ML20064C696

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Responds to NRC Ltr Re Violations Noted in Insp Repts 50-528/93-48,50-529/93-48 & 50-530/93-48.Corrective Actions: Night Order Issued Detailing Specific Interim Controls to Be in Place When RCS Level to Be Reduced
ML20064C696
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 02/01/1994
From: Conway W
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
102-02810-WFC-B, 102-2810-WFC-B, NUDOCS 9403100168
Download: ML20064C696 (12)


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Arizona Public Service Company P O DOX 53949

  • PHOENIX ARIZONA 85072 4 999 WILLIAM F CONWAY m eumgs-February 1,1994 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Mail Station P1-37 Washington, D. C. 20555 -

Reference:

Letter dated January 5,1994, from C. A. VanDenburgh, Acting Deputy Director, Division of Reactor Safety and Projects, NRC, to W. F. Conway, Executive Vice President, Nuclear, APS

Dear Sirs:

Subject:

Palo Verde Nuclear Generating Station (PVNGS)

Units 1,2, and 3 Docket Nos. STN 50-528/529/530 Reply to Notice of Violations 50-528/93-48-05 and 50-529/93-48-02 File: 94-070-026 Arizona Public Service Company (APS) has reviewed NRC Inspection Report 50-528/529/530/93-48 and the Notice of Violations dated January 5,1994. Enclosure 1 to this letter is a restatement of the Notice of Violations. APS' responses are provided in 1

APS shares the NRC's concern with regard to the implementation of operational controls.

APS has been working to improve the control of plant evolutions, and progress is being made as evidenced by the recent, mid-loop operation evolutions in Units 2 and 3. In addition, APS has targeted overall human performance as one of several strategic areas that will be the focus of intense improvemer,t initiatives. Other strategic areas being addressed include Culture and Training. All of these areas are closely linked, and actions developed for the Culture, Human Performance, and Training Strategies will directly contribute to enhancing operator performance. Proposed actions include assessments of supervisory / managerial skills; implementation of cultural expectations through the Performance Enhancement Program; simplification of processes and procedures; implementation of a performance analysis and trend program which would include a requirement for functional areas to employ self-assessment programs; reassessment of Training Program ownership; Training to customer and customer to Training job rotations, and inclusion of High Intensity Training in the Ucensed Operator Requalification Program.

Optimal operator performance is a major goal of APS' strategic planning.

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U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Reply to Notice of Violations 50-528/93-48-05 and 50-529/93-48-02 Page 2 Both the cited and non-cited violations discussed in the referenced letter and the Inspection Report have been addressed through the APS Positive Discipline Program.

Should you have any questions, please call Burton A. Grabo at (602) 393-6492.

Sincerely, J7{

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WFC/ BAG /PJC

Enclosures:

1.

Restatement of Notice of Violations 2.

Reply to Notice of Violations cc:

K. E. Perkins, Jr.

K. E. Johnston l

B. E. Holian

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ENCLOSURE 1 RESTATEMENT OF NOTICE OF VIOLATIONS l

50-528/93-48-05 AND 50-529/93-48-02 NRC INSPECTION CONDUCTED NOVEMBER 2 THROUGH DECEMBER 6,1993 l

Restatement of Notice of Violations 50-528/93-48-05 and 50-529/93-48-02 During an NRC inspection conducted on November 2 through December 6,1993, two violations of NRC requirements were identified.

In accordance with the " General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, j

Appendix C, the violations are listed below:

A.

Unit 1 Technical Specification 6.8.1 requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Appendix A of Regulatory Guide 1.33, February 1988.

Regulatory Guide 1.33, Appendix A, requires, in part, that procedures be prepared for operation of safety-related systems.

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Normal operating procedure 410P-1 ZZ16,"RCS Drain Operations," Step 5.3.7.5(3),

requires operators to monitor reactor coolant system level while draining.

Contrary to the above, on November 3,1993, operators in Unit 1 failed to monitor i

reactor coolant system level while draining for approximately eight minutes.

This is a Severity Level IV violation (Supplement I) applicable to Unit 1.

B.

Unit 2 Technical Specification 6.8.1 requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Appendix A of Regulatory Guide 1.33, February 1988.

Regulatory Guide 1.33, Appendix A, requires,in part, that procedures be prepared for operation of safety-related systems.

Normal operating procedure 420P-2CH01,"CVCS Normal Operations, " Step 7.3.4, requires the controller for valve CHN-210X to be returned to automatic following reactor coolant system dilution evolutions.

Contrary to the above, on November 23,1993, in Unit 2, the controller for valve CHN-210X was not returned to automatic following a dilution evolution.

This is a Severity Level IV violation (Supplement I) applicable to Unit 2.

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i ENCLOSURE 2 i

a REPLY TO NOTICE OF VIOLATIONS a

1 50-528/93-48-05 AND 50-529/93-48-02 i

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NRC INSPECTION CONDUCTED NOVEMBER 2 THROUGH DECEMBER 6,1993 i

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REPLY TO VIOLATION A (50-528/93-48-05)

Reason For The Violation As discussed at the November 15, 1993, APS/NRC Status Meeting, APS management initiated an in-depth investigation in response to the Unit 1 inadvertent entry into reduced inventory during a partial Reactor Coolant System (RCS) draindown. The RCS was partially drained and being maintained at a level of 112 to 113 feet to support steam generator tube plugging activities while ensuring prevention of possible overpressurization of nozzle dams. Because of occasional (depending upon system alignment) safety injection boundary valve leakage from the refueling water tank, it was necessary for Unit 1 operators to reduce RCS level in accordance with procedure i

410P-1ZZ16 from three to six times per shift to maintain the required RCS level band.

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On November 3,1993, during the midnight shift, the operating crew was reducing RCS level and entered reduced inventory when the Refueling Water Level Indication 4

System indicated RCS level was being inadvertently lowered below 111 feet. The indicated level had reached a minimum of about 108 feet,5 inches when the operating crew stopped level reduction and initiated makeup to restore RCS level to 112 feet. The indicated level was below 111 feet for approximately six minutes.

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l The APS investigation revealed that at the time of the level reduction evolution, the Shift Supervisor was functioning in the capacity of Control Room Supervisor (CRS). The activities being performed were not excessive in number or significance, nor were there questions as to order of importance of those activities. There was no increased urgency to complete the actions which subsequently distracted the Primary Operator. During the initial performance of RCS level reduction on the day preceding the event, the CRS had conducted a detailed walk-through of the task with the Primary Operator and discussed the initiation of makeup flow as a contingency and the effects of connecting the reactor vessel head vent system on the RCS levelindicator response. The Primary Operator had then successfully completed the task approximately nine times over two operating shifts.

At approximately 0120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br />, the Primary Operator observed RCS level i

approaching the high end of the band being maintained. He announced to the control room at large that he was initiating RCS level reduction and began the activity in accordance with procedure 410P-1ZZ16. The third Reactor Operator acknowledged the announcement; then continued with other tasks. Neither the CRS nor the Secondary Operator acknowledged the Primary Operator's announcement, nor did the Primary Operator assure that he received an acknowledgement from the CRS. The Primary Operator then initiated draindown of the RCS level and immediately verified that the expected RCS level decrease was in progress. The Primary Operator began monitoring RCS level from a monitor located at the control board, but became distracted by other activities and left the monitor. As the Primary Operator was returning to the monitor, the Page 2 of 7

Secondary Operator, who had been engaged in a strategy discussion with the acting CRS, observed from the monitor that the RCS was decreasing below the desired level.

i The Secondary Operator immediately alerted the Primary Operator and the CRS of the need to initiate makeup flow to the RCS. The Primary Operator began restoration of RCS

't level, and at 0131 hours0.00152 days <br />0.0364 hours <br />2.166005e-4 weeks <br />4.98455e-5 months <br /> the indicated RCS level returned to > 111 feet exiting the reduced inventory status. RCS level was then stabilized at 112 feet,4 inches.

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l The primary cause of the event was the operating crew's diminished sensitivity to the safety significance of the RCS reduction evolution due to the task's lack of complexity and the frequency with which it was being performed. Control room supervision did not establish and maintain the expected communication standards nor exercise adequate control of a safety significant evolution.

4 APS' Nuclear Safety Assessment of the event determined that the actual RCS level reached a minimum of approximately 111 feet,8 inches which is above reduced inventory conditions. During RCS level draindowns, indicated level typically reads conservatively Iow due to the restriction of containment air flow into the reactor vessel through the reactor vessel head vent orifice. The Nuclear Safety Assessment results also confirmed that during the event the plant was not in a condition in which the core would have been uncovered or radioactive material released through the open containment hatch.

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l Corrective Steps That Have Been Taken And Results Achieved A night order was issued detailing specific interim controls that were to be in place when RCS level was to be reduced. The established controls included (1) designation of an operator to have responsibility to control and monitor the evolution; (2) a requirement to obtain permission from the CRS to perform RCS draindown, and (3) a requirement for the CRS to diredly supervise the evolution. The wide-range indicators for the Refueling Water Level Indication System were assigned to addressable trend recorders located near the board containing the RCS level controls.

The operating crew involved in the event was removed from shift to participate in l

l the investigation. The Unit 1 control room staff (operating crews) was briefed to apprise j

them of the event and the initial corrective actions. A Category 2 incident investigation was conducted.

l Corrective S eps That Will Be Taken To Avoid Further Violations i

t The operating crew involved in the event completed specialized High intensity Training (HIT) to improve teamwork and reinforce the expected communication practices.

Further, Unit 1 Operations management will review the HIT evaluations of the Unit 1 operating crews and assess the crews' performance on-shift to verify that they meet Page 4 of 7

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management's expectations for communication standards and teamwork. Completion i

of the assessment is expected by June 24,1994.

During mid-December 1993, the Unit 1, 2, and 3 Plant Managers provided a

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detailed review of the event to their respective operations departments / management with l

emphasis on the need for control of activities affecting key plant parameters and safety functions.

i The performance history of the shift supervision involved 'in the event was l

evaluated. Appropriate discipline was implemented for the individuals involved in the event in accordance with the APS Positive Discipline Program.

i As an enhancement to further sensitize operators to the significance of specific RCS partial drain activities, the Nuclear Training Department has revised the mid-loop 1

classroom instruction provided to them to discuss vulnerability to error and the need to minimize distractions in the control room during evolutions affecting RCS level.

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i Date When Full Compliance Will Be Achieved 5

Full compliance was achieved at 0131 hours0.00152 days <br />0.0364 hours <br />2.166005e-4 weeks <br />4.98455e-5 months <br /> when the Primary Operator restored i

RCS level to greater than 111 feet and exited the reduced inventory status.

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4 REPLY TO VIOLATION B (50-529/93-48-02)

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Reason For The Violation i

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The failure to retum the reactor makeup water-to-volume control tank valve l

controller, CHN-FIC-210X, to automatic following a

dilution operation on i

i November 23,1993, is attributable to personnel error in not complying with the applicable

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procedural requirements. The crew had performed repetitive dilutions during the shift i

and had been operating the controller in manual because at flow rates of less than 10 gpm, automatic controller operation tends to be unstable as noted in 42OP-2CH01, "CVCS Normal Operations."

Makeup to the Reactor Coolant System (RCS) was not j

required after the last dilution on that shift, and the controller was left in manual rather than being returned to automatic as required. It is management's expectation that the j

CVCS operations would have been closed out prior to shift turnover, and the controller 4

should have been returned to automatic in accordance with procedure 42OP-2CH01.

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Corrective Steos That Have Been Taken And Results Achieved l

As part of the APS evaluation, Unit 2 Operations management discussed operation of valve controller CHN-FIC-210X with each of the Unit 2 shift supervisors and determined

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that the operation of this controller is not a generic problem among the operating crews.

Unit 2 Operations management briefed each crew on this incident and reinforced management's expectations for procedural adherence. Appropriate positive discipline in i

accordance with the 'APS program was administered to the individual who was involved a

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Corrective Steps That Will Be Taken To Avoid Further Violations The corrective actions described above address the individual violation; however, f

as discussed in the cover letter for this response, PVNGS is in the process of developing l

and implementing broad scope improvements in several strategic areas. Many of the proposed improvements target human performance issues including those associated 1

with Operations personnel.

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i Date When Full Compliance Will Be Achieved I

Full Compliance was achieved when the valve controller was returned to automatic by the oncoming operating crew.

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