ML20062K000

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Notice of Violation from Insp on 820426-0525
ML20062K000
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 06/03/1982
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20062J893 List:
References
50-259-82-15, 50-260-82-15, 50-296-82-15, NUDOCS 8208160520
Download: ML20062K000 (2)


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APPENDIX A NOTICE OF VIOLATION Tennessee Valley Authority Docket Nos. 50-259, 260, & 296 Browns Ferry 1 2, and 3 License Nos. DPR-33, 52, & 68 As a result of the inspection conducted on April 26 - ttay 25,1982, and in accordance with the NRC Enforcement Policy, 47 FR 9987 (March 9,1982), the following violations were identified.

A.

10 CFR 50.59 requires that the licensee maintain records of changes in the facility and that records shall include a written safety evaluation which provides the bases for the determination that the change does not involve an unreviewed safety question.

Contrary to the above, the requirement that a written safety evaluation be made was not met in that the off-gas post-treatment sampling station configuration was modified by the addition of a temporarily installed sample pump without a safety evaluation being performed.

The off-gas sampling station is described in figure 7.12-2a of the Final Safety Analysis Report.

This is a Severity Level IV Violation (Supplement I.D.1) and pertains to all three units.

B.

Technical Specification 4.8.B.1.a requires that for effluent streams having continuous monitoring capability, the activity and flow rate shall be monitored and recorded to enable release rates of gross radioactivity to be determined on an hourly basis.

Contrary to the above, the requirement that effluent streams having continuous monitoring ca. ability have the activity monitored on an hourly c

basis was not met in that the inspectors detennined that the sampling line for the turbine building exhaust ventilation going to Continuous Air Monitor (CAM) had accumulated water (approximately two cups) obstructing the sample fl ow.

The sample line had been blocked by water accumulation for an 4

undetermined amount of time. The licensee had previously identified that this line has a tendency to accumulate water and had replaced the sample l

pipe with clear plastic hose to aid in determining water accumulation; l

however, no specified frequency was established to determine moisture build up.

This is a Severity Level V Violation (Supplement IV.E.) and is applicable to l

Unit 2.

C.

Technical Specification 6.3 requires that detailed written procedures shall be adhered to, reviewed by the Plant Operating Review Committee (PORC) and approved by the Plant Superintendent.

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Tennessee Valley Authority 2

Docket Nos. 50-259, 260, & 296 Notice of Violation License Nos. DPR-33, 52, & 68 Contrary to the above, the requirement that procedures be adhered to, reviewed by PORC and approved hy the Plant Superintendent was not met in tha t:

1.

The procedure used to perform the weekly off-gas post treatment analysis, required by Technical Specification (TS) 4.8.B.3, Radiochemical Laboratory thnual (RLli) procedure 7098, was not of.the current revision.

2.

The procedure used to perform the weekly sensor check of waste gas monitors, required by TS 4.8.B.4, Rui procedure 741, was not reviewed by PORC or approved hy the Plant Superintendent.

3.

The procedure being used for inspection of new fuel, General Operating Instruction (G0I) 100-2, was not of the current revision, in that the data sheet being used to sign off inspection points had been superseded by a later revision.

This is a Severity Level V Violation (Supplement I.E.) and is applicable to all three units.

Pursuant to the provisions of 10 CFR 2.201, you are hereby required to submit to this office within thirty days of the date of this Notice, a written statement or explanation in reply, including:

(1) admission or denial of the alleged viola-tions; (2) the reasons for the violations if admitted; (3) the corrective steps which have been taken and the results achieved; (4) corrective steps which will be taken to avoid further violations; and (5) the date when full compliance will be achieved.

Consideration may be given to extending your response time for good cause shown.

Juh 0 31982 Da te:

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