forced Reason: Method: Exhibit F - Instructions

, S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data i

B-Maintenance or Test 2-Manual Scram. Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (LER) File D-Regulatory Restriction 4-Continuations (NUR).)-0161)

E-Operator Training & License Examination 5-Load Reduction F-Administrative 9-Other 5 G-Operational Error (Explain)

H-Other (Explain) Exhibit H - Same Source

r 1 1

i Page- 1 of I l l

UNIT SHUTDOWN AND POWER REDUCTIONS EXPLANATION SHEET DOCKET NO. 50-338 l

REPORT MONTH September UNIT NAME NA-1 YEAR 1982 DATE 10-01-82 COMPLETED BY G. D. Schmitendorf NO ENTRIES THIS MONTH

r. , , _

.n., ., . _ . , , _ , , . . _ . _n., , ,

m OPERATING DATA REPORT DOCKET NO. 50-339 DATE 10-01-82 COMPLETED BY G. D. Schmitendorf TELEPHONE (703) 894-5151 X2502 OPERATING STATUS Notes

1. Unit Name: North Anna 2
2. Reporting Period: September 1982
3. Licensed Thermal Power (MWt): 2775
4. Nameplate Rating (Gross NWe): 947
5. Design Electrical Rating (Net MWe): 907
6. Maximum Dependable Capacity (Gross MWe): 939
7. Maximum Dependable Capacity (Net MWe): 890
8. If Changes Occur in Capacity Ratings (Items No. 3 thru 7) Since Last Report, Give Reasons:

NA

9. Power Level To Which Restricted, If Any (Net MWe): N/A
10. Reasons For Restrictions, If Any: N/A This Month Yr.-to-Date Cumulative
11. Hours In Reporting Period 720 6,551 15,743
12. Number of Hours Reactor Was Critical 693.4 2,886 10,300.8
13. Reactor Reserve Shutdown Hours 29.8 388.6 2,021.8
14. Hours Generator On-Line 690.2 2,798.7 10,258.1
15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Thermal Energy Generated (MWH) 960,712 6,073,698 24,856,539
17. Gross Electrical Energy Generated (MWH) 626,330 2,319,920 8,629,152
18. Net Electrical Energy Generated (MWH) 595,585 2,190,997 8,193,413
19. Unit Service Factor 95.9 42.7 65.2
20. Unit Availability Factor 95.9 42.7 65.2
21. Unit Capacity Factor (Using MDC Net) 92.9 37.6 58.5
22. Unit Capacity Factor (Using DER Net) 91.2 36.9 57.4
23. Unit Forced Outage Rate 4.1 33.9 23.2
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

None

25. If Shut Down At End Of Report Period, Estimated Date of Startup:
26. Units In Test Status (Prior to Commercial Operation):

Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION

c.

AVERAGE DAILY UNIT POWER LEVEL

. DOCKET NO. 50-339 UNIT NA-2 DATE 10-01-82 COMPLETED BY G. Schmitendorf TELEPHONE 703-894-5151X2502 MONTH September DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 797 17 882 ,

2 876 18 878 3 878 19 869 4 876 20 823 5 879 21 696 6 881 22 0 7 880 23 631 8 882 24 878 9 885 25 872 10 879 26 874 11 874 27 821 12 886 28 859 13 881 29 880 14 878 30 867 15 878 31 16 881 INSTRUCTIONS On this format, list the average daily unit power level in MWe-fiet for each '

day in the reporting month, Compute to the nearest whole megawatt.

i

UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-339 UNIT NAME North Anna 2 DATE 10-01-82 REPORT MONTH September COMPLETED BY G. D. Schmitendorf TELEPHONE (703) 894-5151 X2502 Type Duration Reason2 l

Nc. Date Method of Licensee System Component Cause & Corrective (Hours) Shutting vent da Code Action to 3 4 5 Down Reactor Report # Prevent Recurrence 82-15 820921 F 29.8 A 1 NA NA NA Repair of Steam Generator FW PP Recirc Valve 2-FW-250C 82-16 820927 F NA A 1 NA NA NA Repair of steam generator feedwater control valve l

f 1 2 3 4 F: Forced Reason: Method: Exhibit F - Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram. Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (LER) File D-Regulatory Restriction 4-Continuations (NUREG-0161)

E-Operator Training & License Examination 5-Load Reduction F-Administrative 9-Other 5

, G-Operational Error (Explain)

. H-Other (Explain) Exhibit H - Same Source

Page 1 of 1 UNIT SHUTDOWN AND POWER REDUCTIONS EXPLANATION SHEET DOCKET NO. 50-339 REPORT MONTH September UNIT NAlfE NA-2 YEAR 1982 DATE 10-01-82 COMPLETED BY G. D. Schmitendorf 4

82-15 (A) (1) At 1800 on September 21, 1982 with the unit at 100% power a rampdown to Generator off line was commenced. The Generator was taken off line and Control Banks driven to zero steps.

The reactor was suberitical and maintained in Mode 3 (Hot Standby). Feed Pump Recire Valve 2-FW-250C required repair due to an excessive leak. In order to isolate and repair no recirc path would be available for the Main Feed Pumps.

The unit was brought off line and the repairs made in approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, at which time the unit was returned to power (Generator on line) at 0333 on September 23, 1982.

82-16 (A) (5) At 2015 on September 27, 1982 commenced power reduction to 32 percent power to allow repair of "B" feedwater control valve.

Bypass feedwater control valves were used while repairs were made to normal feedwater control valve pneumatic control system.

Repairs were successful and unit was returned to power, reaching 100 percent at 0300 on September 28, 1982.

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