ML18059A488

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Forwards Insp Rept 50-255/93-20 on 930819-0929 & Notice of Violation
ML18059A488
Person / Time
Site: Palisades Entergy icon.png
Issue date: 10/27/1993
From: Greenman E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Hoffman D
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
Shared Package
ML18059A489 List:
References
NUDOCS 9311080032
Download: ML18059A488 (38)


See also: IR 05000255/1993020

Text

Docket No. 50-255

Consumers Power Company

ATTN:

Mr. David P. Hoffman

Vice President

Nuclear Operations

1945 West Parnall Road

Jackson, MI

49201

Dear Mr. Hoffman:

October 27, 1993

SUBJECT:

SPECIAL TEAM INSPECTION REPORT 50-255/93020(DRS)

This refers to the special team inspection led by Mr. Robert Lerch of this

office, to follow up events from your Summer 1993 refueling of the Palisades

Nuclear Plant and to observe routine activities. The team was composed of

Michael Parker, Ronald Bailey, Thomas Tongue and David Nelson of the

Region III office and our contractor Carl B~yer of Battelle Northwest*

Laboratories. This refers also to the inspection of your cycle 11 core reluad

plan conducted by Anthony Hsia, Edward Kendrick, James Davis, and

Shih Liang Wu of the Office of Nuclear Reactor Regulation.

At the conclusion

of the onsite inspection, an interim "exit" meeting was held with you and

members of your staff to discuss the inspection findings.

On September 29,

1993, a final exit was held.

Areas examined during the inspection are identified in the enclosed report.

Within these areas, the inspection consisted of selective examinations of

procedures and representative records, interviews with personnel, and

observation of activities in progress.

The teams concluded that your

corrective actions for the damaged 1-24 and stuck SAN-8 fuel assemblies were

adequate for cycle 11 operation.

Your root cause determination efforts were

found sufficiently completed and technically thorough that repetition of those

problems would be prevented this cycle. However, some long term corrective

actions have yet to be determined.

We understand that you plan to collect *

additional information and further evaluate contributing factors for the next

cycle (12).

Our observations of plant activities, though limited, concluded

that your staff was ready and capable to start up and routinely operate the

pl ant.

A review of the regulatory issues.documented in the Augmented Inspection Team

  • (All) inspection report, (Report No. 50-255/93018), was also performed.

Based

on these inspection, certain of your activities appeared to be in violation of

NRC requirements as described in the enclosed Notice of Violation (Notice) .

9311080032 931027

---

.PDR

ADOCK 05000255 .

G

PDR

~*

Consumers Power Company

2

October 27, 1993

We considered these issues for escalated enforcement pursuant to the NRC

Enforcement Policy, 10 CFR Part 2, Appendix C.

We concluded that escalated

enforcement was not appropriate because some of the issues share common causes

with, and predate, issues previously addressed in our Notice of Violation and

Proposed Imposition of Civil Penalty (EA-93-178) dated September 14, 1993.

The previous escalated enforcement action was taken, in part, to emphasize the

necessity for strict, disciplined control and verification of proper

performance of activities involving reactor components.

We are concerned that

additional violations were observed later in the outage, in which management

controls in the form of procedures were not followed.

Although some of these

violations occurred in the presence of your supervisors and/or auditors, they

did not intervene to stop the activity and correct it.

You are required to respond to this letter and should follow the instructions

specified in the enclosed Notice when preparing your response.

In your

response, you should document the specific actions taken and any additional

actions you plan to prevent recurrence.

After reviewing your response to this

Notice, including your proposed corrective actions and the results of future

inspections, the NRC will determine whether further NRC enforcement action is

necessary to ensure compliance with NRC regulatory requirements .

In your response to these violations, you are specifically requested to

address actions you have taken or plan to take to ensure:

1.

procedures or other controls exist which exactly define the means ~nd

limits for handling reactor components so they will not become damaged;

2.

the controls/procedures are strictly followed;

3.

compliance is carefully monitored and verified; and,

4.

reactor component performance in service is analyzed, acceptance limits '

are established, and proper performance within limits is monitored and

verified.

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of

this letter and its enclosures will. be placed in the NRC Public Document Room.

The responses directed by this letter and the enclosed Notice are not subject

to the clearance procedures of the Office of Management and Budget as required

by the Paperwork Reduction Act of 1980, Pub.

L~ No. 96.511 .

~*

Consumers Power Company

3

October 27, 1993

We will gladly discuss any questions you have concerning this inspection.

Enclosures: *

I. Notice of Violation

2.

Inspection Report

No. 50-255/93020

cc w/enclosures:

David P. Hoffman, Vice President

Nuclear Operations

David W. Rogers, Safety

and Licensing Director

OC/LFDCB

Resident Inspector, Riii

James R. Padgett, Michigan Public

Service Commission

Michigan Department of

Public Health

A. H. Hsia, LPM, NRR

SRI, Big Rock Point

J. Lieberman, OE

R. DeFayette, RA

bee w/enclosure:

PUBLIC 'IE-01

Sincerely,

Original signed by Edward G. Greenman

Edward G. Greenman, Director

Division of Reactor Projects

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Consumers Power Company

3

October 27, 1993

We will gladly discuss any questions you have concerning this inspection.

Enclosures:

1.

Notice of Violation

2.

Inspection Report

No. 50-255/93020

cc w/enclosures:

Gerald B. Slade, General

Manager

David W. Rogers, Safety

and Licensing Director

OC/LFDCB

Resident Inspector, Riii

James R. Padgett, Michigan Public

Service Commission

Michigan Department of

Public Health

A. H. Hsia, LPM, NRR

SRI, Big Rock Point*

J. Lieberman, OE

R. DeFayette, RA

bee w/enclosure:

PUBLIC IE-01

Sincerely,

Original signed by Edward G. Greenman

Edward G. Greenman, Director

Division of Reactor Projects

Riii

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See Following Page----------~--------------------

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Bailey

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Nelson

Jorgensen

10/ /93

10/ /93

10/ /93

10/ /93

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NRR

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See Following Page-----------------------

W. Dean

OeFayette

Forney

Greenman

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~*

Consumers Power Company

2

October 27, 1993

Procedure for NRC Enforcement Actions" (Enforcement Policy), 10 CFR Part 2,

Appendix C.

Accordingly, no Notice of Violation is presently being issued for

these inspection findings.

In addition, please be advised that the number and

characterization of apparent violations described in the enclosed inspection

report may change as a result of further NRC review.

You will be advised by separate correspondence of the results of our

deliberations on this matter.

No response regarding these apparent violations

is required at this time.

In accordance with 10 CFR 2.790 of the Commission's regulations, a copy of

this letter and the enclosed inspection report will be placed. in the NRC

Public Document Room.

We will gladly discuss any questions you have concerning this inspection.

Sincerely,

Edward G. Greenman, Director

Division of Reactor Projects

Enclosure:

Inspection Report

No. 50-255/93020

cc w/enclosure:

David P. Hoffman, Vice President

Nuclear Operations

David W. Rogers, Safety

and Licensing Director

OC/LFDCB

Resident Inspector, Riii

James R. Padgett, Michigan Public

Service Commission

Michigan Department of

Public Health

A. H. Hsia, LPM, NRR

SRI, Big Rock Point

J. Lieberman; OE

R. Defayette, RA

Rill

Riii

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See Following Page-------------------------------

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Bailey

Tongue

Nelson

Jorgensen

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2

October 27, 1993

enforcement action in accordance with the "General Statement of Policy and

Procedure for NRC Enforcement Actions" {Enforcement Policy}, 10 CFR Part 2,

Appendix C.

Accordingly, no Notice of Violation is presently being issued for

these inspection findings.

In addition, please be advised that the number and

characterization of apparent violations described in the enclosed inspection

report may change as a result of further NRC review.

You will be advised by separate correspondence of the results of our

deliberations on this matter.

No response regarding these apparent violations

is required at this time.

In accordance with 10 CFR 2.790 of.the Commission's regulations, a copy of

this letter and the enclosed inspection report will be placed in the NRC

Public Document Room.

We will gladly discuss any questions you have concerning this inspection.

Enclosure:

Inspection Report

No. 50-255/93020

cc w/enclosure:

David P.

H~ffman, Vice President

Nuclear Operations

David W. Rogers, Safety

and Licensing Director

OC/LFDCB

Resident Inspector, Riii

James R. Padgett, Michigan Public

Service Commission

Michigan Department of

Public Health

A. H. Hsia, LPM, NRR

SRI, Big Rock Point

J. Lieberman, OE

R. DeFayette, RA

R1ir4

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Lerch/cg

10/ty /93

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Bailey

10/ ii.I /93 ~~

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Sincerely,

Edward G. Greenman, Director

Division of Reactor Projects

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Greenman

10/

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-*

NOTICE OF VIOLATION

Consumers Power Company

Palisades Nuclear Plant

Docket No. 50-255

License No. DPR-20

During an NRC inspection conducted on July 8 through July 20, and August 19

through 27, 1993, violations of NRC requirements were identified.

In

accordance with the "General Statement of Policy and Procedure for NRC

Enforcement Actions," 10 CFR Part 2, Appendix C, the violations are listed

below:

A.

10 CFR 50.59 (b)(l) requires in part that the licensee have a

written safety evaluation which provides the bases for

determination that a change in the facility as described in the

Safety Analysis Report does not involve an unreviewed safety

question.

Section 3.3.2.6 of the Updated Safety Analysis Report

describes use of hafnium poisoned assemblies as part of a neutron

fluence reduction program.

Contrary to the above, the licensee's 50.59 evaluation of extended

use of hafnium poisoned I-series fuel assemblies for cycles 10 and

11 did not provide complete bases for the determination that there*

was no unreviewed safety question.

Specifically, the evaluations

did not include consideration of the effects of the neutron

spectrum at th~ periphery of the core (which was proportionally

higher in "fast" neutrons and lower in "thermal" neutrons compared

to non-periphery locations) on mechanical properties of the

assemblies.

These evaluations were therefore incomplete.

This is a Severity Level IV violation (Supplement I).

B.

10 CFR 50, Appendix B, Criterion XI, requires that a test program

c.

'_be established to assure that all testing required to demonstrate

that structures, systems, and components will perform

satisfactorily in service is identified and performed in

accordance with written test procedures.

Contrary to the above, the licensee's Cycle 10 radiochemistry

testing did not positively identify failed I-series fuel, nor was

additional testing performed between cycles 10 and 11 to assure !-

series fuel would perform satisfactorily for a sixth cycle, which

constituted a unique fuel performance demand.

This i*s a Severity Level IV violation (Supplement 1).

10 CFR 50, Appendix B, Criterion XVI, requires in part that

measures be established to assure that conditions adverse to

quality are promptly identified and corrected.

In the case of

significant conditions adverse to quality the measures shall

assure that the cause of the condition is determined and

corrective action taken to preclude repetition.

--

9311080036 931027

,.

PDR

ADOCK 05000255

0

PDR

-*

Notice of Violation

2

Contrary to the above, when the upper guide structure (UGS) was

lifted from the reactor on July 6, 1993, and a fuel bundle from

core location Z-11 stuck onto the UGS, it marked the third

occasion for this same interference between core components.

This is a Severity Level IV violation (Supplement I).

D.

Technical Specification 6.8.1.b requires that written procedures

be established, implemented and maintained for activities covering

refueling operations.

1.

Licensee procedure RVI-M-1, Revision 16, "Removal and

2.

  • storage of the Upper Guide Structure," provided instructions

for installation for a Tl-2000 load cell readout device

only.

Contrary to the above, on July 6, 1993, while lifting the

UGS, a J-300 load cell readout device was used.

Licensee procedure RVI-M-1, Revision 16, "Removal and

storage of the Upper Guide Structure," Section 5.3.6.g,

includes a stipulation to follow Work Order No. 24301781 for

steps to use a load cell. Step 3.3.A.7 of the work order

requires that the load cell readout device be zeroed.

Contrary to the above, on July 6, 1993, while p~rforming

procedure RVI-M-1, the load cell readout device was not

zeroed.

3.

Licensee procedure RVI~M-1, Revision 16, "Removal and

storage of the Upper Guide Structure," Section 5.3.14,

specifies an upper load limit of 62,000 pounds.

Contrary to the above, on July 6, 1993, while performing

procedure RVI-M-1, after the UGS was raised approximately

six inches, indicated load reached 62,800 pounds, which is

in excess of the upper load limit.

4.

Licensee procedure FHS0-18, "Recovery of Bundle SAN-8,"

requires in steps 4.2.6 and 5.2.l that chainfall tension be

limited to a combined load of 1500 ~ 1600 pounds.

Contrary to the above, on July 7, 1993, the chainfalls were

tightened to a combined load of 2300 pounds.

This is a Severity Level IV violation (Supplement I) .

-*

Notice of Violation

3

Pursuant to the provisions of 10 CFR 2.201, Palisades Nuclear Plant is hereby

required to submit a written statement or explanation to the U.S. Nuclear

Regulatory Commission, ATTN:

Document Control Desk, Washington, D.C. 20555

with a copy to the Regional Administrator, Region III, and a copy to the NRC

Resident Inspector at the facility that is the subject of this Notice, within

30 days of the date of the letter transmitting this Notice of Violation

(Notice).

This reply should be clearly marked as a "Reply to a Notice of

Violation" and should include for each violation:

(1) the reason for the

violation, or, if contested, the basis for disputing the violation, (2) the

corrective steps that have been taken and the results achieved, (3) the

corrective steps that will be taken to avoid further violations, and (4) the

date when full compliance will be achieved.

If an adequate reply is not

received within the time specified in this Notice, an order or a Demand for

Information may be issued to show cause why the license should not be

modified, suspended, or revoked, or why such other action as may be proper

should not be taken.

Where good cause is shown, consideration will be given

to extending the response time .

Da~ed a~~len Ellyn, Illinois

th1s35day of October 1993

-*

U. S. NUCLEAR REGULATORY COMMISSION

REGION I I I

Report No. 50-255/93020(DRS)

Docket No. 50-255

Licensee:

Consumers Power Company

Palisades Nuclear Plant

27780 Blue Star Highway

Covert, MI

49043

Facility Name:

Palisades Nuclear Plant

Inspection At:

Palisades site, Covert, MI

License No. DPR-20

Inspection Conducted:

August I9 - 27, and September 29, I993

Inspectors:

Thomas Tongue

Ronald M. Bailey

Michael Parker

Shih Liang Wu

Appr*v*d ay: ~ifl:~rr

Team Leader

David Nelson

Anthony H. Hsia

Edward D. Kendrick

James L. Davis *

Date

Inspection Summary

Inspection on August I9 - 27. and September 29. I993 (Report No. 50-255/93020}

Areas Inspected: Special, announced, team inspection of licensee activities

relating to Summer I993 refueling outage problems, and to plant restart

preparations, including: the safety evaluation for the cycle II core reload,

routine plant operations activities, the impact of the fuel lost from the

damaged fuel assembly, the root cause evaluation for the stuck fuel assembly,

the regulatory issues identified in the All report, and the September 9, I993

public meeting.

Results: Apparent violations resulting from the All *inspection are identified

in paragraph 7 .

9311080041 931027

PDR

ADOCK 05000255

G

PDR

.i

REPORT DETAILS

1.0

Persons Contacted

G. B. Slade, Plant General Manager

T. J. Palmisano, Plant Operations Manager

K. M. Haas, Radiological Services Manager

R. B. Kasper, Maintenance Manager

D. W. Rogers, Safety and Licensing Director

R. M. Rice, Director, Nuclear Performance Assessment Department (NPAD)

K. E. Osborne, System Engineering Manager

These people and others were present at the exit meetings on July 27, and

September 29, 1993.

R. M. Rice was not present at the September 29, 1993

exit. Other members of the plant staff and NPAD were contacted during the

inspection period.

2.0

Introduction

On July 1, 1993, at Palisades Nuclear Plant, a broken fuel rod was identified

in the tilt pit area of the reactor cavity.

On July 6, 1993, while removing

the upper guide structure (UGS) as part of the investigative activities

associated with the broken fuel rod, a fuel assembly was inadvertently lifted

from the core.

In response to these events, an Augmented Inspection Team

(AIT) was sent to the site to document and validate the relevant facts,

determine the probable causes, and evaluate the licensee's analyses efforts

and review of the events including corrective actions. A public All exit

meeting was held with plant management on July 20, 1993.

The results of the

All inspection were documented in Inspection Report 50-255/93018.

After the All exit, the NRC continued to monitor the licensee's corrective

actions in several ways.

Daily briefings on the licensee's root cause

analyses and recovery efforts were conducted via conference calls with the NRC

until two teams were sent to the site. One team reviewed the safety

evaluation for the core reload, which uses reconstituted L-series fuel

assemblies - see paragraph 3. A technical review of the of the root cause

determinations for the fuel assembly stuck to the UGS was conducted - see-

paragraph 4.

The second team evaluated the plant staff in the performance of

routine activities and a trial installation of the upper guide structure - see

paragraph 5.

A contractor with the second team evaluated the licensee's

search for the fuel lost from the damaged fuel assembly and the consequences

this fuel might have - see paragraph 6.

An assessment of the ftndings from

the All report was conducted to determine which ones represented regulatory

issues - see paragraph 7. A public meeting was held.with the licensee on

September 9, 1993 - see paragraph 8 .

2

-*

3.0

The 50.59 Safety Evaluation of the Cycle 11 Core Reload

The NRR team reviewed the license~'s performance in implementing the-

requirements set forth in 10 CFR 50.59.

The principal measure of this

performance is the quality of the 50.59 safety evaluation prepared by the

licensee for the revised Cycle 11 core design which included the 16

reconstituted L-assemblies in the corner core locations. Also included in

assessment was the documentation of the 50.59 safety evaluation, the

licensee's procedure for safety evaluations, and the PRC review process.

review of the 50.59 safety evaluation included its scope, accuracy, and

thoroughness in both technical content and documentation.

the

The

As a result of the root cause analysis for the damaged fuel assembly, the

licensee revised the original Cycle 11 core design by replacing all the

I-series fuel assemblies with thrice-burned L- series assemblies reconstituted

with 14 stainless steel rods (see Section 3.1 for detailed descriptions).

These modified L-series assemblies were located at the 16 corner core

locations as shown in Figure 2.

According to Palisades Procedure No.3.07,

Rev.7, the licensee performed a safety evaluation of the revised Cycle 11 core

design in compliance with the regulations set forth in 10 CFR 50.59. Their

evaluation was documented in "Palisades Nuclear Plant Safety Review", Plant

Safety and Licensing (PS&L) Log No.93-1025, which concluded that there were no

unreviewed safety questions in accordance with 10 CFR 50.59.

On August 19,

1993, the Plant Review Committee (PRC) reviewed the 50.59 safety evaluation,

agreed with the conclusions and approved the revised Cycle 11 core design.

From the perspective of mechanical design, material, core physics, and thermal

hydraulics, the inspection focused on the licensee's evaluations of safety

significance and whether there was any unreviewed safety question stemming

from the revised Cycle 11 core design.

The inspectors also assessed the

licensee's root cause analysis to date, its plans for continued root cause

analysis, and the changes made to address the root causes.

The team also

agreed with the Pal.isades PRC conclusion that the revised Cycle 11 core design

do~s not constitute an unreviewed safety question and its approval of the

revised cycle 11 core design.

,

3.1

Description of Changes in the Facility from that Described in the

Final Safety Analysis Report (FSARl

3.1.1

Fuel Assemblies

The M-assemblies, N-assemblies, 0-assemblies, and SAN-assemblies have not been

altered for the revised Cycle 11.

The L-assemblies have been reconstituted_

for the revised Cycle 11 by replacing 14 fuel rods with 14 solid stainless

steel rods.

Eight stainless steel rods were placed in the corner of the fuel

assembly in the shroud corner with the stainless steel rods placed from the

guide bar to the corner plus the location next to the corner location as shown

in Figure 1.

Each remaining corner of the fuel assembly contains 2 stainless

steel rods as shown in Figure 1 .

3

The criteria used by the licensee to select the L-assemblies to replace the

I-Hafnium assemblies were:

1.

8urnup < 37,500 MWD/MTU at EOC 11 for J~assemblies and K-assemblies.

Licensee Justification: This criteria is somewhat arbitrary and less

important if the L- assemblies are used.

The objective is to stay below the

1-24 assembly burnup at the start.of cycle 10 when the 1-24 assembly was

intact. The L-assemblies have the spacers manufactured with a vertical roll

and will grow in that direction with fluence.

The spacer cells will not get

bigger, rather they willget taller; so, the design limit of 46,000 MWT/MTU is

still applicable for the L-assemblies for cycle 11.

2.

Assemblies can not be used that have previously occupied one of the

eight octant symmetric corner shroud positions.

Licensee Justification: This requirement may be conservative for all eight

octant positions.

However, it is advantageous to avoid assemblies that

previously occupied 8-19 and X-19 core locations.

3.

Consider assembly bowing to avoid largely bowed assemblies.

Licensee Justification: Assembly to shroud interference already existed at

Cycle 10 8-19 and X-19 locations. Placing the bowed assembly towards the

shroud in Cycle 11 may*worsen the problem.

4 .

L-assemblies may*have some advantages over the. J-assemblies and the K-

assemblies.

Licensee Justification: The spacer plate material for the L-assemblies was

stamped in a preferential direction to minimize cell opening due to growth.

Also, using L-assemblies will not require ultrasonic examination since they

were examined after their last cycle.

The J-assemb.lies and K-assemblies will

require ultrasonic examination prior to use in Cycle 11.

'

5.

Fluence rates values should not exceed Cycle 9 values.

Licensee Justification: Cycle 9 fluence rates were used for consistency with

the pressurized thermal shock data currently being reviewed by the NRC.

3.2

Mechanical Design

The stainless steel rods are 0.437 inches in diameter while the fuel rods they

replaced were 0.417 inches in diameter.

The licensee proposed that the larger

diameter rods will reduce the probability of fretting damage during Cycle 11

due to an estimated increase in spring force of 0.6 pounds.

The licensee

proposed that the corners with 2 stainless steel rods will be less likely to

fret and that the load on adjacent fuel rods will be symmetrically increased,

decreasing the probability of fretting on the adjacent fuel rods .

4

-*----

The revised L-assemblies and SAN-assemblies have standard design spacers and

all of the remaining assemblies in the core for cycle 11 have the debris

resistant, High Thermal Performance (HTP) spacers.

The I-assemblies that "the

revised L-assemblies replaced also had the standard design spacers. Hence,

the licensee concluded that the use of the revised L-assemblies will not

affect spacer induced flow conditions in the core for the revised Cycle 11.

3.3

Core Physics Design

The revised Cycle 11 core contains 52 twice-burned M-assemblies, 68 once-

burned N-assemblies, 60 fresh 0-assemblies, 8 once-burned N Shield Assemblies

(SAN}, and 16 modified thrice-burned L-assemblies with 14 solid stainless

steel rods inserted in the assembly corners. The difference between the

revised and the original Cycle 11 core designs is the 16 reconstituted

L-assemblies and the relocation of the selected M and N assemblies

(20 assemblies in each batch}.

Figure 2 shows the revised Cycle 11 core

design.

For fluence reduction purposes, the revised Cycle 11 core is a low radial

leakage core incorporating 8 SAN assemblies in the flat peripheral regions and

16 reconstituted L-assemblies in the core corner locations. A higher initial

reactor coolant boron concentration is needed to offset the additional

reactivity in the revised Cycle 11 because of the revised L-assemblies (which

are more reactive as compared to the.I-assemblies), because the 0-~ssemblies

have enrichment higher than previous fuel assemblies, and because of less

gadolinia used in Cycle 11 fuels as compared to previous cycles .

3.4

Impact on the FSAR and the Technical Specifications (TS)

The licensee's 50.59 safety evaluation as documented in PS&L Log No. 93-1025

indicates that many FSAR Sections and TS Sections have been reviewed for

possible changes due to the revised Cycle 11 core design.

These reviews

identified FSAR Sections 3.3.1, and 3.3.4.3, and Tables 1-2, and 3-11 to be

affected by the design changes.

None of the TS Sections was identified to be

affected by the design changes.

The licensee plans to update FSAR Sections 3.3.1 and 3.3.4.3 to delete the

discussions on the boron carbide neutron absorber rods and the Hafnium

clusters that are no longer used, and to add the discussions on the 16

modified L-assemblies and the new assemblies with debris resistant features.

The licensee also plans to update Table 1-2 to include Batch 0 average U-235

enrichment, and to update Table 3-11 for inclusion of L-assemblies and

deletion of* boron carbide neutron absorber rods and Hafnium clusters.

The staff rev~ew also identified FSAR Section 3.3.2.6 which discusses the H-

assembl ies with stainless steel rods in Cycle 8, the I-assemblies with-Hafnium

clusters in Cycle 9, and the SAN assemblies in Cycle 10, as used by the

licensee to reduce neutron fluence on the reactor vessel. This section should

have been identified by the licensee for deletion of the Hafnium clusters and

inclusion of the r~vised L-assemblies.

The licensee plans to make these

additional changes to the FSAR .

5

-*---

The Licensee's 50.59 safety evaluation stated that the radial peaking factor

limits listed in TS Table 3.23-2 were not_ changed by the revised L-assemblies

used to replace the I-assemblies. Although Table 3.23-2 does not specifically

list the limits for the revised L-assemblies and the SAN assemblies, Table 6.1

in the Siemens Power Corporation (SPC) report EMF-92-177, Rev~2, implies that

  • the "Revised L" and "SAN" assemblies are bounded by the "M and earlier" and

"N" assemblies, respectively. * The licensee uses the PIDAL code to perform its

weekly monitoring of the radial peaking factors for the 5 different batches of

fuel assemblies (Revised L, M, N, SAN, and 0).

The NRC evaluation of the FSAR and TS Sections, in light of the revised Cycle

11 design, found it necessary for the licensee to amend the TS Tables 3.23-1

and 3.23-2 to include the different assemblies in the core pri?r to operation

above 25% power.

3.5

Root Cause Analysis Evaluation for I-Assembly Failure

The licensee had proposed that there were 8 potential root causes for the fuel

failure in the 1-24 assembly discovered after cycle 10.

These were:

1.

2.

3.

4.

5.

6.

7 .

8.

Damaged during fuel moves during previous cycle(s);

Damaged during EOC 9 Ultrasonic Test Inspection;

Damaged during fuel moves in this refueling outage;

Fuel failure due to a loose spacer grid;

Fuel failure due to increased primary coolant system (PCS). flow;

Fuel failure due to core barrel vibration;

Fuel failure due to a manufacturing defect; and, .

Fuel failure due to a shroud/fuel assembly interface problem.

Number 1 was eliminated because all of the assemblies placed in the core for

cycle 10 were ultrasonically tested (UT) between cycle 9 and-cycle 10.

Number 2 was eliminated since the records indicate that the I-24 bundle was

not rotated during UT examination and could not have been damaged by the UT

test rig.

Number 3 was eliminated by reexamination of the chemistry results

for cycle 10.

Number 4 was eliminated by the licensee as the root cause but

is thought to be a contributing factor.

The licensee considers numbers 5, 6,

and 7 to be less likely as the root cause.

However, the licensee has proposed

that 5 and 6 may be contributing factors. The licensee has proposed that

number 8 is the most likely cause of the I-24 assembly rod failure.

The use of stainless steel rods in the corners of the replacement assemblies

addresses possibility 4, according to the licensee, by increasing the spring

force on these rods.

The use of stainless steel rods in the replacement

assemblies addresses possibilities 5, 6, and 8 by placing sacrificial rods

that do not contain fuel in locations where damage occurred to some rods

during cycle- 10 and which are more suscepUble to potential damages in* future

fuel cycles.

The licensee did not think that the use of stainless steel rods would prevent

the type of spacer,fretting that occurred on 1-24 during cycle 10.

However,

the licensee proposed that the stainless steel rods would be the only rods

affected and no fuel would be lost as a result of spacer fretting .

6

-*--

The team did not complete its assessment of the root cause analysis since the

licensee had not finalized the root cause analysis.

Additional data such as examination of core vibrational data, fuel failure

monitoring, end of cycle {EOC} 11 fuel assemblies examination, and EOC 11

shroud examination will contribute to the understanding of the root causes.

This will be tracked as inspection follow~up item {IFI 50~255/93020-01}

3.6

3.6.1

3.6.1.1

Technical Evaluations

Mechanical Design

Fuel Reconstitution and Generic Letter CGLl 90-02 Supplement 1

The NRC staff issued GL 90-02, Supplement 1, to address the nuclear industry

trend of reconstituting fuel assemblies with dummy {nonfueled} rods of

stainless steel or zircaloy.

The use of dummy rods facilitates the

replacement of failed fuel rods when leakers are detected.

GL 90-02,

Supplement 1 requires that NRC-approved methodologies be applied for

reconstitution to ensure compliance with General Design Criteria {GDC} 10.

The staff is reviewing SPC topical report ANF-90-082, entitled "Application of

ANF Design Methodology for Fuel Assembly Reconstitution." This report is

expected to be approved soon.

The licensee's reconstitution for the revised

Cycle 11 core is not covered explicitly by ANF-90-082, as discussed in

licensee's 50.59 evaluation. However, SPC reanalyzed the Cycle 11 core with

the 16 new reconstituted assemblies as described in the safety analysis report

EMF-92-177, Revision 2.

The results showed that the Chapter 15 analyses were

still bounded by the previous analyses.

The team considers the reanalyses of

Cycle 11 core adequate.

3.6.1.2

Oversized Stainless Steel Rods

The*stainless steel rods in the reconstituted L assemblies ~re slightly larger

in diameter, than the fuel rods.* The larger stainless steel rods in the corner

will exert more force on the lantern spring, thereby tightening up the

adjacent fuel rods. This results in higher spring force on fuel rods to

compensate the spring relaxation during irradiation. The fuel vendor's

analysis and testing results confirmed that there was higher spring force on

  • the adjacent fuel rods. Since SPC has confirmed that the bimetallic spring

relaxed as expected, the use of larger stainless steel rods tends to reduce

the potential for fretting between the fuel rQds and spacer springs. Thus,

the team considered the use of larger stainless steel rods acceptable.

3.6.1.3

Spring Retention

The rod withdrawal force data frQm fuel assemblies I, J, K, H, and L have

shown that the spring force relaxed significantly during Cycle 10.

In some

cases, the rod cell force was completely diminished.

However, this result was

not unexpected by SPC .

7

-*--

SPC incorporated the Palisades data into the spring force relaxation versus

burnup_data from other SPC assemblies.

The results showed that the bimetallic

spring relaxed with higher burnup as expected for Palisades' spacer springs.

SPC's analysis has demonstrated that the spring force will remain higher than

-the vibration force until the end of Cycle 11.

The team understands that the

licensee's current fuel design uses the high thermal performance (HTP) grid

spacer.

The HTP grid spacers do not use bimetallic springs and should be less-

prone to the fretting damage.

Because the Palisades spring data were within

the bounds of the ~nalysis and the larger stainless steel rods were used to

increase spring retention, t~e team ~oncludes that the spring retention has

been adequately addressed.

3.6.1.4

Fretting Wear Against Core Shroud

Although the licensee has not yet determined the root cause, some possible

causes were surveyed and examined.

The licensee speculated that the most

probable cause was due to interference between the core shroud and fuel

assembly, indicated by the missing or torn grid spacers and the corresponding

wear indications on the core shroud.

While the Palisades fuel failure root

cause analysis is continuing, the licensee has taken actions to prevent such a

phenomenon from recurring by placing stainless steel corner rods in the

reconstituted L-assemblies which will be placed in the core corner locations.

This is a solution that is similar to that used in resolving the Westinghouse

reactor baffle jetting problem.

The reconstituted L-assemblies will reside in

the Cycle 11 core for only one cycle, and will be replaced by new shielding

assemblies in future reloads.

Based on the reconstituted assemblies, the team

concludes that the licensee has taken appropriate action in mitigating the

consequence of interference between fuel assembly and core shroud.

3.6.1.5

Wear of the Control Rods

The revised L-assemblies are placed in the core with fluence induced bow

toward the center of the core.

The licensee has proposed that orienting the

revised L-assemblies in this manner minimizes the possibility of interactions

of the fuel assemblies with the shroud corner.

The revised L-assemblies were

selected based on those L-assemblies with the most uniform fluence.

The

maximum projected burnup gradient across the revised L-assembly at the end of

Cycle 11 was calculated by the licensee to be approximately 6,400 MWD/MTU.

Eight of the revised L-assemblies are next to a control rod.

The maximum

projected gradient for an L-assembly next to a control rod is calculated to be

about 4,600 MWD/MTU.

The licensee reports that during previous cycles,

assemblies with gradients as high as 7,000 MWD/MTU were oriented towards a

control rod resulting in no interaction between the assembly and the control

rod.

The licensee proposes that the burnup gradients for the revised

L-assemblies is expected to be bounded by past operating history of SPC fuel

at Palisades.

The space between fuel assemblies is 0.365 inches and the width of the blades

on the control rod is 0.180 inches leaving a gap of 0.093 inches between the

fuel assembly and the control rod blade on each side of the blade.

The

licensee has proposed that the bow in the assembly will be less that 0.093

inches based on past operating history and calculations by the licensee's fuel

8

supplier.

The NRC team concurs with the licensee's analysis that the fuel

assemblies next to the control rods will not affect the functionality of the

control rods.

-

3.6.2

Core Physics Design

As stated in the SPC Letter, to the licensee dated August 17, 1993, HGS:312:93

the evaluation of the core physics design changes is documented in Revision 2

(August 17, 1993) of EMF-92-177, "Palisades Cycle 11 Safety Analysis Report,"

and in Revision 1 (August 23, 1993) of EMF-92-178, "Palisades Cycle 11:

Disposition and Analysis of Standard Review Plan Chapter 15 Events,"

The physics characteristics evaluated in Revision 2 of EMF-92-177 include

power distribution, control rod reactivity, and moderator temperature

coefficient {MTC) considerations.

The Cycle 11 core loading configuration was

redesigned by SPC to minimize radial peaking factors; specifically, to remain

within the approved Technical Specification {TS) limits of:

Assembly Radial Peaking Factor, FrA limit of 1.76 {Batch 0), 1.66

{Batch N), and 1;57 (Batches Mand L)

Total Radial Peaking Factor, F; limit of 2.04 {Batch 0), and 1.92

{a 11 others)

-Linear Heat Generation Rate {LHGR) li'mit of °15.28 kw/ft to 60%

core height; linearly decreasing to 14.21 kw/ft at 100% core

height

The maximum calculated_values for Fril and F; were 1.575 and 1.851,

respectively; which, when combined with the TS uncertainties, are within the

TS power peaking limits. The largest calculated LHGR is 11.63 kw/ft which is

also within the TS limiting value with the TS uncertainty included.

Shutdown margin calculations were performed for the modified Cycle 11

configuration, yielding a cycle minimum shutdown margin of 2.56% delta-rho at

End of Cycle {EOC}, Hot Full Power {HFP) conditions, which is above the TS low

limit of 2.00%.

The moderator temperature coefficient {MTC) was evaluated for

the revised Cycle 11 core configuration at both Hot Zero Power {HZP) and HFP

for Beginning of Cycle {BOC) and EOC conditions.

The calculated MTC values

are within the safety analysis limits of +0.5xl0-

4 delta-rho/degree F and -

3.5x10-4 delta-rho/degree F.

-

The minimum departure from nucleate boiling ratio (MDNBR) evaluation for the

revised Cycle 11 core configuration was performed with the ANFP CHF

correlation for the TS limiting radial peaking factor values.

The -re-analysis -

of eight Standard Review Plan (SRP) Chapter 15 events, as reported in

Revision 1 of EMF-92-178, shows that calculated DNB margins were improved with

the exception of Events 15.4.2 - Uncontrolled control rod bank withdrawal at

9

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power, 15.4.3(5} - Control rod misoperation: single rod withdrawal, and

15.6.1 - Inadvertent opening of pressure relief valve, which showed a slight

DNB margin degradation. All FSAR event acceptance criteria, however, were met

for the revised Cycle 11 core.

3.6.3.

Assembiy Flow Vibration And Core Barrel Vibration

The licensee considered core barrel vibration and assembly flow vibration as

two possible contributi~g factors to the fretting wear problem.

The core

barrel vibration problem was discovered early in the plant life and was

addressed by adding a hold-down ring to the UGS.

There was no indication in.

subsequent operations that the core barrel vibration occurred again.

The

licensee included the core barrel vibration in its root cause analysis and

concluded that it was a possible contributing factor.

The team considered the

licensee's effort in addressing the concern of core barrel vibration adequate.

For the assembly flow vibration, the licensee has reconstituted the

L-assemblies with larger stainless steel rods in the corner locations. The

reconstituted assemblies are designed to mitigate the potential fuel rod

damage due to assembly flow vibrations.

The team considered_ the licensee's

effort in addressing the concern of assembly flow vibration adequate.

  • Recently, a few other PWR plants also experienced similar phenomena of fuel

failure and fretting wear near the ~ore shroud.

The ~ssemblies involved were

of a newer spacer design located near the core shroud.* Subsequent

examinations and flow testing uncovered that there was a natural vibrational

frequency that existed for.a combined condition of a particular spacer design

and restricted flow.

Those licensees involved have modified the fuel

assemblies to dampen the flow ~ibration for the short term.

The fuel design

and flow testing procedures have been modified to take into account this

effect. Since this phenomenon is rather new and unique, the staff is

preparing an Information Notice to alert all licens~es of this type of flow

induced vibrational fretting.

The effects of the modified L-assembly oversized stainless steel rods.on local

assembly flow distributions and the intra-assembly and inter-assembly cross

flows was evaluated by SPC and was found to be insignificant .. The effects of

the revised core loading configuration on the core-wide flow distribution were

analyzed by SPC using the XTG computer code, including the simulation of the

two spacer designs {bi-metallic for the L-assemblies and HTP for the remaining

assemblies}.

The results showed that the revised core design had

insignificant effects on the core wid~ flow distribution.

3.6.4

Materials

The licensee analyzed the irradiation-induced spring force relaxation. The

spacer springs are designed such that they will not damage the cladding during

installation nor will they damage the cladding during operation due to

differential thermal expansion.

The spring force should be sufficiently high

to prevent fretting of the cladding, and to suppress as-fabricated and thermal

bow of the fuel rods and to resist flow induced vibration of the fuel rods .

10

-*

/

The springs start with a spring force ranging from 2.6 to 4.5 pounds.

The

minimum spring force is the force required to overcome flow induced vibration

force, which is 0.08 pounds.

The minimum spring force at the end of life will

be a 90 percent relaxation of the 2.35 pound beginning of life spring force or

0.2 pounds, which exceeds the flow induced vibration force of 0.08 pounds.

The team reviewed the licensee's iubmittal dated August 16, 1993, responding

to the NRC request for additional information on the fuel failure event, and

had the following comments.

Examination of the I-assembly fuel rod withdrawal

data showed that many of the individual spacers had apparent spring forces

less than 0.20 pounds with many of the spring forces being 0.0 pounds.

There

was no evidence of fretting damage at many of the spacers with low recorded

spring forces.

On the other hand, there were spacers with spring forces of

1.43, 1~32, 0.69, and 0.59 pounds that gave minor eddy current indications,

and spacers with spring forces of 0.69, 0.68, 0.59, 0.48, 0.34, and 0.29

pounds that gave severe eddy current indications.

Eddy current indications

are indicative of fretting damage.

The average spring forces for all of the

spacers appear to confirm the licensee's analysis; however, individual spacer

data are contradictory.

The average Palisades rod withdrawal force relaxation versus burnup data

agrees with data from other SPC assemblies.

The team agreed with the

licensee's determination of a 90 percent relaxation of spring forces at end of

life as being conservative based on the data presented.

The data presented by the licensee indicates that fast flux exposure for a

fourth cycle on the reconstituted L-assemblies will not affect the performance

of the assemblies.

The licensee does not intend to use the reconstituted L-

assemblies past cycle 11.

The team concurred that fast flux exposure for a

fourth cycle will not adversely affect the L-assemblies.

Furthermore, the

preferential stamping of the L-assemblies grid spacers so that the cells will

not increase in size with exposure is a marked improvement for the

reconstituted L-assemblies over earlier assembly designs.

3.6.5

, Burnup Considerations

Initially,, the I-shielding assemblies were planned for three cycles {Cycles 9,

10, and 11) in the core periphery.

The I-assemblies would have been in the

core for a total of six cycles, taking into account the previous three cycles

of normal operation. During the Cycle 9 outage, the licensee examined the

whole core with ultrasonic testing {UT).

There were no leakers among the !-

assemblies.

During Cycle 10 operation, some I-assemblies were damaged by the

flow vibrational fretting. Thus, it is prudent practice that, after three

cycles of normal power operation, an assembly should not go beyond one more

cycle {the fourth cycle) when used for shielding. The licensee plans to use

the reconstituted L-assemblies for only one cycle, Cycle 11, and plans to

replace the reconstituted L-assemblies with a new design of shielding

assemblies for future reloads.

The selection criteria used for replacement candidates for the I-assemblies

included a target EOC 11 burnup for J and K assemblies of less than the BOC 10

burnup for assembly 1-024 {37,500 MWD/MTU).

The assemblies finally chosen

11

-*

were from the L-assemblies with an allowable maximum burnup limit of 46,000

MWD/MTU due to the improved grid spacer design.

The projected batch average

EOC 11 exposure for the L-assemblies is approximately 36,500 MWD/MTU (with a

range of 33,321 to 40,028). Thus, the team concluded that, based on burnup

considerations, the reconstituted L-assemblies were acceptable.

3.6.6

Fluence Reduction

The design criteria .for the revised Cycle 11 core loading configuration

includes a requirement that fluence rates not exceed the documented Cycle 9

values. According to the Palisades reactor engineering staff, the criteria

used by SPC to meet this requirement was that the bundle powers in the

peripheral core locations be less than or equal to the Cycle 9 core peripheral

bundle powers. A preliminary scoping analysis was then performed by Palisades

staff using their in-house DOT-IV model which confirmed that the corresponding

fast fluence (>1.0 Mev) values were less than the Cycle 9 values at the

critical weld orientations. The final fluence evaluation calculations *will be

performed by Westinghouse, to be consistent with the Cycle 9 results

previously furnished to the NRC.

3.7

Plant Review Committee (PRC) Review and Approval

The PRC reviewed and approved the 10 CFR 50.59 submittal on the modified core

reload plan on August 19, 1993.

The PRC review was observed by members of the

NRC team.

The Palisades team that prepared the 10 CFR 50.59 review were

questioned extensively by the PRC personnel prior to receiving approval.

.

Questions were raised about the chromium plating on the SAN-8 upper tie plate

alignment pin hole inside diameter, about the cycle 11 fuel load integrity,

about the plans to detect a low power fuel rod failure during cycle 11, about

the plans to determine if the shroud is interacting with fuel assemblies

during cycle 11, and numerous additional questions. All of the questions were

addressed adequately by the licensee staff.

3.8

Documentation of the Licensee's 50.59 Safety Evaluation

The 50.59 safety evaluation was documented according to Procedure No.3.07,

Rev. 7, "Safety Evaluations".

However, the audit team found the 50.59

evaluation package designation confusing in that the current revised Cycle 11

core was identified as FC-934, Rev. 0, with an associated safety evaluation

SE Rev. 1 whereas the original Cycle 11 core was also identified as FC-934,

Rev. 0, with an associated safety evaluation SE Rev. 0.

The licensee

indicated that the difference between *these Cycle 11 designs was documented in

an Engineering Design Change (EDC).

The existence of the associated EDC was

not mentioned in the current FC-934, Rev. 0 documentation for the reader to

realize that the current FC-934, Rev.a is different from the original Cycle 11

core design bearing.the same Item Identification Number.

The team reviewed the documentation of the 50.59 safety evaluation for its

technical depth and thoroughness and found it acceptable but improvements are

needed.

The licensee's 50.59 evaluation adequately documented the revised

Cycle 11 core physics design, the various assembly mechanical designs,

I-assembly replacement criteria, detailed L-assembly modifications, assembly

12

-*

reconstitution considerations, qualitative thermal hydraulic DNB

considerations, and the evaluation of the projected bowing from the revised

L-assemblies.

The documentation should have included or referenced the thermal hydraulic

analysis addressing the core average and subchannel flows as a result of the

new design, its impact on core barrel and assembly vibrations; the loose grid

spacer, spacer spring retention forces and its impact on fretting wear; and a

discussion of how the fluence reduction criteria are satisfied by the new

design. These issues were addressed in other documentation as discussed

above.

3.9

Conclusions

_The team completed its audit review of the licensee's 50.59 safety evaluation

for the revised Cycle 11 core design and concluded that the licensee followed

their procedure in performing the safety evaluation and the evaluation and its

associated documentation are acceptable.

The team also agreed with the

Palisades PRC conclusion that the revised Cycle 11 core design does not

constitute an unreviewed safety question and its approval of the revised

cycle 11 core design.

No violations, deviations, unresolved or inspector followup items were

identified.

4.0

Stuck Fuel Assembly Root Cause Evaluation

On July 6, 1993,, fuel assembly SAN-8 was inadvertently partially lifted with

the upper guide structure (UGS) from core position Z-11.

Two previous

incidents involving inadvertent lifting of a fuel assembly from core position*

Z-11 with the UGS were experienced in 1988 and 1992.

Initial followup of the

July 6, 1993, stuck fuel assembly was performed by the resident inspectors and

documented in inspection report No 50-255/93017(DRP). Subsequent followup of

the event was performed by an augmented inspection team (All) and documented

in inspection report No. 50-255/93018.

The All performed an extensive review

of the event including evaluation of the root cause for the stuck fuel

assembly.

At the conclusion of the All inspection the licensee had not

identified any single root cause for the stuck assembly; however, several

potential contributors had been identified.

The potential contributors to the lifting of the stuck fuel assembly with *the

UGS were:

Undersized upper tie plate pin holes in SAN-8 .

Deformation of core shroud creating an interference between the

UGS fuel alignment pins and the fuel assembly.

Fuel assembly bow .

13

UG5 fuel alignment pins loose or returned to a bent state during

operation.

UG5 fuel alignment pins out of position or the core support plate

alignment holes out of position.

Debris causing hang-up of the fuel assembly in the UG5 .

UG5 not level during lift, to the extent that there was

interference between the UG5 and the fuel assembly.

Core support barrel mis-located .

Damage to alignment pins or to the lower alignment plate lifting

or setting of UG5.

Degraded surface condition of the UG5 alignment pins at core

location Z-11 which could have promoted sticking within fuel

assembly upper tie plate holes.

Loss of preload on cap screws and alignment pins, which hold the

UG5 together, resulting in a significant loss of structural

rigidity.

The licensee developed an action plan to determine the role of each of the

potential contributor~, during the lifting-of the fuel assembly with the UG5;

As a result, the licensee identified 75 action items relating to the 11

potential contributors,. for further followup.

Followup inspection on the action items has resulted in the licensee's root

cause investigation team identifying the following:

UG5 fuel alignment plate pins bent in location Z-llN (1.56

degrees), Z-115 (0.41 degrees), and Z-165 (0.99 degrees).

A single gage of 0.995" diameter could not be placed on pins Z-llN

and Z-165, indicating the pins to be curved.

Analyses indicated that angular misalignment between UG5 fuel

alignment pins and fuel assembly upper tie plate of 1-1.5 degrees

was sufficient to lift fuel assemblies.

Qualification test results and analyses indicate that bent and

straightened pins have a gap between alignment pin* shoulder and

the UG5 lower alignment plate. Bent and *straightened pins are

less rigid and less resistant to bending than originally installed

pins.

14

--*

SAN-08 upper tie plate had two distinctive peen marks offset from

the center of upper tie plate holes by approximately 0.5 inch.

Peen marks are in the orientation and separated by about the

spacing of UGS fuel alignment plate pins.

SAN-08 video camera inspection in the spent fuel pool identified a

piece of debris stuck to the bottom of one foot. Debris could

have made it harder to fully seat SAN-08.

An object 0.05 inch

thick under an assembly foot would dislocate the upper tie plate

by approximately 0.5".

With only SAN-08 removed from location Z-11, the core support

plate was inspected with no debris identified. Several days

later, with five assemblies removed from around Z-11 location,

debris was observed.

Reactor head alignment pin at 0 degree location was incorrectly

installed.

\\

Measurement of UGS levelness on successive lifts indicates

significant variation of direction and magnitude of out-of-

levelness.

Analysis indicated assembly bow may contribute to angular

misalignment between.UGS alignment pins and upper tie plate.

Close up video camera inspection of UGS alignment pins at location

Z-11 indicated a greater degree of engagement in the upper tie

plate alignment holes.

Tip of UGS fuel alignment plate pin at location Z-16S was observed

to be distorted during video camera inspection.

The above findings resulted in the following potential contributors to a stuck

fuel assembly being eliminated:

UGS fuel alignment pins out of position or the core support plate

alignment holes out of position.

UGS fuel alignment pins loose or returned to a bent state during

operation.

Deformation of core shroud creating an interference between the

UGS fuel alignment pins and the fuel assembly.

Undersized upper tie plate holes in SAN-8 *

Loss of structural rigidity of the UGS .

Damage to the UGS fuel alignment plate .

15

-*

Debris between the fuel assembly upper tie plate holes and the UGS

fuel alignment plate pins.

Mis-location of core support barrel .

The remaining potential contributors have been categorized as to their

significance in contributing to the stuck bundle.

Potential contributors found highly likely to solely result in bent fuel

alignment pins and/or stuck fuel assemblies were:

Tilted/unlevel UGS .

UGS with bent fuel alignment pins .

Fuel assembly not properly positioned or seated .

Potential contributors having moderate magnitudes and probabilities and which

could combine with other contributors to bend fuel alignment pi~s and/or stick

fuel assemblies were:

Fuel assembly bow.

Fuel alignment pins. with degraded surface conditions.

  • The licensee has taken the following actions to specifically address the five

remaining potential contributors identified above:

Replaced UGS fuel alignment plate pins Z-llN, Z-llS, and Z-16S.

Replaced the fuel assembly (SAN-08} upper tie plate for core

location Z-11.

The upper tie plate modified design reduces the

potential for interference between tie plate alignment holes and

UGS altgnment pins.

Implemented methods to evaluate fuel assembly elevations and

relative positions after reactor core reloads.

Modified equipment and revised procedures to assure UGS lift

rig/UGS levelness is established.

Modified procedures to assure UGS is level within acceptable

limits prior to lift of UGS.

In reviewing the licensee's root cause analysis, corrective actions to prevent

. reoccurrence, and. trial insertion/removal, the inspectors noted that the

licensee had expended significant resources to address the root cause for the

fuel assembly lifting. The licensee's root cause investigation team was

composed of highly dedicated individuals who utilized extensive problem

solving techniques.

Management was actively involved throughout the

investigation. Although the licensee had not completed all the long term

16

-*

actions, the actions taken were demonstrated adequate for cycle 11 operation.

The following long term actions were being evaluated by the licensee.

-

.

UGS levelness.

Replacement of RV head/UGS alignment pins.

Minimized fuel assembly bow.

Centering of crane.

Fuel assembly height/levelness/core verification.

Modification of upper tie plate for all fuel assemblies.

Camera/ljghtning/water clarity.

Dedicating specific load cell for UGS removal/insertion.

Future gauging of fuel alignment pins.

UGS key/keyway measurements.

Procedure upgrades, as. necessary.

No violations, deviations, unresolved, or inspection followup items were

identified in this area .

5.0

Observations of Activities

The team observed selected activities and interviewed licensee personnel to

evaluate the effectiveness of communications in the plant staff and workers

understanding of management expectations. Overall, the results were positive

with regards to employee readiness for operations.

At the time of the

inspection ~owever, there was limited activity in the plant; the outage work

was mostly completed and the.licensee was concentrating on finalizing the

efforts of the root cause assessment teams and final engineering restart

issues.

5.1

Operations

The team observed the conduct of operations personnel both inside and outside

of the main control room during major evolutions. This observation included

equipment testing, surveillantes and maintenance activities being conducted in

support of the outage.

Based upon these observations, the team concluded that

the-operations personnel demonstrated a ve~*good*awareness of plant

conditions and were able to communicate their knowledge through proper

coordination and control of plant activities in a safe manner. Additionally,

the operation's shift turnover activities were performed in a professional and

competent manner which ensured the appropriate transfer of information to

oncoming shift personnel .

17

Due to the low frequency of assigned work orders and surveillance tests in

progress, the team was unable to properly evaluate the adverse effects of

maintenance and testing activities on the operators' ability to control

support activities and maintain safe plant operations. However, a limited

number of activities that were observed appeared to be conducted in a

controlled manner which did not affect the operators' ability to perform

normal duties.

In general, procedures and administrative controls were in place to adequately

control and direct the safe startup and continued operation of the plant .. The

team reviewed selected operations procedures and controls (i.e. tagouts) to

verify the current plant conditions with existing procedural requirements with

minimal discrepancies noted. This verification included the system walkdown

of one safety system tagout and daily plant tours observing equipment status.

The team determined through interviews and observation of on-the-job

performance that operations personnel were knowledgeable and capable of

performing their licensed duties. Shift manning was maintained in accordance

with Technical Specifications at all times.

The team concluded that management actions to improve performance were in

place and.efforts undertaken to date were effective. The team interviewed

selected personnel in the management and non-management staff positions for

licensed operators.

In general, the non-management position operators felt

that management goals, directives and policies were adequately represented to

them but the importance of incorporating operator feedback into the

improvements was not clear. Management position operators felt that

management goals, directives and policies emphasized the professionalism with

which they conducted their jobs and were making improvements in plant

performance.

5.2

Maintenance

The team observed work in all the maintenance disciplines and saw that. work

orders and procedures were available~ adequate and followed, spare parts and

tools were proper and available, and that the knowledge and training of the

personnel involved was adequate for the job. Observations were made of shift

briefs, and pre-job briefs, which were thorough, with ~ood discussion.

Management expectations were made known.

Post-maintenance testing was also

observed and found to be appropriate. The test results met the acceptance

criteria and were properly documented and trended.

The team noted the

presen~e and involvement of first line supervisors and system engineers.

Interdepartment cooperation was good.

NPAD assessors were also present

occasionally.

In summary, in light of the limited activities in progress, the

maintenance observed was performed in an acceptable manner with adequate

resources and oversight, and with appropriate consideration for safety.

5.3

Engineering

The team discussed engineering efforts in progress and readiness for startup

with the engineering staff. For the issues discussed, the engineering

deliberations were thorough and conservative with regard to achieving complete

18

and final resolutions. Nuclear engineers were prepared for startup having

identified personnel assignments, training, and the procedural approach to

startup testing. It was noted however, at the time of the inspection, that

engineering was involved in resolving several significant operability issues

the licensee had identified. The issues were being appropriately identified,

discussed, and evaluated for corrective action.

5.4

Radiological Services

During the inspection, Radiological Services Department {RSD} performance

during the refueling outage was assessed and RSD plans for supporting start-up

activities evaluated.

In addition, the RSD plan for responding to the

presence of fuel in the primary coolant and corresponding systems, once start-

up activities begin, was reviewed. Conclusions drawn were based on interviews

with RSD management and involved personnel, observations of work activities in

radiologically controlled areas and reviews of pertinent documents.

The RSD participation in the outage had four specific elements, each of which

was assessed during the inspection.

RSD planning and scheduling activities both before and during the

outage were excellent. Jobs were performed on schedule and the

RSD had ample staff to provide coverage when needed.

Even after

the master schedule was changed, following the stuck control rod

incident and the discovery of a failed fuel pin, the RSD planners

were able to plan new work requests in a timely manner and work

with the schedulers to insure that critical jobs were not delayed .

RSD pre-job briefs needed improvement.

Interviews with

individuals who had attended pre-job briefs indicated that there

were numerous distractions {doors opening and closing, people

talking and phones ringing} in the areas were the briefs were held

and the quality of the presentation was dependent on the

technician giving the brief. Prior to the inspection, the*RSD had

, been made aware of the deficiencies and had taken steps to correct

them.

The RSD tried to find quieter areas to hold the briefs and

had developed a check-off sheet to be used by the presenter to

insure that all the relevant information was passed on to the

worker during the brief.

Radiation safety technician performance during the outage was

generally very good.

The technicians appeared to be technically

competent and well trained. There were, however, problems with

contractor technicians setting poor examples for other workers .. A

Nuclear Performance Asses.sment Department {NPAD} survei 11 ance

reported that a number of contractor technicians had used poor *

radiological practices. Those practices included improper

placement of dosimetry and wearing scrubs in areas where scrubs

were not allowed.

The poor practices were brought to the

attention of RSD management and immediate corrective action was

taken.

The surveill~nce concluded that, in general, technicians

19

did a good job of-keeping workers informed of radiological

conditions, providing advice about radiological conditions, and

controlling access to various radiological areas.

The inspectors

who had worked with the RSD technicians during the inspection

concurred with this conclusion.

Post-job briefs were held in accordance with station procedure and

appeared to be effective.

In conclusion, the RSD performance during the outage was effective. The one

deficiency identified during the outage, pre-job briefs, had been noted by the

RSD and corrective action had been taken.

Following the discovery of a broken fuel pin in the Reactor Cavity Tilt Pit,

the RSD developed a RSD Fuel Failure Response Plan to identify, track the

status of, and document RSD actions taken as result of the fuel failure.

The

plan was a living document and once completed would document the basis for the

program .wit~ regard to failed fuel.

The plan contained assumptions made about

the risks associated with failed fuel and detailed the organizational

structure for implementing the plan. Actions within the plan were assigned to

specific individuals and target dates were set for completing the assigned

tasks. Of the more than 56 action items identified in the plan a number were

directly related to RSD start-up activities and RSD plans for tracking data *

points to indicate failed fuel in the future.

Those actions directly related

to start-up activities included:

Review and revision of the whole body counter's (Fast Scan)

library to accommodate fuel material

Reevaluation of the frequency of surveys during start-up and

normal operations

Reviewed derived air concentration (DAC) calculation and skin dose

methodology to account for new fuel nuclide mix

Evaluation of TLD (Panasonic) algorithms for response to the

presence of fuel

Evaluati~n of PCM-lb (Personnel Contamination Monitor), PM-7

(Portal Monitor) and frisker energy distribution of calibration

sources

Tr~ining the-RSD staff in preparation for start-up activities

The whole body counter, PCM-lb and PM-7 and DAC evaluations had been performed

and completed.

The RSD decided to increase the frequency of surveys during

start-up activities, electronic dosimeters would be posted in critical areas

throughout the plant and the data collected every four hours during start-up.

Following start-up the electronic dosimeters would stay in place and the data

they supply tracked .

20

RSD plans for tracking data points for an indication of failed fuel included:

Part 61 samples were collected and sent to the licensee's vendor

laboratory for analysis. Future analyses would be tracked for the

presence of fuel.

The hot spot program was reevaluated to include the possibility of

finding fuel fragments.

Criteria for determining when to perform

gamma spectral analyses on newly discovered hot spots would be

developed.

That evaluation was due to be completed by October 31,

1993.

The licensee would review the data collected from personnel

contamination incidents, whole body counts, air samples, and

massilin survey smears to determine if it could be used in the

future to indicate fuel failure. That evaluated is due to be

completed by October 31, 1993.

In conclusion, the response plan was comprehensive in scope and provided a

good basis for integrating the RSD response to operational events during

start-up activities and implementing plans for tracking various parameters

during normal operations for the presence of failed fuel.

The RSD appeared

fully prepared to support the facility during start-up activities.

The Nuclear Performance Assessment Department performance during the outage

with regard to the RSD activities was also assessed.

One surveillance and a

number of Field Manito~ Reports were reviewed.

Following field assessment

activities, NPAD assessors issue Field Monitor Reports to report their

findings.

If deficiencies are noted during the assessment they are recorded

in the department's database and the NPAD director meets with the plant

manager once a week to discuss the previous week's findings.

If a deficiency

warrants management attention the assessor will normally issue a Deficiency

Report. A review of the weekly reports indicated that while many of the*

deficiencies identified during the assessments had been brought to

management'~ attention, none of them had been documented in the RSD deficiency

reporting system (radiological deficiency reports).

NPAD uses its database to record deficiencies and track corrective actions.

In principle the RSD is responsible for correcting its own deficiencies,

however, if those peficiencies are not reported in the RSD system NPAD assumes

that responsibility. For example, during th~ dutage NPAD conducted a

surveillance to assess health physics technician performance during backshift.

In general, the assessors found that the technicians had demonstrated good

performance, however, several technicians were*observed using poor

radiological practices.

In the surveillance, NPAD reported that the RSD had

been informed of the observed practices and had taken corrective action.

The

deficiencies, however, had not been documented in the RSD deficiency system

and plant management had not been given a copy of the surveillance.

Under

this system NPAD, not the RSD, had been responsible for insuring that the

deficiencies had been corrected and the actions taken documented.

This was a

weakness in the program .

21

In summary, the RSD performance during the outage was good to excellent. The

pre-job briefs needed improvement and steps were taken to require use of the

briefing check list. The RSD had developed a comprehensive plan in

preparation for start-up activities and the plan provided a good basis for

supporting those activities. The NPAD system for reporting deficiencies and

documenting corrective actions needed improvement.

5.5

Trial installation of the UGS

The licensee decided to perform a trial insertion and removal of the UGS to

demonstrate successful removal of the UGS without a fuel assembly.

This.

action was also used to demonstrate/identify the interaction of the UGS with

the fuel assemblies and the core support barrel by closely monitoring this

activity with underwater cameras.

The licensee performed the trial insertion

and removal on August 21 and August 22, 1993, respectively.

The inspectors

observed both the insertion and removal activities. The observations are

addressed below.

The inspectors observed the upper guide structure {UGS) set onto the core on

August 21, 1993, and also the lift from the core on August 22, 1993.

Both

activities were performed in accordance with the applicable sections of

procedure RVI-M-12, "Final 1993 Installation of Upper Guide Structure."

The inspector attended the pre-job brief for both activities. The briefs were

comprehensive, and covered the procedure steps that were to be performed in

detail. The inspector verified that all personnel with assigned

responsibilities were present .

Proper radiological protective meaiures were established for personnel once

inside containment.

Proper dosimetry and protective clothing were worn by

each indivjdual, and coverage by the radiation protection technician assigned

to monitor the job was good.

The inspector observed that proper communications were established ,between the

control room and the senior reactor operator/shift supervisor directi.ng the

evolutions from containment.

Cameras, lights, video equipment, and other

measuring devices were properly aligned and _staged.

The actual lift evolution was satisfactory. The UGS was lifted to the six

inch elevation above the t6p of the fuel assemblies and hel~ for data

gathering and visual inspection. During the lift, the fuel alignment plate.~n

the bottom of the UGS was monitored for attached fuel assemblies and none were

observed.

Particular attention was paid to core location Z-11.

The lift of

the UGS was smooth and no swaying or tilting of the UGS was observed.

Levelness of the UGS was checked acceptable.

The load cell indicated that the

UGS was within its expected weight.

The UGS*was then lifted to the three foot elevation and a thorough camera

inspection was performed to verify that there were no attached fuel

assemblies.

Following this inspection the UGS was transferred to its storage

location and set on its pads with no apparent problems .

22

No violations, deviations, unresolved or inspector followup-items were

identified .

6.0

Evaluation of the Fuel Lost from the 1-24 Assembly

The Palisades Nuclear Power Plant experienced a fuel failure in assembly 1-24

at core location 819 during cycle 10 of operation. This failure resulted in

significant fuel loss from one fuel rod to the primary system during operation

and additional fuel loss from this rod during handling of the 1-24 assembly

during the outage.

The purposes of this inspection were to 1) evaluate the

licensee's efforts to find the missing -900 g of U02 from the failed rod, 2)

evaluate the loose parts in the primary coolant, and 3) evaluate the

licensee's ability to detect fuel failures during cycle 11 operation ..

6.1

Search For Missing Fuel

Higher than normal activities were found on primary system and core components

but these activities account for only 6 to 7% of the total fuel lost frQm

assembly 1-24. The core was examined to the maximum extent possible without a

full core off-load.

The reactor cavity tilt pit was where the failed fuel rod was stripped from

the assembly during the fuel handling operations. However, a significant

quantity of the fuel may have been lost from the fuel rod prior to its

transport to the tilt pit. The bottom of the tilt pit was examined, however,

a thorough visual examination was not possible because of hoses and machinery

at the bottom of the pit. The licensee intends to drain the pit to a lower

water level and see if they can find fuel fragments with activity detectors.

The tilt pit was vacuumed and drained after the rod was stripped from the

assembly in the tilt pit. A survey of the filters following this first

vacuuming of the pit resulted in higher than normal activity levels but only

accounted for less than 1% of the lost fuel.

The majority of the piping

{>90%) that leads from this drain was surveyed and while some small increases

in activity were noted they were not at the high levels expected if large

fragments ~f fuel were present. However, the less than 10% of piping not

surveyed was located in concrete nearest the drain location.

From the piping

surveys, and surveys of the filters from three separate vacuuming efforts on

the bottom of the tilt pit, less than 1% of the total fuel loss had been

accounted for in the tilt pit.

The team concluded that it was not likely that the licensee would find

significant additional quantities of the missing fuel.

The fuel appeared to

be efther hiding in inaccessible locations in the primary system, the drains

of the reactor cavity tilt pit and the adjacent spent fuel pool, or, more

likely, a combination of the above.

6.2

Loose Parts in the Primary Coolant

There are parts missing from the failed fuel assembly that are either in the

primary system or in the reactor cavity tilt pit.

Among the missing parts are

1) a half diameter piece of cladding approximately 20-inches in length,

2) three to four pieces of the spacer grid including a lantern spring {each is

23

estimated to be less than an inch in length and less than one-half inch in

width), and 3) an insulator disk (approximately the size of a fuel pellet) .

These loose parts have the potential of causing further fuel failures due to

debris fretting if they reside in the primary system.

They may also contrib-

ute to damage of other primary system components.

However, historically,

debris in the primary system has primarily been a fuel failure problem rather

than significantly impacting other components.

It should be noted that of

201 fuel assemblies in the cycle II core, 136 assemblies are debris resistant

assemblies by design.

6.3

Ability to Detect Fuel Failures in Cycle II

If a significant quantity of the fuel missing from the failed rod (>10%)

resides in the reactor coolant system, the ability to detect further fuel

failures will be hampered.

The licensee had significantly improved their

failed fuel detection capabilities for cycle II operation.

They expanded

their activity measurements to include additional radioactive isotopes that

help in identifying fuel failures with high tramp (background) activity

levels. The licensee has also improved their analytical capabilities.

Even

with these increased measurements and capabilities the licensee will most

likely have difficulty in detecting any small failures from a small number of

failed rods; however, they will be able to detect fuel failures with large

defect sizes such as those experienced in cycles 9 and 10.

These were well

below Technical Specification limits.

The licensee had an action plan for addressing increased coolant activity

levels. However, this plan left out some of the actions recommended in EPRI

report EPRl-NP5521.

In addition, the highest activity level that can be

achieved before the licensee will consider shut down, or derating, was close

to the Technical Specification limit for coolant activity. These action

levels were being reevaluated by the licensee.

No violations, deviations, unresolved or inspector followup items were

identified in this area.

7.0

AIT Report Findings Compliance Review

A review was conducted to evaluate findings of the NRC Augmented Inspection

Team (All), as documented in Inspection Report 50-255/93018(DRS)~ against

applicable regulatory requirements.

The review identified a number of

examples of noncompliance with requirements. These are discussed further

below, organized by their applicability to the three broad conclusions reached

by the All.

7.1

The Licensee's Organization Had a Less than Questioning Attitude

Operating Cycles 10 and 11 involved the use of previously burned fuel

assemblies (from the I-series fuel) to provide reactor vessel neutron flux

reduction shielding. At the beginning of Cycle IO, the I-series assemblies

had operated three full fuel cycles. The licensee had little or no experience

operating fuel assemblies beyond three cycles. A review of the proposed

extended use of I-series bundles was performed pursuant to 10 CFR 50.59. This

24

review was required to fully consider whether the proposed action involved any

Unreviewed Safety Questions (USQ).

The conditions of the proposed use

involved placing the assemblies at the periphery of the reactor core, where

the neutron exposure spectrum (and other parameters) were different from other

core locations.

In particular, the neutron spectrum at the periphery of the

core was proportionally higher in "fast" neutrons and lower in "thermal"

neutrons compared to non-periphery locations. A full consideration of the

potential that a USQ might be involved required that the effects of the unique

neutron spectrum on the I-series assemblies be specifically evaluated.

The licensee's documented 50.59 analyses did not include consideration of the

effects of the unique neutron spectrum on the I-series assemblies.

Those

analyses were therefore incomplete.

The written safety evaluation for the

subject use of the I-series assemblies did not provide complete bases for the

determination that there was no unreviewed safety question.

This is an

  • apparent violation of 10 CFR 50.59.(b)(l}, which requires such written bases

(Violation 50-255/93020-02).

During Cycle 10, it became apparent that fission products and transuranics

were present in the primary coolant.

The licensee did not have or develop

procedures to evaluate this condition with such scrutiny as. to correctly

identify the root cause.

The cause was ascribed to "tramp" uranium/fuel left

in the coolant from fuel cladding failures during the previous cycle, Cycl~ 9.

This was not correct.

As a consequence of failure to identify that a low power peripheral fuel rod

had failed in service, the fuel was not inspected for damage after Cycle 10 .

The damage to fuel assembly 1-24 was not detected, and the assembly was

returned to the reactor for Cycle 11.

Utili~ation of primary coolant radiochemistry testing procedures which did no~

assure that reactor fuel was performing properly in service, is an apparent

violation of 10 CFR 50, Appendix B, Criterion XI, "Test Control"

(Violatitin 50-i55/93020-03a).

7.2

Conservative Decisions were not Made When Warranted

As noted above, the I-series fuel assemblies were not inspected between

Cycles 10 and 11.

This was despite radio-chemistry evidence of fuel in the

primary coolant system and despite the fact they were the oldest assemblies in

the reactor.

Furthermore, the I-series assemblies were known to have been

fabricated with grid straps which were susceptible to relaxation due to strap

growth from prolonged exposure to radiation. This potential relaxation would

impose a risk of fuel pin vibration and fretting against the grid strap, which

could damage the cladding of the pin. This is potentially what occurred.

Failure to verify by test or inspection that I-series fuel assemblies would

perform acceptably in service after five previous cycles in the reactor is

another apparent violation of 10 CFR 50, Appendix B, Criterion XI, "Test

Control" (Violation 50-255/93020-03b) .

25

When the Upper Guide Structure (UGS) was lifted from the reactor on July 6,

1993, and a fuel bundle from core location Z-11 stuck onto the UGS, it marked

the third occurrence of this problem.

Root cause analyses and corrective

actions for the previous events failed to prevent recurrence.

Following the

event of September 3, 1988, no corrective actions were taken with respect to

the alignment pins. After the event recurred on February 29, 1992, the

alignment pins at location Z-11 were determined to be bent and they were

straightened.

Procedure changes were made to provide protection for the

alignment pins during handling of the UGS, so they would not become bent

again.

These changes failed. After the event of July 6, 1993, the alignment

pins were found to be bent once more.

The pins have now been replaced and a

series of actions taken to eliminate more potential causes of pin damage, as

well as other potential causes of interference between the UGS and the fuel.

Failure to preclude repetition of interference between core components, which

caused fuel mishandling events, is an apparent violation of 10 CFR 50,

Appendix 8, Criterion XVI, "Corrective Action" (Violation 50-255/93020-04).

7.3

Management Expectations were not Effectively Applied

Controls which were developed for the lift of th~ Upper Guide Structure (UGS)

were not positively and effectively applied.

The load cell equipment used for

the lift on July 6, 1993, was not the equipment specified by the applicable

procedure, No. RVI-M-1, Revision 16, "Removal and storage of the Upper Guide

Structure."

The procedure specified a Tl-2000 load cell but a J-300 device was actually

used.

A procedure stipulation (Section 5.3.6.g) to follow Work Order No.

24301781 for steps to use the load cell was violated in that the readout

device was not zeroed as required by step 3.3.A.7.

In addition, the specified

upper load limit of 62,000 pounds (Section 5.3.14) was exceeded by the

indicated load of 62,800 pounds after the UGS was raised about six inches. A

licensee supervisor was present during this evolution and did not intercede

effectively to enforce compliance.

Failures to implement requirements of the UGS lift procedure as described

. above are apparent examples of violations of Technical Specification 6.8.1.b

(Violation 50-255/93020-05a).

The activities associated with recovery of the fuel assembly which stuck to

the UGS on July 6, 1993, though successful in safely returning the assembly to

the reactor without damage, were not positively controlled in all respects.

Specifically, the RWP and procedure FHS0-18, "Recovery of Bundle SAN-8" were

not properly implemented.

The limitations of procedure FHS0-18 steps 4.2.6

and 5.2.1, in instructing that chainfall tension be limited to a combined load

of 1500-1600 pounds, were violated.

The chainfalls were tightened to a

combined load of 2300 pounds.

Failure to implement requirements of the stuck fuel assembly recovery

procedures as described above are an additional apparent example of violation

of Technical Specification 6.8.1.b (Violation 50-255/93020-05b) .

26

Seven apparent violations, some involving more than one example, were

identified.

No deviations, unresolved items, or inspector followup items were

identified.

8.0

Public Meeting on September 9. 1993

A public meeting was held between managers of Consumers Power Company and the

NRC on September 9, 1993.

The meeting was held in the Holiday Inn, Route 94,

in Benton Harbor, Michigan.

The NRC was represented by Hubert J. Miller,

Deputy Regional Administrator of Region III and members of his staff, and

James G. Partlow, Associate Director for Projects for the Office of Nuclear

Reactor Regulation, and members of his staff. Consumers Power Company was

represented by David Hoffman, Vice President for Nuclear Operations, Gerald

Slade, General Manager of the Palisades Plant, and members of his staff. The

purpose of the meeting was for the licensee to present the results of the root

cause assessments done for the damaged fuel bundle 1-24 and the fuel bundle

lifted with the UGS.

Mr. Miller opened the meeting, the licensee made the

presentation, then Mr. Miller closed the meeting and responded to questions

from the public.

Licensee representatives also remained to respond to

questions.

9.0

Exit Meetings

Interim exit meetings were conducted with licensee representatives* on

August 21, 1993, and August 27, 1993. A final exit was conducted

September 29, 1993.

The first exit was by the team of inspectors reviewing

the cycle 11 core reload safety evaluation.

The second exit interim was by

the team which observed routine activities. The final exit summarized the

results of the NRC review of the AIT findings for regulatory issues. The

inspectors summarized the scope and findings of the inspection.

Tbe licensee

acknowledged the statements made by the inspectors,

The inspectors also

discussed the likely informational content of the inspection report with

regards to documents and processes reviewed by the inspectors during the

inspection and the licensee did not identify any such documents or processes

as proprietary .

27

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CORNER ALWAYS POSITIONED TO BE AT THE CORE SHROUD CORNER.

Figure 1 - Revised L~assembl y for Cycle _11 *

Figure i

Revised

CYCLE II CORE PLAN

PALISADES NUCLEAR PLANT

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23

Batch 0: New Fuel 14 Batch N: Once Burnt rt SAN: Once Burnt

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SAN assemblies contain Stainless Steel pins

Cycle 11 Core Plan uses ~ core rotational symtnetry

Figure 2 - Revised Cycle 11 Core Design

E