ML20059C241

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AIT Insp Rept 50-271/93-81 on 930910-14.Major Areas Inspected:Plant 930903 & 09 Fuel Handling Incidents
ML20059C241
Person / Time
Site: Vermont Yankee File:NorthStar Vermont Yankee icon.png
Issue date: 10/05/1993
From: Beall J, Durr J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20059C243 List:
References
50-271-93-81, NUDOCS 9311010065
Download: ML20059C241 (20)


See also: IR 05000271/1993081

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.U.S. NUCLEAR REGULATORY COMMISSION

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REGION I

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Docket No.

50-271

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Report No.

50-271/93-81

License No.

DPR-28

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Facility Name:

Vermont Yankee Nuclear Power Plant

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Inspection At:

Vernon, Vermont

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Inspection Conducted:

September 10-14, 1993

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inspectors:

G. West, Jr., Engineering Psychologist, NRR

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T. Shedlosky, Project Engineer, DRP

P. Harris, Resident inspector, DRP

A. Burritt, Operations Engineer, DRS

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Observer:

W. Sherman, State of Vermont

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Team Leader:

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Beall, Team Leader

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ineering Branch, DRS

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Approved By:

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Dafe

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J. P. gurr, Chief,

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Engineering Branch, DRS

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Inspection Summary:

See Executive Summary

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9311010065 931021

PDR

ADOCK 05000271'

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TABLE OF CONTENTS

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EXECUTIVE SUMMARY

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1.0

INTRODUCTION

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1.1

AIT Scope and Obj ectives . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . I

1.2

AIT Process

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2.0

DESCRIPTION OF THE EVENTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

3.0

PERSONNEL PERFORMANCE AND REFUELING OVERSIGHT

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3.1

Training . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

3.1.1 Operator Training Prior to September 3,1993 . . . . . . . . . . . . . 3

3.1.2 Reactor Engineer Training Prior to September 3,1993 . . . . . . . . 4

3.1.3 Operator / Reactor Engineer Training rollowing the

September 3,1993 . . . . . . .

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3.2

Fuel Handling Procedure . . . . . . . . .

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3.2.1 Procedure Adequacy . . . . . .

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3.2.2 Fuel Handling Steps

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3.3

Personnel Performance . . . . . .

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3.3.1 Reactor Engineers

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3.3.2 Refueling Platform Operators . .

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3.3.3 Senior Reactor Operators .

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3.4

Management Oversight . . .

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3.4.1 Procedure Usage

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3.4.2 Communications

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3.4.3 Fuel Movement Briefings . .

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3.4.4 Schedule

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3.4.5 Refuel Staffing and Overtime .

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3.4.6 Management Oversight of Fuel Handling

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4.0

REFUELING BRIDGE FUEL HANDLING EQUIPMENT DESIGN

CHANGES

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4.1

Fuel Grapple Replacement . . . . . . . . . . .

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4.2

Refuel Platform Upgrade

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4.3

Refueling Platform Hoist Interlock Modification

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MAINTENANCE AND TROUBLESHOOTING OF REFUELING

EQUIPM ENT . . . . . . . . . . . . . . . . . . .

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Table of Contents

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HUMAN FACTORS REVIEW

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6.1

Human-System Interfaces

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Human Factors Weaknesses . . . . . . . . . . . . . . . . . . . . . . . . . . . .

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6.3

Conclusion

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7.0

LICENSEE CORRECTIVE ACTIONS

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S AFETY SIGNIFICANCE . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

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C O N CLU S I ON . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

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10.0 M AN AG EMENT MEETING S . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

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ATTACHMENT 1 - NRC Augmented Inspection Team Charter

A'ITACHMENT 2 - Persons Contacted

ATTACHMENT 3 - Sequence of Events for the Vermont Yankee Refueling Incidents

ATTACHMENT 4 - Human Factors Weaknesses

ATTACHMENT 5 - September 3,1993: Post-Event Radiological Summary

ATTACHMENT 6 - Slides Presented at September 21,1993 Public Exit Meeting

FIGURE 1 - Grapple Up and Down Control

FIGURE 2 - Refueling Bridge Control. Console

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EXECLTf1VE SUMMARY

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On September 3,1993, at about 12:30 p.m., Vermont Yankee personnel inadvertently

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dropped a fuel assembly approximately eight feet back into its reactor core location during

fuel handling activities. At the time, the plant was shutdown in a refueling outage with about

one-third of the planned fuel moves already completed. On September 7,1993, the licensee

resumed fuel handling activities after completion of troubleshooting, implementation of

corrective actions, and discussions with tne NRC. On September 9,1993, a second fuel

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handling incident occurred when operators inadvertently lowered a fuel assembly onto a core

component. After the second incident was reported, the licensee suspended further fuel

handling.

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An Augmented Inspection Team (AIT) was dispatched by the NRC to determine the

circumstances that led to the events, their causes, safety significance and generic

implicaGons. The AIT began its assessments on September 10,1993, completed its onsite -

review on September 14,1993, and presented its preliminary findings in a public exit

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meeting on September 21,1993.

Errors by operators were the immediate causes of the events. The preponderance of the

physical evidence indicated that the grapple had not properly closed on the fuel assembly

handle and that the grapple light had not energized resulting in the drop of the assembly on

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September 3,1993. The September 9,1993, event was an inadvertent operator performance

error. Human factors weaknesses contributed to the error in lowering rather than raising the

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fuel assembly. The team concluded that the fuel handling incidents had been appropriately

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mitigated by the systems operable and the existing plant configuration, and were,

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independently, of minor safety significance.

The team concluded that the root cause of the dropped fuel assembly event was a significant

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weakness in management oversight of fuel handling activities. Weak management oversight

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had allowed many of the measures intended to prevent a fuel handling accident to become

degraded. The AIT found that design changes were not transmitted to allow timely and

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accurate training on the modifications; training was not effective in that operators were not

aware of certain key procedure steps; procedures were not used and were not adhered to; and

supervisors did not ensure that procedures were followed. Management did not communicate

expectations and provide proper oversight of fuel handling activities.

The decision by the senior reactor operator to continue the planned move of the assembly

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which had, on September 9,1993, inadvertently been lowered onto a core component was

not in compliance with the licensee's fuel handling procedure. This procedure compliance

error was not identified by licensee line management or by the licensee's event investigation.

This was indicative of a weakness in corrective actions to the September 3,1993, incident

and a continued weakness in management oversight of fuel handling activities.

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DETAILS

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1.0

INTRODUCTION

Upon being informed of the fuel handling incidents on September 3 and 9,1993, at the

Vermont Yankee Nuclear Power Station, the NRC Region I Regional Administrator and

senior management from the Office of Nuclear Reactor Regulation (NRR) and the Office for

Analysis and Evaluation of Operational Data (AEOD) determined that an augmented

inspection team (AIT) should be formed to review the circumstances and evaluate the

significance of the events. The bases for the determination were the need for the NRC to

fully understand the causes of the events and to determine if these were associated with

generic issues which required further NRC action. Accordingly, an AIT was selected,

briefed, and dispatched to the site on September 9,1993.

1.1

AIT Scope and Objectives

The charter for the AIT (Attachment 1) was finalized on September 9,1993. The charter

directed the team to conduct an inspection and to accomplish the following general

objectives:

Develop a detailed sequence of events related to both events, from September 3

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through 9.

b.

Determine the specific circumstances and causes of the apparent operator errors that

occurred during refueling operations on September 3 and 9,1993.

Determine and evaluate any changes (specifically Plant Design Change 92-11

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implemented in Spring 1993) made in the design, maintenance, testing, or operation

of the refueling bridge including hoist, grapple, and operator controls. Also, included

was associated training for such modifications.

d.

Evaluate the human factors aspects of both events, including: 1) command ano

control, and communications; 2) human performance factors, such as staffing,

overtime, and schedule; and 3) human-systems interfaces, such as with console

design.

Assess the safety significance, including existing damage to the affected fuel

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assemblies.

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Determine the adequacy of Vermont Yankee's maintenance and troubleshooting

practices for refueling equipment, including vendor interface and control.

Evaluate Vermont Yankee's corrective actions and management controls following the

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September 3rd event, as they relate to the second September 9th event, particularly

on-the-job training.

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AIT Process

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During the period September 10 - 14, 1993, the AIT conducted an independent inspection,

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review, and evaluation of the conditions and circumstances associated with the events. The

team inspected fuel handling, equipment, and controls; held discussions and formal

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interviews both with personnel involved in the event and others performing the same duties;

reviewed relevant records, including operator logs, modification packages, and training

documents; and evaluated the adequacy of established procedures, personnel training, and

management oversight. Attachment 2 is a list of personnel contacted by the AIT.

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DESCRIPTION OF TIIE EVENTS

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On August 27,1993, the licensee initiated a reactor shutdown and entered a refueling outage.

On Septen'ber 1,1993, the licensee commenced the first of (about) 700 planned movements

of fuel assemblies necessary to refuel the reactor. On September 3,1993, during fuel move

number 233, one fuel assembly became detached from the grapple while being lifted out of

the reactor core. The assembly fell an estimated 8 feet back into its original location. Some

assembly damage and a small radioactive release occurred.

The licensee suspended fuel handling, notified the NRC, and investigated the event. After

the licensee completed their investigation and implemented certain corrective actions, fuel

handling was resumed with NRC concurrence.

On September 9,1993, during fuel mon number 388, a fuel assembly was inadvertently

lowered, instead of raised, resulting in an apparent impact with another assembly or

component in the core. The potentially damaged assembly was then moved to a fuel sipping

can, as originally planned. The licensee reported the event, suspended fuel handling

activities, and the NRC dispatched an AIT to investigate the fuel handling incidents.

A chronology associated with the fuel handling incidents is contained in Attachment 3.

3.0

PERSONNEL PERFORMANCE AND REFUELING OVERSIGIIT

The AIT assessed the preparation, performance and practices associated with core

alterations / fuel movement prior to, between and after the two refueling events. The findings

of the team are grouped into four categories: Training, Procedures, Personnel Performance

and Management Oversight.

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3.1

Training

3.1.1 Operator Training Prior to September 3,1993

Prior to the refueling event on September 3,1993, all operations personnel received specific

refueling training as a part of the normally scheduled continuing training cycle. The training

was provided to licensed operators and non-licensed Auxiliary Operators. The training,

conducted during the six week period between June 29,1993 and August 6,1993 was one

and a half hours in length. All operations personnel attended the normally scheduled training

except for two who completed a read and sign package on refueling operations as a make-up.

An outline in lesson plan LOT-00-234H, Revision 8 (06/93), was used to guide the training

provided on refueling. The outline specified a discussion of vessel disassembly, refuel

outage tests, planned modifications to the refuel bridge along with a review of the listed

licensed operator objectives. Although, one of the objectives required the use and/or

understanding of procedure 1101, the objective did not provide clear performance

expectations regarding the level of understanding. The lesson plan included a memorandum

on the scope of PDCR 92-011, " Refuel Platform Upgrades." The memorandum stated that

the main hoist controls would be replaced but did not provide any details about the new

controls. The figure of the main hoist controls in the lesson plan was not the same as the

controls installed at the beginning of the outage. The training occurred prior to the controls

being replaced.

Based on interview data, procedure 1101, " Management of Refuel Activities and Fuel

Assembly Movement" was discussed in class with emphasis on the administrative limits and

duties and responsibilities sections. The body of the procedure was briefly reviewed with

particular attention to notes and cautions. The instructor did not specifically discuss the

procedure steps or procedural adherence.

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Instruction provided to cover the objectives for requalification training, by practice is left to

the discretion of the instructor. Although the training provided was generally considered to

be adequate based on interviews, there was no documentation of what was covered in class

as well as no assurance that the same information was presented from one class to the next.

On The Job Training (OJT) by either demonstration or hands on practice was not provided

prior to the September 3,1993 event. This training was not considered on the basis that it

had not been done in the past for requalification training. Although the personnel involved

in refuelling generally had a significant amount of fuel movement experience, some

individuals interviewed felt hands on practice was necessary. Since core alteration fuel

movements are done infrequently, the team concluded that it would be a good practice to

renew manipulative skills under non-safety significant conditions, particularly following the

modification of equipment, indications and controls.

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Training practices prior to the September 3,1993, event were weak. This assessment is

based on the absence of OJT prior to refueling and the results ofinterviews. Through

interviews, the AIT determined that most of the operators were not aware of certain

important procedural requirements and routinely had not performed all the required steps

during fuel movement operation.

3.1.2 Reactor Engineer Training Prior to September 3,1993

Prior to the refuel outage the reactor engineers were provided a number of training sessions.

One of these sessions was given using an informal 5 page briefing sheet. The intent of this

training was to review refueling goals, various procedural requirements along with refuel

contingency plans with the reactor engineers providing fuel movement support. The " Things

to remember when moving fuel" section contained a specific discussion that the reactor

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engineer should verify the grapple close light to be on prior to lifting a fuel bundle.

The AIT did not review all the training and documentation for the instructional briefings

provided to the reactor engineers, but the team did confirm that the expectations to verify

grapple closure were clearly addressed.

3.1.3 Operator / Reactor Engineer Training Following the September 3,1993

Training immediately following the September 3,1993 event was performed as a part of the

facility corrective actions. The training consisted of a classroom session, a read and sign

package, and handsen OJT for the operators and reactor engineers.

The classroom training included a review and discussions of procedure 1101, " Management

of Refuel Activities and Fuel Assembly Movement," Revision 21, in detail. Although the

lesson plan had no specific objectives, it did clearly document the key points to be

emphasized and appeared appropriate for the circumstances. The training took approximately

3/4 of an hour to perform and was done prior to the OJT portion.

The read and sign package was provided to operations personnel on the revised procedure

1101, " Management of Refuel Activities and Fuel Assembly Movement," Revision 23.

The OJT consisted of moving the bridge and trolley to coordinates provided in the spent fuel

pool, grappling the bundle, performing the grapple engagement verifications including the

rotation check under load. All members of the refuel teams performed in their normal

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positions while practicing the direction and communications required.

Training provided following the September 3,1993, event was adequate. The team noted,

however, that although the controls were operated during the OJT portion of the training, the

changes in hoist speed and the effective reversal of switch motion compared to hoist direction

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were not addressed.

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3.2

Fuel llandling Procedure

3.2.1 Procedure Adequacy

The AIT reviewed procedure 1101, " Management of Refuel Activities and Fuel Assembly

Movement," Revisions 21,22, and 23. Although a number of enhancements were made in

each of the successive revisions, the team determined Revision 21 of the procedure to be

adequate for fuel movement with the main hoist.

The procedure provided expectations that the reactor engineer and the SRO were required to

visually verify grapple closure. Additionally, the reactor engineer and SRO verification step

was imbedded in the step to close the grapple. The procedure, Revision 23, required a more

directed evolution by the SRO as well as establishing additional verifications to ensure proper

grappling of a fuel bundle. The additional procedural barriers consisted of SRO verification

of proper grapple head orientation prior to engaging the grapple and redundant checks by the

reactor engineer and SRO to verify the grapple light was energized following grapple

closure.

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The procedure, Revision 21, ZZ axis (refueling hoist depth) counter reference values were

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incorrect. These reference points provide approximate relative height for key components

within the spent fuel pool and reactor core. The values had changed based on the installation

of a new ZZ axis indication system prior to the refuel outage. Although these levels

provided valuable operator informationf additional operator aids were in place, updated daily

and effectively ensured that the operator had the most up to date reference values.

The AIT identified specific weaknesses with procedure 1101, " Management of Refuel

Activities and Fuel Assembly Movement," Revision 21, but concluded that these weaknesses

did not significantly contribute to the September 3,1993 event. Further, Revision 23 of this -

procedure was assessed as adequate to perform fuel movements with the main hoist and

therefore was not a contributing factor in the September 9,1993 event.

3.2.2 Fuel IIandling Steps

Procedure 1101, Revision 23, directed operators withdrawing a peripheral fuel assembly to

withdraw it "to just above the core, move toward the center-core area, then fully raise" the

assembly. The licensee chose this method over the alternative, raising the assembly fully and

then moving toward the center, to reduce radiation levels in the drywell when handling fuel.

This allowed fewer restrictions on personnel access to the drywell; such restrictions could

increase the time to complete scheduled outage work.

Operators interviewed stated that it was their general practice to move all assemblies using

the method directed for peripheral assemblies. Most facilities similar to Vermont Yankee

restrict access as necessary and use the " full lift then move to center" approach for moving

fuel. The team did not conclude that the licensee's fuel handling steps were inadequate, but

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did note that the approach used significantly increased the chance that an inadvertent operator

error, such as occurred on September 9,1993, would result in a fuel assembly impacting a

core component. Using the more common fuel handling steps, an operator would have over

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30 feet of clearance to correct a mistake rather than the two to three feet (or four to six

seconds) available to operators.

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Personnel Performance

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3.3.1 Reactor Engineers

During the September 3,1993, dropped fuel assembly event, the reactor engineer was off the

bridge of the refueling platform performing other duties on the refueling platform floor.

Therefore, the reactor engineer did not follow the facilities Operating Procedure No,1101,

Revision 21, and verify grapple closure which stated: " Move the Grapple Open/Close

Switch to the CLOSE position, the SRO and the Reactor Engineering representative visually

verify grapple closure."

Operating Procedure 1101, Revision 21, indicated that the reactor engineer shall:

a.

watch for and notify the Senior Licensed Operator of any occurrence which may

potentially jeopardize safe refueling,

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ensure compliance with the Fuel: Loading Schedule,

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maintain tag boards on the refuel floor and place target tags on boards for operator

reference,

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assist the Senior Licensed Operator on the refuel floor,

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maintain the Refueling I.og (DP 0420).

The above duties placed conflicting organizational expectations by management on the reactor

engineer. When only one reactor engineer was assigned to a refueling shift crew, the

individual had duties that were both on the refueling platform bridge and on the refueling

platform floor. This conflict was a contributing factor to the dropped fuel assembly event.

The team concluded that, prior to the September 3,1993, event; the reactor engineers should

have been aware of all assigned responsibilities and identified conflicting duties to their

supervision.

Reactor engineer performance was good during the September 9,1993, inadvertent lowering

of the fuel assembly event. The reactor engineer quickly observed that the fuel bundle was

being lowered rather than raised, called to the refueling platform operator to stop, which

probably mitigated the consequences ~of the event,

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3.3.2 Refueling Platform Operators

The refueling platform operator involved in the dropped fuel assembly event reported that he

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verified grapple closure (i.e., observed that the grapple closed-light was on). Moreover,' the -

operator noted that he observed the change in state of the grapple closed light. The report

and observation by the operator were inconsistent with the preponderance of physical

evidence, which indicated that the grapple was not closed when raised. The team assessed

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the performance of the refueling platform operators to be poor prior to the

September 3,1993, event; the operators generally were not aware of the requirement to

perform a rotational check, which ensured proper engagement, after grapple closure. That :

rotational check, not done for the dropped assembly, was intended to detect improper

grappling and may have prevented the September 3,1993, event.

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The refueling platform operator engaged in the inadvertent lowering of the fuel bundle event

committed an error resulting principally from two reasons. First, the human factors aspect.

of the change to the main crane controls, a " joystick," was a contributing factor (see Section

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3.1.1). The operator had received no training on how to use the new joystick. The -

relationship between the motion of the joystick and control of the grapple was inconsistent

with his past experience and reversed the direction of control used in the previous outage.

Second, the way the licereee moved fuel, that is, initially raising each assembly 2-3 feet

above the core, next moving the bundle to the center of the core, and finally taking the

assembly full up, was also a contributor. This pattern provided an additional opportunity to

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commit an error of this type (see Section 3.2.2).

3.3.3 Senior Reactor Operators

The SRO's performance (specifically, command and control) during the dropped fuel

assembly event was unsatisfactory for several reasons. The senior reactor operator failed to

verify grapple closure and did not ensure that the reactor engineer, who was off the refueling

platform bridge, verified grapple closure. Operating Procedure 1101, Revision No. 21,

required the senior reactor operator and the reactor engineer to visually verify grapple

closure. Further, the senior reactor operator did not comply with the following step of the

subject procedure: " Verify the fuel assembly is grappled by: 1) attempting to carefully

rotate the control console one way then the other..." Thus, the senior reactor operator

lacked command and control not only because he failed to follow procedure, but also because

he did not require the shift crew to follow procedure.

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The SRO's performance regarding command and control was also unsatisfactory during the

inadvertent lowering of the fuel bundle event. After the fuel bundle was inadvertently

lowered, the SRO continued with the movement of the fuel bundle to the spent fuel pool.

This action was contrary to Operating Procedure 1101, Revision No. 23, which stated:

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If any off-normal condition or evidence of interference or binding of components in

the core develops, further operation in that area of the core shall be immediately

stopped and the problem investigated and corrected.

Fuel bundles not properly seated may be rescated. However, no fuel movement or

core alteratio;s shall be made to correct a damaged, mistoaded or misoriented bundle

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in the reactor until the R/CE Manager has been notified.

Halt any activity in the event of an unusual or abnormal occurrence. Once any

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activity has been halted, it may only be re-initiated by the Shift Supervisor after

receiving concurrence from the Operations Manager.

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Management Oversight

3.4.1 Procedure Usage

The facility did not have an administrative procedure or guideline that dictated the level o,f

use required for procedures. Based on interviews, the team was unclear on what the

management expectations were for use of procedure 1101, " Management of Refuel Activities-

and Fuel Assembly Movement." Prior to the September 9,1993, event, operators did not

use procedure 1101 during fuel handling, did not have it on the fuel bridge for reference

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purposes, and did not know it it was available on the refuel floor. Some operators thought it

was appropriate to have the procedure available on the refuel bridge for either step by step

referral or to reference it as needed, since there was a lot of information to remember.

However, the majority of personnel interviewed thought this was not necessary due to the

repetitive nature of fuel movement and due to housekeeping concerns while over the vessel

and spent fuel pool.

The AIT determined that clear management expectations did not exist for the required level

of use of refuel procedures. The team was concerned that lack of clear management

expectations may have created an environment in which refuel procedures routinely were not

used.

3.4.2 Communications

During interviews, the AIT determined that the SRO used a hand-held phone to maintain

communication with the control room during fuel movement within the core. Additionally,

the operator would use binoculars to observe fuel assembly placement. These two factors

would challenge the ability to hold and use the procedure. The team considered

communications to have been adequate, but noted that the current practice could inhibit

future in-hand procedure use on the refuel bridge.

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3.4.3 Fuel Movement Briefings

During interviews, the AIT determined that pre-job or pre-shift briefs had not been

conducted prior to fuel movements. The FSAR stated that "All supervisors shall hold

instructional briefings with members of their staffs prior to executing a refuel procedure in

the interest of safety and good power station practice," (FSAR Section 13.9.3). The failure

of shift supervisors or the refuel floor SROs to perform the briefings, represents a missed

opportunity to review and verify the understanding of key administrative and procedural

requirements to ensure safe refuelling practices. Based on interviews, the team concluded

that cognizant licensee managers had not been aware of the FSAR commitment.

3.4.4 Schedule

Based on interviews, the AIT determined that the refuel teams had felt no undue sense of

urgency or pressure from management related to fuel movement. All personnel interviewed

stated that there was a clear emphasis on "doing things right and safely." Additionally, there

appeared to be no competition between shifts that potentially could have compromised safety.

3.4.5 Refuel Staffing and Overtime

The AIT reviewed the plant staffing assigned to refueling activities and concluded that the

refuel staff size was appropriate for the conduct of safe refueling operations. A good

initiative was demonstrated by VY to atigment the number of senior licensed operators with

two individuals from the Training Department. However, the team concluded that the

staffing for refueling was inadequate during occasions when only one of the two reactor

engineers were on the refuel floor. During these occasions, the remaining engineer was

challenged to effectively perform all assigned duties and responsibilities because the

engineer's attention was divided between administrative requirements (maintenance of the

status board and refuel log) and refuel activities (grapple, hoist, and bridge operation). This

conflict contributed to the dropped fuel assembly event (see Section 3.3.1). Following the

event, two engineers were assigned to the refuel floor during refueling.

The team reviewed the hours of work for control room and refueling operators and

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concluded that the use of overtime was within licensee requirements and NRC guidance and

did not contribute to either event. The team verified that operators had received at least 8-

hours off between shifts and noted that 12-hour breaks were normally scheduled. Operators

interviewed by the team stated that they had had adequate rest and the team concluded that

there was no evidence that fatigue had contributed to either event. Based on a myiew of

time and attendance records, the team concluded that the licensee had effectively

administered operator hours.

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3.4.6 Management Oversight of Fuel IIandling

The team concluded that there had been little or no management oversight of fuel movement.

Operations management stated that there had been no management observations of fuel

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movement during the current outage. The quality assurance organization had not performed

any fuel movement surveillance since 1987.

4.0

REFUELING BRIDGE FUEL IIANDLING EQUIPMENT DESIGN CIIANGES

The team reviewed the details of design changes made to the refueling platform fuel handling

equipment over the past five years. During that period, the licensee completed three separate

activities intended to improve the performance of this equipment. The fuel grapple was

replaced in 1988 with an improved design with two independent hooks to carry the fuel

assembly. This year, modifications were made to improve the overall reliability of the

equipment by replacing the hoist and its controls and the other associated components such as

the refueling hoist depth (ZZ axis) monitoring and display. Following the

September 3,1993, dropped fuel assembly event, an interlock was added to the hoist upward

control circuit.

Modifications to the handling equipment controls had also occurred. Earlier training

illustrations depicted a " joystick" control on the operator console to control trolley movement

left and right, a second joystick for platform forward and reverse motion and a third for fuel

grapple hoist raise and lower. These three vertical joysticks were replaced with three

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horizontal rotary lever controls. These were operated, for example, by rotating the lever

clockwise toward the operator to raise the hoist and counter clockwise away from the

operator to lower the load.

4.1

Fuel Grapple Replacement

The original fuel grapple was replaced with a grapple of improved design in

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April - May 1988. The new grapple had redundant hooks that carried the fuel assembly

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handle. The two hooks operated independently, each actuated by its own air cylinder.

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Separate position sensing switches were operated by each of the two hooks. The switch was

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operated when its associated hook was fully engaged under the fuel assembly hand.Ie. The

switches were wired in series such that both had to be closed to illuminate the grapple closed

lamp located on the hoist operator's console.

The team reviewed the documentation for the grapple replacement contained in Plant Design

Change Request (PDCR) No. 87-03, " Fuel Grapple Replacement," and General Electric

Company Service Information Letter (SIL) No.181, " Redundant Hook Grapple Head." The

safety evaluation accompanying the design changes reasoned that the redundant hook grapple

had two hooks each with a factor of safety equal to or greater than the original single hook.

Also, the position sensing microswitches of the new grapple were believed to be more

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reliable than the proximity switch used in the original design.

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The team discussed the grapple design with vendor representatives. The redundant grapple

was designed such that a single component failure would not result in dropping a fuel bundle.

In regard to load safety factors, under normal conditions, the entire grapple assembly had a

safety factor of three, the primary hook a safety factor of 12, the secondary of 8.5 and the

shaft on which the hooks pivoted has a safety factor of 21. The redundant hooks were

configured such that it should not be possible for both to simultaneously hang up on a fuel

bundle. For example, one of the two hooks was 3/16 inch shorter that the other.

Additionally, the opening in the grapple head that accepted the fuel assembly bale handle had

been machined to provide 1/4-inch clearance across the handle width and 1/8-inch across its

thickness. When seated on the fuel assembly handle, the grapple hooks passed under the

handle with approximately 0.5 inch clearance. Additionally, the configuration of the grapple

closure sensing microswitches and their associated grapple hooks provided a positive

indication of grapple closure that was relatively insensitive to changes in switch position

adjustment. The team concluded that the grapple design provided a close tolerance fit with

the fuel assembly handle, and that the redundant hooks and their associated microswitches

provided good assurance of positive grapple operation.

During the 1988 installation, the licensee exercised an option and changed the vendor

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recommended design not to install an electrical interlock involving hoist upward motion.

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The design, as proposed by the vendor in SIL 181, provided an interlock to prevent upward

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hoist motion when loaded to approximately 480 pounds unless both grapple hook position

switches were closed indicating that the hooks were fully positioned under the fuel assembly

handle. During the design change review process, the licensee decided not to include this

electrical interlock because of their experience and the poor performance of the proximity

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switch in the old grapple. The interlock was not installed because of their concern that the

grapple might become inoperable if a microswitch failed.

4.2

Refuel Platform Upgrade

The licensee began the first phase of modifications intended to upgrade the reliability of the

refuel platform with PDCR 92-11. The work associated with this change was performed in

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the period of June 25 through August 19, 1993. The scope of these modifications was

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determined by a task force formed to review past problems with the platform and provide

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recommendations to improve reliability and performance. The equipment replaced included

the main hoist including the motor, drum, brakes, cable and controls, a new depth indicator

including a digital encoder and display, new electronic load cells and display with

programmable interlock modules, new air hoses and reels, a new air dryer and stainless steel

air lines, a new main power cable, a new access ladder and a new remote readout assembly

for the digital displays.

The team reviewed the design change documents including the safety evaluation, the design

change review comments, the completed procedure for shop tests of the hoist and controls,

and the installation and test procedure. The design change was routed within the licensee

staff for review and comment. Included on the routing were the operations and training

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departments. These documents described the various aspects of the modifications including

their operator interface aspects such as the type and location of new digital displays for main

hoist depth and main hoist load. The new hoist and its motor speed controller and associated

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joystick control were selected to provide the operator with better fine control of hoist motion.

The hoist was replaced primarily due to limitations on obtaining spare parts for the old hoist

mechanism.

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The design change document did not address the hoist direction in relation to joystick

movement, nor did it address the difference in control when replacing the rotary motion

controller with the joystick and the resultant differences to operations personnel. The

installation and test procedure for PDCR 92-11, Step 7.24.2, required operation of the main

hoist joystick and verification that the hoist rotated in the proper direction. It was necessary

to reverse motor leads to complete this requirement. Proper hoist operation was an attribute

that was verified as a third party quality control inspection.

The team concluded that the refuel platform modifcations resulted in an overall improvement

in the reliability of fuel handling equipment. However, the licensee did not seek design input

from operations personnel concerning modification of the operator interface components 'such

as controls and indication. The team also noted that the modification work was not

scheduled for completion early enough before the current refueling outage to allow hands-on

training of personnel prior to fuel movement.

4.3

Refueling Platform Holst Interlock Modification

The control circuit for the refueling platform main hoist was modified on September 6,1993,

by the licensee in response to the September 3,1993, event. The modification added an

electrical interlock that prevents upward movement of the hoist when loaded to greater than

approximately 450 pounds if both fuel grapple hooks are not fully closed. The installation

was accomplished as Temporary Modification (TM)93-053, and done under Work Order

No. 93-07052-04. The interlock installed was similar to that recommended by the vendor for

incorporation with the redundant hook fuel grapple (see Section 4.2).

The licensee modified the vendor recommended circuit after finding that a resistor in series

with the close grapple relay coil did not allow the relay to pick-up. A "b" contact in the

same relay was used to bypass the resistor and, therefore, allowed enough current to pass for

the relay to operate. The team concluded that the modification should be transparent to the

operator under normal circumstances. The grapple closed indicator lamp and main hoist load

cell operated in the same manner as before the rnodification.

5.0

MAINTENANCE AND TROUBLESHOOTING OF REFUELING EQUIPMENT

The team reviewed records of work requests and work orders for plant refueling equipment.

The team found that the licensee had been performing preventive and corrective maintenance,

applying appropriate priority to these activities.

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Under Work Order 93-07019-00, an inspection was made of the grapple, its hooks, and their

air cylinder operators and position indicating switches on September 5,1993, two days after

the dropped fuel assembly event. Other than air cylinder leaks, all components were

determined to be functioning properly. A small air leak was found at the lower air

connection to a cylinder, the other was found filled with water. The second cylinder was

replaced. The grapple hook position microswitches were found to be set to open with slight

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outward motion of the grapple hooks. In that condition, the grapple closed light would go

out as the main hoist mast was rotated to verify proper engagement with a fuel assembly

handle. The AIT was unable to determine the extent, if any, that the leaking air cylinders

contributed to the dropped fuel assembly; however, the licensee's investigation findings

discounted any contribution by the condition of the air cylinders to the event.

Work Order 93-07133-00 was written to adjust the microswitches and eliminate the

intermittent loss of grapple closure indication. This was performed on September 8,1993.

Although the team did not identify any concerns with technician performance, the team noted

that the work was accomplished without the benefit of a written procedure.

The licensee was unable to reproduce an incomplete grapple configuration with the grapple

light energized. The team concluded that the preponderance of the physical evidence

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indicated that the grapple light had not been energized during the September 3,1993, event.

The team noted, however, that the incomplete grapple configurations tested by the licensee

on smooth bar stock had not demonstrated sufficient gripping or pinching force to allow a

partial lift of a fuel assembly. The licensee stated that the assembly handle geometry, which

had a chamfered underlip. would have allowed more lift force to be transferred. The team

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considered the licensee's troubleshooting, completed about one week before the AIT

investigation, to have been adequate.

6.0

IIUMAN FACTORS REVIEW

The AIT reviewed the human factors aspects of both events regarding (a) human-system

interfaces with the refueling platform console and (b) human performance, including

ccmmand and control. In addition, human engineering deficiencies relative to the refueling

platform console that were not necessarily related to the two events were also identified.

6.1

Iluman-System Interfaces

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During the previous outage the control for the grapple was a lever switch. To raise the

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grapple, the lever switch would be pushed forward (see Figure 1). Prior to the current

outage (during August 1993), the lever switch was changed to a joystick. Although training

received information on this design change No. 92-11 (June 1993), refueling platform

operators (RPOs) received no training on how to use the new joystick. Funher, the

classroom training that was taught in preparation for the outage used a figure that

erroneously depicted the lever switch as the control for the grapple.

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The licensee indicated that the joystick was installed based on Occupational Safety and Health

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Administration (OSHA), American Society of Mechanical Engineers (ASME), and Crane

Manufacturers Association of America (CMAA) guidelines. OSHA 1910.179 section 3(iv)

states: " As far as practicable, the movement of each controller handle shall be in the same

general directions as the resultant movements of the load." CMAA Specification 70-1988,

Section 5.7.3, states: "The movement of each master switch handle should be in the same

general direction as the resultant movement of the load, except as shown in Figures 5.7.3a

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and 5.7.3b, unless otherwise specified." ASME B30.2-1990, Section 2-1.13.3(d), states:

"The movement of each manual controller or master switch handle should be in the same

general direction as the resultant movement of the load, except as shown in Figs. 6 and 7."

The licensee interpreted the above guidelines as a control panel in the horizontal plane. The

licensee considered the control console (shown in Figure 2) for the refueling platform to be

an incline plane design (i.e., about 30 degrees). Thus, the licensee installed and labelled the

joystick with the resultant load in the direction that would be appropriate for a fully vertical

plane design (i.e., forward motion is up and backward motion is down, as shown in

Figure 1). An alternate rationale would be to consider forty-five degrees to be the dividing

line for deciding whether guidelines should be applied for horizontal or vertical plane design.

In either case refueling platform operators should have been trained regarding the control

change for the refueling platform grapple.

6.2

Human Factors Weaknesses

The walkthrough, interview results, and desk top review of photographs relative to the

operation of the refueling platform console identified several additional human factors

weaknesses to the guidelines of Section 6 of NUREG-0700. The weaknesses are presented in

Attachment 4.

6.3

Conclusion

The team concluded that the human factors weakness associated with the joystick controls

change was a significant contributor to the September 9,1993, fuel assembly inadvertent

lowering event. The licensee stated at the September 21,1993, public exit that the joystick

controls had been changed as one of the licensee's corrective actions. The licensee indicated

that forward motion was now "down" and backward motion was "up" as appropriate for a

control panel in the horizontal plane.

7.0

LICENSEE CORRECTIVE ACTIONS

Following the September 3,1993 event, the licensee conducted maintenance and

troubleshooting of the hardware involved (see Section 5.0), conducted additional training (see

Section 3.1.3), and revised the fuel handling procedure (see Section 3.2). The licensee also

added a grapple interlock (see Section 4.3) and required oversight by QA during the

supplemental training sessions.

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8.0

SAFETY SIGNIFICANCE

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The team reviewed the radiation surveys, air sample records, and chemistry results following

both fuel handling incidents. No evidence was found of any increases following the

September 9,1993 event. Some small increases were identified to have occurred after the

September 3,1993 event. These increases are summarized in Attachment 5. The team

concluded that the radiological safety significance of the events was low. The team noted,

however, that the observed gaseous activity increases suggested some damage probably

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occurred to one or more fuel rods.

The team reviewed the videotapes taken of the two assemblies involved in the events and the

central core structures potentially impacted during the September 9,1993 event. There was

no indication of any damage other than to the two assemblies, but the full extent of damage

from the September 3,1993 event could not be assessed without removing the dropped

assembly. The damage visible in the videotapes was of low safety significance.

A fuel handling accident is a design basis accident and, as such, is addressed in Section

14.6.4 of the Vermont Yankee FSAR. Secondary containment integrity and operability of

key ventilation systems are prerequisites for handling fuel and were confirmed by the team to

have been in place during both events. The team concluded that the fuel handling incidents

had been appropriately mitigated by the systems operable and the existing plant

configuration, and were of minor safety significance separately.

The team was concerned, however, tiikt the weaknesses in management oversight had

allowed many of the measures intended to prevent a fue' handling accident to become

degraded. Design changes were not properly transmitted to allow timely and accurate

training on the modifications. Training was not effective in that operators were not aware of

certain key procedure steps. Procedures were not used and were not adhered to.

Supervisors did not ensure that procedures were followed. Management did not effectively

communicate expectations and provide proper oversight of fuel handling activities.

9.0

CONCLUSION

The AIT concluded that the preponderance of the evidence indicated that the

September 3,1993, event resulted from operator error. An improperly grappled fuel

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assembly became detached and fell about eight feet back to its original location with some

minor damage to the assembly. The root cause of the event was a weakness in management

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oversight of fuel handling activities as evidenced by lack of knowledge of and adherence to

the fuel handling procedure by operators, engineers, and supervisors.

The team concluded that mistaken lowering of a fuel assembly onto another core component

on September 9,1993, was an inadvertent operator performance error caused, in part, by

human factors weaknesses. The continuance of movement of the affected assembly was a

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precedure compliance error. This procedure compliance error was not identified by licensee

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line management or by the licensee's event investigation. This was indicative of a weakness

in corrective actions to the September 3,1993, incident and a continued weakness in

management oversight of fuel handling activities.

10.0

MANAGEMENT MEETINGS

Licensee management was informed of the scope of this AIT during an entrance meeting on

September 10, 1993. The team briefed licensee mam.gement of the team's observations

routinely and at the conclusion of onsite review on Sepkmber 14, 1993.

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A public exit meeting was conducted on September 21,1993, at 10:00 a.m., at the Vernon,

Vermont, town hall with licensee representatives identified in Attachment 2 to discuss the

preliminary inspection findings. The slides presented at the public exit meeting are contained

in Attachment 6. The licensee acknowledged the inspection findings and provided the results

of their assessment of the event and the short term and long term corrective actions.