ML20062H559
| ML20062H559 | |
| Person / Time | |
|---|---|
| Site: | Hatch |
| Issue date: | 08/10/1982 |
| From: | Eazzetta B GEORGIA POWER CO. |
| To: | |
| Shared Package | |
| ML20062H554 | List: |
| References | |
| NUDOCS 8208160094 | |
| Download: ML20062H559 (13) | |
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UNIT SIlUTDOWNS AND POWER REDUCil0NS UNIT N AME DATE 8-M COMPLETED !!Y R.A. Ea779tta July REPORT MONT11 TELEPfl0NE OI? %7-7851 i
"E Lic nsee g't h,g E
Cause & Corrective
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Date E
Event
-2 oo Action to
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$~c sE jsy Report #
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Prevent Recurrence b
I 82-37 820703 F
202.6 A
3 IB lilSTRU h scram due to false hign rx. pressure indica tion.
.[
82-38 820711 F
14.5 A
5 IB IrlSTRU Power ramp fiom above scram REC. !!B -
Unit offline due to high H2 content in 0
82-39 820712 F
9.0 H
1 MB offgas-82-40 820713 F
11.6 H
5 MB RECOMB Ramp froin above reduction L
82-41 820713 5
4.2 8
5' CC' VALVEX Power hold due to relief valve testing f
82-42 820713
.F 11.5. A 5
CH HTEXCH Power ' reduction due to steam leak in f.
[
Ramp from above power reduction 82-43 820713 F
72.0 A
5 CH HTEXCH
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Exhibit G Instructions
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.F: Forced Reasim:
A L uipment Failure (Explain) 1 Manual for Preparation of Data S: Scheduled i
[14f aintenance of Test 2-Manual Scram.
Entry Sheets for Licensee 3 Automatic Scram.
Even. Report (LERI File (NUREG-I C-Refueling D Regulatory Restriction 4 -Continuations 0161)
E Operator Training & Ucense Examination 5-Icad Peduction j
'3 F-Administrative 9-Other (Explain)
Exhibit'I-Same Source G-Operational Error (Explain)
(9/77)
Ilother(Explain) 5 h
9
I DOCKET Wo.
UNIT SIIUTDOWNS AND POWER REDUCTIONS UNIT N A%1E 0-4-6' DATE
'd Z 4e L Ld COMPLETED BY July
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NO E U Prevent Recurrence H
5 u
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I 82-44 820716 F
5.2 A
5 CG VALVEX Power reduction due to faulty rx water cleanup valve f
1 82-45 820718 F
49.7 A
2 CG VALVEX Rx. scram to repair rx. water cleanup 1
valve 1
82-46 820719 F
-29.9 A
5
.CG VALVEX Ramp from above scram j,
82-47 820724 S
5.6 H
5 RC C0tlROD Power reduction to perform rod pattern
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adjustment' & weekly turbine test i
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82-48 820725 S
44.8 H
5 RC COUROD Ramp from above reduction 82-49 820730 S
2.0 B
5 RC CONROD Power. reduced for rod pattern adjust-ment & weekly turbine test
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Exhibit G Instructions i
F: Forced Reason:
5: Scheduled A. Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram.
Entry Sheets for Licensee 3 Automatic Scram.
Event Repori(LER) File (NUREG-C Refueling D Regulatory Restriction 4 -Continuations 0161) i E-Operator Training & Ucense Examination 5-Ioad Beduction 3
F Administrative 9 @ar (Explain)
Exhibit I-Same Source l
G-Operational Error (Explain)
(9/77)
Ilother(Explain) t-
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NARRATIVE REPORT Date Unit 1 July 3 RX. scram on high RX pressure at 0736 hours0.00852 days <br />0.204 hours <br />0.00122 weeks <br />2.80048e-4 months <br />.
July 10 RX critical at 0920 hours0.0106 days <br />0.256 hours <br />0.00152 weeks <br />3.5006e-4 months <br />.
July 11 RX tied to line at 1826 hours0.0211 days <br />0.507 hours <br />0.00302 weeks <br />6.94793e-4 months <br />.
July 12 Power reduction due to high H2 content in off-gas at 0830.
July 12 Unit off line due to high H2 content in off-gas'at 0856 hours0.00991 days <br />0.238 hours <br />0.00142 weeks <br />3.25708e-4 months <br />.
July 12 RX tied to line at 1802 hours0.0209 days <br />0.501 hours <br />0.00298 weeks <br />6.85661e-4 months <br />.
July 13 Power hold due to steam leak in feedwater heater 0405 hours0.00469 days <br />0.113 hours <br />6.696429e-4 weeks <br />1.541025e-4 months <br />.
July 13 Power hold due to steam leak in feedwater heater 0946 hours0.0109 days <br />0.263 hours <br />0.00156 weeks <br />3.59953e-4 months <br />.
July 16 Power reduction to repair RX-water clean-up valve.
July 24 Power reduction for rod pattern adjustment at 2132 hours0.0247 days <br />0.592 hours <br />0.00353 weeks <br />8.11226e-4 months <br />.
July 24 Power reduction for weekly turbine test at 2300.
July 25 Weekly turbine test complete at 0311 hours0.0036 days <br />0.0864 hours <br />5.142196e-4 weeks <br />1.183355e-4 months <br />.
July 30 Power reduction for weekly turbine test and rod pattern adjustment at 2200.
July 30 Weekly turbine test and rod pattern adjustment complete at 2400 h'ours.
O
HATCH 1 SAFETY RELATED MAINTENANCE REQUESTS TO BE REPORTED FOR JULY 1982 Number Date Completed Description 81-4127 6-1-82 The off gas loop seals 1N62-A003 were modified.(Per DCR-80-159) 82-3043 6-3-82 The Psw Pump lP41-C001D was disassembled and repaired (Per HNP-1-3182) 81-6361 6-17-82 The Conduit for the torus water clean-up electrical system 1G51 was routed and supported (Per DCR-78-200) 81-6599 6-17-82 The Torus water clean-up electrical system 1G51 had switches and indicators installed.(Per DCR-78-200-R2) 82-1600 6-22-82 The Torus water clean-up valve 1G51-F012 was modified and reinstalled.(Per DCR-78-200) 82-3915 7-14-82 The main steam SRV's 1B21-F0BE & L were disassembled and inspected.
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2 UNIT SilUTDOWNS AND POWER REDUCTIONS UNIT NAM E ri a t. c n DATE 3-HP July COMPLETED BY B-A.
Fa77etta i
REPORT MONTil TELEPil0NE 0l?-367-7851 i
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.Y ~h Licensee
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!1, Cause & Currective No.
Date g
3g 3g5 Event u sr E3 Action to
$5 5
j;5g Report #
rE0 yU Prevent Recurrence 4
5 Power reduction due to circ water temp) 82-23 820701 F
4.0 A
5 CB FILTER problems (due to clogged fiume screen i
82-24 820701 F
16.3 A
5 CB FILTER Power. ramp from above reduc tion 82-25 820702 S
2.4 B
5 HA TURBIN-Weekly turbine test 82-26 820704 F
1.5 A
5 WC DEMIllX Power reduction due to problems in "C" condensate demineralizer (low flow) 82-27 820705 F
1.3 A
5' UC DEMINX Power. reduction to backwash & precoat demineralizer 82-28 820710 S
3.0 8
5 HA TURBIN Weekly turbine test 82-29 820715 F
16.1 A
3 WC DEMI!!X Reactor scram due to loss of suction from condensate demineralizer i
I i
1 2
3 4
-F: Forced Reason:
Method:
Exhibit G-Instructions l
S: Scheduled A Equipment Failure (Explain) 141snual for Preparation of Data B4taintenance o( Test 241anual Scram.
Entry Sheets for Licensee C-Refueling 3 Automatic Scram.
Event ReporI(LERI File (NUREG-e
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D Regulatory Restriction 4 -Continuations 0161)
E-Operator Training & Ucense Examination 5-Ioad Pcduction 3
F-Administrative
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Exhibit I-Same Source G-Operaticnal Error (Explain)
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llother(Explain)
(9/77) 1 e
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r 50-366 DOCKET NO.
UNIT SIIUTDOWNS AND POWER REDUCTIONS UNIT N AME ttatcn 4 DATE 8-2-82 July COMPLETED BY R.A.
Fa770tta REPORT MONT11 TELErl!ONE 912-367-7951
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3 Yk Licensee
,E r, Cause & Corrective E3 Action to No.
Date g
3g s
3g5 Event
- 7
$5 5
jsy Report *
- G ju Prevent Recurrence d
82-3C 820715 F
16.1 A
3 WC DEMINX Ramp from above scraa 3
82-31 820717 S
1.4 B
5 HA TURBIN Weekly tur'bine test 82-32 820723 S
3.5 B
5 RC CONROD.
Load reduction to perform rod sequence exchange 82-33 820723' S
4.7 B
5 HA TURBIN Weekly turbine test.
6 82-34 820724 S
42.8 8
5 RC CONROD Ramp from above rod exchange 82-35 820730 F
'12.4 D
5 2-82-79 EE GENERA Load redtetion to repair 2C diesel generator ~
l 82-36 82-07-30
'F 26.2 D
2 2-82-79 EE GEFERA flanual scram to repair 2C diesel gene-rator I
2 3
4 F: Forced Reason:
Method:
Exhibit G-Instructions 5: Scheduled A. Equipment Failure (Explain) 1-Manual for Preparation of Dara l
B Maintenance of Test 2-Manual Scram.
Entry Sheets for Licensee i
C-Refueling 3-Automatic Scram.
Event Report (LER) File (NUREG-l D-Regulatory Restriction 4 -Continuations 016I)
E-Operator Training & Ucense Examination 5-Icad Itduction 5
I F-Administrative 9-Other (Explain)
Exhibit I Same Source G-Operational Error (Explain)
(9/77)
Il-Other (Ezpla'a) e
.t NARRATIVE REPORT UNIT 2 Date Unit 1 i
i July 1 Power reduction due to circ.
water temperature i
problems at 0345 hours0.00399 days <br />0.0958 hours <br />5.704365e-4 weeks <br />1.312725e-4 months <br />.
July 1 Power increased from above reason at 0745 bours.
July 2 Power reduced for weekly turbine test at 2245 hours0.026 days <br />0.624 hours <br />0.00371 weeks <br />8.542225e-4 months <br />.
July 3 Weekly turbine test complete at 0110 hours0.00127 days <br />0.0306 hours <br />1.818783e-4 weeks <br />4.1855e-5 months <br />.
July 4 Power reduction due to low flow in "c" condensate domineralizer at 0325 hours0.00376 days <br />0.0903 hours <br />5.373677e-4 weeks <br />1.236625e-4 months <br />.
July 5 Power reduced ude to backwashing and precounting demineralizer at 0050 hours5.787037e-4 days <br />0.0139 hours <br />8.267196e-5 weeks <br />1.9025e-5 months <br />.
July 10 Power reduced for weekly turbine test at 2015 hours0.0233 days <br />0.56 hours <br />0.00333 weeks <br />7.667075e-4 months <br />.
Test complete at 2315 hours0.0268 days <br />0.643 hours <br />0.00383 weeks <br />8.808575e-4 months <br />.
1 July 15 RX scram due to low suction on condensate booster pump.
! O Juiv 1s Rx crietcel ee 181s noure.
July 16 RX tied to line at 0046 hours5.324074e-4 days <br />0.0128 hours <br />7.60582e-5 weeks <br />1.7503e-5 months <br />.
July 23 Power reduction due to weekly turbine test at 2230 hours0.0258 days <br />0.619 hours <br />0.00369 weeks <br />8.48515e-4 months <br />.
July 24 Weekly turbine test complete at 0140 hours0.00162 days <br />0.0389 hours <br />2.314815e-4 weeks <br />5.327e-5 months <br />.
July 24 Load reduction to. perform rod sequence exchange at 0510 hours0.0059 days <br />0.142 hours <br />8.43254e-4 weeks <br />1.94055e-4 months <br />.
July 30 Load reduction to repair diesel generator at 1322 hours0.0153 days <br />0.367 hours <br />0.00219 weeks <br />5.03021e-4 months <br />.
July 30 Rx manualy scrammed to repair diesel generator at 2148 hours0.0249 days <br />0.597 hours <br />0.00355 weeks <br />8.17314e-4 months <br />.
O
s HATCH 2 SAFETY RELATED MAINTENANCE REQUEST TO'BE REPORTED FOR JULY 1982 O
Number Date Completed Description 82-906 4-22-82 Tee-quenchers and their supports 2T23 were installed inside torus. (Per DCR-79-345)82-907 4-22-82 Shell stiffeners and nozzle reinforcements were added to outside of Torus 2T23.(Per DCR-80-200) 82-2115 5-14-82 Pneumatic tests were performed on check valves 2B21.(Per HNP-6907) 82-2122 5-14-82 A
cable was deleted for Drywell personnel airlock interlock system.(Per DCR-78-403)82-412 6-3-82 A foundation pad was prepared for main control room vertical panel 2Hil-P691.(Per DCR-79-440) 82-1933 5-14-82 A tap off connection was installed and a valve was relocated on RCIC q
low speed trans.
bypass line.(Per b
DC R 4 40 -Rl) 82-1503 6-25-82 Power and control cables for MOV's pulled. (Per DCR-78-068) 82-1565 7-2-82 Conduit and support for LPCI inverter room.MOV.'s were fabricated and installed.(Per DCR-78-68) 82-1939 7-9-82 Cables were terminated in control.
room for drywell sump radiation monitors 2Dll-RE-NO37.
82-2157 7-14-82 Control and power cables 2Z41-B020A
& B were pulled. (Per DCR-78-68) 82-1410 7-14-82 The conduit and supports for RCIC pump suction transfer raceways were installed.(Per DCR-81-175) 82-3343 7-17-82 The A/C MCC starter assemblies 2R24 were removed from original units and reinstalled into new un its. (Per DCR-78-68)
O 82-1584 7-17-82 The powe and control cables 2Z41-B020A B were redlined.(Per DCR-78-68)
I a
UNIT 2 (Cont.)
Number Date Completed Description 82-2267 6-3-82 A Hydrostatic test was performed on D/W torus pressure instr.
and remote shutdown system.(Per DCR-79-4400)82-413 5-5-82 A sample line for the post accident sampling system 2P33-G001 was fabricated and installed.(Per DCR 4 76-Rl)
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