ML20059C199

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Insp Rept 50-344/90-21 on 900609-0721.Violation Noted Re Inattentive Fire Watch.Major Areas Inspected:Operational Safety Verification,Maint,Surveillance,Event Followup,Sys Engineering & Open Item Followup
ML20059C199
Person / Time
Site: Trojan File:Portland General Electric icon.png
Issue date: 08/16/1990
From: Morrill P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML20059C197 List:
References
50-344-90-21, NUDOCS 9008310110
Download: ML20059C199 (18)


See also: IR 05000344/1990021

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U. S. NUCLEAR REGULATORY COMMISSION

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REGION V

Report No.

50-344/90-21

Docket No.

50-344

License No.

NPF-1

Licensee:

Portland General Electric Company

121 S.W. Salmon Street

Portland, OR 97204

Facility Name: Trojan

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Inspection at: Rainier, Oregon

Inspection conducted:

June 9 - July 21, 1990

Inspectors:

R. C. Barr

SeniorResidentInspector, Trojan

C. J. Bosted

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Senior Resident Inspector, WNP-2

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J. F. Melfi

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Resident Inspector

B. Olson

P

ct Inspector

B//6/W

Approved By:

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P.J.forrill, Chief

Dhte Signed

ReactorProjectsSection1

Summary:

Inspection on June 9 - July 21,1990 (Report 50-344/90-21)

Areas Inspected:

Routine inspection of operational safety verification,

maintenance, surveillt.nce, event follow-up, system engineering, and open item

follow-up.

Inspection procedures 30703 61726, 62703, 71707, 71710, 92700,

92701,93702,and97202wereusedasguIdanceduringtheinspection.

Results

General Conclusions and Specific Findings

This inspection identified a continuing weakness in the licensee's

administrativecontrol.ofsetpoints.Additionallyionsofsafetysyste.o

the operations grc m made

several procedural errors that resulted in actuat

(Section7).

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Significant Safety Matters

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None

Summary of Violation and Deviations

One cited violation identified an inattentive firewatch (Section 3).

Open Itemo Summary

Five LERs, two followup items and one unresolved item were closed.

One

unresolved item. in addition to the previously discussed Notice of Violation

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was identified.

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DETAILS

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1.

Persons Contacted

  • J. E. Cross, Vice President, Nuclear

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  • W. R. Robinson Plant General Manager

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  • C. K. Seaman,Assistart to Plant General ManagerdeneralManager,

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O. P. Yundt

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"G.A.Lievallen,GeneralManager,TrolanExcellence

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  • M. J. Singh, Manager, Plant Hodificat ons

J. D. Reid, Manager, Quality Support Services

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  • J. W. Lentsch, Manager, Personnel Protection
  • A. R. Ankrum, Manager, Nuclear Security
  • J. A. Reinhart, Acting Manager, Operations

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  • R. M. Nelson, Manager, Nuclear Safety and Regulation
  • M. W. Hoffman, Acting Manager, Planning and ControlNuclear Plant Engineeri

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A. N. Roller, Acting Manager

  • S.A.Bauer,BranchManager(e,NuclearRegulation
  • J. F. Whelan, Manager, Main nance

J.

Mody, Branch Manager, Plant Systems Engineering

D. L. Nordstrom, P^anch Manager, Quality Operations

J.

Taylor, PM/EA Branch Manager

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G.

Rich, Branch Manager, Radiation Protection

R. L. Russell, Brahch Mana

Operations

R. N. Prewitt, Supervisor,ger,lity Systems

Qua

R.

Reinhart, Supervisor Instrument and Control

J. A. Benjamin, Supervisor,, Quality Audits

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J. D. Guberski, Nuclear Safety and Regulation Department Engineer

  • W. J. Williams, Compliance Engineer

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  • D.

Couch, Compliance Engineer

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The inspectors also interviewed and talked with other licensee employees

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during the course of the inspection.

These included shift supervisors,

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reactor and auxiliary operators, maintenance personnel, plant techniciant

and engineers, and quality assurance personnel.

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  • Denotes those attending the exit interview.

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2.

Plant Status

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At the beginning of the inspection period the facility was in Mode 5. The

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plant entered Mode 4 at 4:56 a.m. on June 24, 1990, June 25, 1990, the

to perform Steam

Generator (SG) Crevice flushing.

At 10:35 a.m. on

facility was returned to Mode 5.

At 11:04 p.m. on June 25, 1990, at the

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conclusion of crevice flushing, Mode 4 was entered for the ascent to full

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power.

The lant entered Mode 3 at 8:32

.m. on June 27 1990.

On June

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28, the faci $ity returned to Mode 4 at 7:$7 p.m. to repalt the Auxiliary

Feedwater Pump control system.

The facility reentered Mode 3 at 9:36

a.m. on June 29.

The facility entered Mode 2 on July 5 at 5:03 a.m. and

low power physics testing (LPPT) was performed.

The facility entered

Mode 1 at 6:39 a.m. on July 10 and conducted main turbine testing.

While

conducting Main Turbine Overspeed testing at 2:50 a.m. on July 11, 1990,

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an Unusual Event (UE) was declared based on a perceived stuck open main

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steam safety valve. The UE was terminated at 3:13 a.m.

The facilit

returned to Mode 3 to investigate this event.

At 4:49 p.m. on Jul

13,

1990, the plant entered Mode 2 with Mode 1 entry occurring at 10:1

p.m.

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The plant reached 100% pcwer at 3:10 a.m. on July 17, 1990, and remained

at 100% power until the end of the reporting period.

3.

Operational Safety Verification (71707)

During this inspection period, the inspectors observed and examined

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activities to verify the operational safety of the licensee's facility.

The observations and examinations of those activities were conducted on a

daily, weekly or biweekly basis.

On a daily basis the insaectors observed control room activities to

verify the licensee's ad1erence to limiting conditions for operation as

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prescribed in the facility Technical Specifications.

Logs,

instrumentation, recorJer traces

examined to obtain information on, and other operational records were

plant conditions, trends, and

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compliance with regulations. On occasions when a shift turnover was in

progress, the turnover of information on plant status was observed to

determine if pertinent information was relayed to the oncoming shift

personnel.

Each week the inspectors toured the accessible areas of the facility to

observe the following items:

General plant and equipment conditions.

Maintenance requests and repairs.

Fire hazards and fire fighting equipment.

Ignition sources and flammable material control,

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Conduct of activities in accordance with the licensee's

administrative controls and approved procedures.

f) Interiors of electrical and control panels.

g) Implementation of the licensee's physical security plan.

a) Radiation protection controls,

i) Plant housekeeping and cleanliness.

j) Radioactive waste systems,

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(k) Proper storage of compressed gas bottles.

Weekly, the inspectors examined the licensee's equipment clearance

control with respect to removal of eouipment from service to determine

that the licensee complied with technical specification limiting

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conditions for operation.

Active clearances were spot-checked to ensure

that their issuance was consistent with plant status and maintenance

evolutions.

Logsofjumpers, bypasses,cautionandtesttagswere

examined by the inspectors.

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Each week the inspectors conversed with operators in the control room,

and with other plant personnel.

The discussions centered on pertinent

topics relating to general plant conditions, procedures, security,

training and other topics related to in-progress work activities.

The inspectors examined the licensee's Corrective Action Program (CAP) to

confirm that deficiencies were identified and tracked by the system.

Identified nonconformances were being tracked and followed to the

completion of corrective action.

Routine inspections of the licensee's physical security program were

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performed in the areas of access control, organization and staffing, and

detection and assessment systems.

The ins)ectors observed the access

control measures used at the entrance to t1e protected area, verified the

integrity of portions of the protected area barrier and vital area

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barriers, and observed in several instances the implementation of

compensatory measures upon breach of vital area barriers.

Portions of

the isolation zone were verified to be free of obstructions.

Functioning

of central and secondary alarm stations (including the use of CCTV

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monitors) was observed.

On a sampling basis, the inspectors verified

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that the required minimum number-of armed guards and individuals

authorized to direct security activities were on site,

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The inspectors conducted routine inspections of selected activities of

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the licensee's radiological protection program.

A sampling of radiation

work permits (RWP) was reviewed for completeness and adequacy of

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information.

During the course of inspection activities and periodic

tours of plant areas, the inspectors verified proper use of personnel

monitoring equipment, observed individuals leaving'the radiation

controlled area and signing out on appropriate RWP s, and observed the

posting of radiation areas and contaminated areas.

Posted radiation

levels at locations within the fuel and auxiliary buildings were verified

using both NRC and licensee portable survey meters.

The involvement of

health physics supervisors and engineers and their awareness of

significant plant activities was assessed through conversations and

review of RW) sign-in records.

The inspectors verified the operability of selected engineered safety

features.

This was done by direct visual verification of the correct

position of valves, availability of power, cooling water supply, system

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integrity and general condition of equipment, as applicable.

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Inattentive Firewatch

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On July 24 1990, at approximately 7:00 a.m., during a routine plant tour

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of the auxiliary building, the inspector noted that a continuous fire

watch had been established as a compensatory measure for a missing fire

barrier between the 77 foot and the 93 foot level (fire areas Al and AS,

A6) of the auxiliary building.

The inspector noted that the fire watch

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in that he was sitting in a chair, his eyelids were

appeared inattentive,back, mouth open, and feet extended out in front of

closed head leaning

him.

iheinspectorobservedthefirewatchforseveralminutesandthen

left to inform the Security Watch Supervisor.

The inspector returned and

observed the firewatch for an additional 10 minutes.

The firewatch

remained in the same position.

During this time, the firewatch's

portable communication radio gave a burst of noise and the firewatch

appeared to startle.

He then observed the inspector.

The inspector then

spoke with the firewatch concerning his duties and responsibilities,

Two security guards came shortly tiereafter and relieved him of his

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duties.

The same individual in the same location performing the same duties was

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observed by the NRC to be inattentive approximately two months previous

to the observation made on July 24, 1990.

During the previous

observation, the individual was given counseling, and the licensee let

all fire watch personnel know their expectations as to the degree of

attentiveness desired.

The inspector subsequently determined that the

firewatch had been at that station since 6:00 a.m. that morning.

The

failure to establish a continuous firewatch is an apparent violation of

technical specification 3.7.9(50-344/90-21-01).

Subsequent review of the incident revealed that the firewatch was

established for corrective actions associated with Corrective Action

Report (CAR) 90-5048.

The barrier was reported inoperable on March 23,

1990.

Technical Specification 3.7.9 states in part that, " Restore the

nonfunctional fire barrier penetration (s) to functional status within 7

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days or, in lieu of any other report required by Specification 6.6.1 or

10 CFR 50.72, prepare and submit a Special Report to the Commission

aursuant to Specification 6.9.2 with the next 30 days ..." The licensee

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las not submitted a Special Report on the inoperable fire barrier as of

the end of the inspection period.

The need to initiate a Special Report

will be be followed up during routine inspection.

One violation was identified.

4.

Engineered Safety Feature (ESF) System Walkdown (71710)

Prior to tre reactor startup from the 1990 Refueling Outage, the

inspectors verified portions of the Service Water (SW) and Residual Heat

Removal (RriR) systems lineups.

The inspectors also reviewed outstanding

Maintenance Requests (MRs) on these systems to identify MRs that needed

to be worked prior to startup.

The inspectors verified that the

housekeeping was adequate and system leakage appeared minimal.

The

inspectors were cor.cerned with the leakage around FE 610 and 611 and

questioned the licensee about the status of work on these RHR

recirculation line flow elements.

The inspectors were informed by the

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licensee that these were to be worked.

During the walkdown, the systems

ap eared to be properly labeled, and the instrumentation was installed

an in calibration.

Subsequent to full power operations, the inspectors walked down portions

of the RHR system.

The system appeared to be satisfactory with the

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following exception:

Valve M0-8703 (hot leg recirculation valve) was

noted to have aight out of 10 bolts missing on the valve actuator

electrical cover and there was boron crystallization on the valve stem.

These observations indicate a weakness in licensee's post outage system

walkdowns.

The licensee wrote a Priority 2 MR (90-8034) to correct the

missing bolts and routine MR (90-8048) to remove the boron accumulation.

The inspectors were informed that there were no open MRs on the valve.

The inspector determihed the valve was not environmentally qualified.

The inspectors will continue monitoring the quality of the licensee's

system walkdowns following planned and unplanned outages.

No violations or deviations were identified.

5.

Maintenance (62703)

On July 11, 1990, the licensee declared an Unusual Event (UE) when three

steam generator safety valves lifted fo11cving an overspeed test of the

main turbine.

Additional concerns were idontified over the operation of

the steam dump system during and following the event.

The inspector

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observed maintenance activities associateo with the troubleshooting

investigation for the steam dump pre.sure controller.

The steam dumps have two modes of control, Temperature Mode and Pressure

Mode.

In the Pressure Mode of control, the steam dumps modulate open

whenever the steam pressure exceeds the established setpoint.

During the

Unusual Event, it was noted that the steam dumps did not open as expected

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in automatic, however they did operate as designed in manual.

Subsequent

to thk , the licensee noted that the controller did not open at the

setpr nt of 9.1 (1092 psig), but it did o

psig). perate satisfactorily when the

controlwasadjustedto 8.9 (1068

The licensee then wrote

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Maintenance Request (MR) 90-7662 to troubleshoot and repair the pressure

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controller (PK-507),

The inspector verified the MR was performed by

qualified personnel, and that the MR instructions were followed.

The licensee investigated the operation of the steam dump pressure

controller.

The licensee determined that the controller was operating

correctly as set.

However, the reset time integrator was found to be set

at 120 seconds as opposed to 90 seconds as designed.

The controller

setting was last established during the 1989 outage.

At the end of the

inspection, the licensee could not identify when the reset time constant

was changed.

The licensee returned the reset setting to 90 seconds.

The

licensee stated that the change in the time response constant would have

had little effect on the transient.

No violations or deviations were identified,

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Surveillance (61726)

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The licensee reloads approximately 1/3 of the core each refueling outage.

For each core reload analytical methods are used to predict basic core

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parameters.

Core performance is evaluated during physics testing prior

to full power operations to verify these parameters.

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Section 10 of the Technical Specifications (TS) allows the plant to

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conduct physics tests for a new core and exceed specific portions of the

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TS by the use of saecial test exceptions.

The licensee used Periodic

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EngineeringTest(PET)13-1,"ReloadCycle13StartupLowPowerPhysics

Tests," which verified the critical boron concentration for certain rod

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configurations, the isothermal and moderator temperature coefficients,

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and tie zero power differential worth, and integral control bank rod

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worth.

The inspector observed the licensee conduct portions of PET 13-1.

These tests help to assure that the values for the Moderator Temperature

Coefficient (MTC) and the shutdown margin are within technical

specification requirements.

To measure the moderator temperature coefficient, the Isothermal

Temperature Coefficient (ITC) is measured and the MTC is found by

subtracting the fuel effects (Doppler. Temperature Coefficient or DiC)

from the ITC.

Technical Specification Surveillance 4.1.1.4.2.a requires

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that the MTC be measured prior to initial operation above 5% thermal

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power.

The licensee used TS special test exemption 3.10.4 to perform the

test prior to 5% power.

During the physics tests the core was kept at less than 5% thermal power

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and each intermediate range and power range nuclear instrument channel

had been subjected to a enannel functional check within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> of

initiating the test.

The reactor trip setpoints were set to less than

25% of rated thermal power.

The licensee was below the Point of Adding

Heat (P0AH)andtheRCSparameterswerestablewiththecontrolrod

position, boron concentration, RCS temperature and pressure set within

the reference bands.

The licensee calculated core reactivity using the reactivity computer,

which uses cycle specific core aarameters ar. input from one nuclear

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instrument channel to measure t1e core reactivity.in values of percent

millitho (pcm).

The values of core reactivity were plotted against RCS

temperature by the reactivity computer.

The value obtained for the ITC

was -1.5 percent millitho per degree Fahrenheit (pcm/oF) during the

cooldown measurement, and -2.7 pcm/oF during heat-up.

The average ITC

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was -2.1 ptm/oF.

The predicted value for tie ITC was -0.8 + 3 pcm/oF.

The value for the DTC was noted as 2.24 pcm/of based the initial (1975)

reload analysis.

An average value of 0.14 pcm/oF was then obtained for

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the MTC which meets the requirement of TS 3.1.1.4.

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The licensee also verified the differential and intparal rod worths for

the control banks.

The licensee monitored the RCS temperature and boron

concentration when taking the control rod worth measurements.

The

licensee maintained the pressurizer heaters on to assure that there was

proper mixing between the RCS and the pressurizer.

The licensee used the

boron endpoint method to determine the rod worths.

The control bank rod

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worths were within the acceptance range s)ecified by the procedure.

The

combined rod worths for control banks A, 3. C, and D were measured to be

3870.5 pcm, which was within the acceptance range of the test (3939 + 394

pcm).

The required shutdown margin by TS 3.1.1.1 is 1.6% delta K/K T1600

pcm).

The reload analysis value for the four control banks was 3939 pcm.

The inspector reviewed the data taken in PET 13-1 and no deficiencies

were identified.

The core physics parameters measured appeared to be

very close to what was analytically predicted by the reload analysis.

Other Issues with Surveillance Observation

During the performance of the core physics test, the licensee was

preparing to implement a new policy change on procedures requiring

ste)-by-step compliance wit 'cocedures.

This resulted in several delays

wit 1 the implementation of H.T 13-1 to allow the procedure to be changed

and/or performed as written.

The inspector observed this process and

identified no problems.

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The inspector questioned the changes to PET 13-1 which were completed at

the request of the Plant Manager.

The inspector observed that the

special test exemptions part of the Technical Specifications have special

surveillance requirements when performing the physics tests.

Two of

these surveillance requirements were to verify rod position every two

hours and thermal power less than 5% every hour.

T1e inspector discussed

the verification of these parameters with the cognizant test engineer who

had been involved with all the core physics testing that had been

performedatTrojan.

The engineer stated that the core status was

continually monitored by the responsible engineers and operators to

assure that the rods did not move inadvertently or that thermal power

exceeded 5%.

Previous revisions of this procedure did not require these

parameters to be documented consequently no proof of compliance with the

technicalspecificationsexIsts.

The inspector was informed that these

new changes would be included in the new revision to PET 13-1.

Ne violations or deviations t.ere identified.

7.

Event Follow-up (93702, 62703, 92701)

Inadvertent Containment Spray Pump (CSP) Start and Reactor Trip Sianal

On June 18, 1990, with the facility in cold shutdown (Moce 5) and

Periodic Instrument and Control Test (PICT) 22-2 " Engineered Safety

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Features Actuation System (ESFAS) Response Time,A being performed on the

B train of ESFAS, an inadvertent start of the B CSP occurred.

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June 30,(1990, while conducting a different section of PICT 22-2 in hot

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standby Mode 3), an inadvertent reactor trip signal was generated.

The

licensee conducted critiques after each event to collect information as

to the cause of the events.

From subsequent investigation the licensee

concluded the cause of the inadvertent CSP start was a jumper was not

removed during the performance of earlier steps of the PICT.

The

licenseeconcludedthejumperwasnotremovedduetoerrorsin

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communication and procedural noncompliance by technicians.

The licensv

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determined the generation of the inadvertent reactor trip signal was a

result of performing procedural steps out of sequence.

The inspector reviewed the licenseets critique notes and independently

investigated the events.

The inspector reached the same conclusions as

the licensee as to the causes of the events.

Additionally, the inspector

verified licen:re's immediate corrective action for these events and

verified the evtnts were reported per 10 CFR 50.72 and would be-

documented per 10 CFR 50.73.

The licensee's long term corrective actions

will be evaluated during the revier of LER 90-26.

MispositionedSafetyInjection(_SI) Pumps'ControlSwitch

At 9:36 a.m. on June 29,iencies, facility operational mode was changed 1990, after re

controller seismic defic

from Mode 4 (hot shutdown) to Mode 3 (hot standby).

One prerequisite

(technical specification 3.5.2) for the mode shift was to have both

safetyinjectionpumpsinautomatic.

At approximately 2:00 p.m. on

June 29, 1990,d that both SI pump control switches were,in aull-to-lock

during the swing shift crew watch relief the oncoming

crew identifie

(off) vice automatic, as required by plant conditions.

Boti SI pump

control switches were immediately placed in automatic.

Per 10 CFR 50.72,

the licensee immediately notified the Nuclear Regulatory Commission via

the Emergency Notification System (ENS).

Licensee investigation of the event concluded the SI pump control

switches were not correctly positioned because plant operators relied on

Mode 3 prerequisites from the June 27 transition to Mode 3, vice

reverifying the prerequisites were met for the June 29 transition.

In

thelicensee'sreviewofGeneralOperatingInstructions(GOI)1-2, ired

" Plant

Heatup-Hot Shutdown through Hot-Standby,"ing the SI pumps in automatic

they found that all requ

steps had been oerformed except for plac

(Step 3.6.2.d .

recurrence inc)luded counselling the operators involved, having theLicensee imm

involved operators provide a training session to their peers on this

event, and revising requirements for procedural compliance.

Previous to

this event, PGE operators were only required to follow procedures in the

sequence they occurred in the procedure when the prerequisites required

verbatim compliance.

The revised PGE requirement for verbatum procedural

compliance is to follow procedures in segeunce except when the

procedure's prerequisites state verbatim compliance is NOT required.

The inspector attended the licensk critique of the event, reviewed the

PGE all employee bulletin on the change in requirements to procedure

compliance and verified operator awareness of the change.

The ins)ector

concluded, due to the low core decay heat inventory and the availaaility

of the other Emergency Core Cooling System pumps,is event in LER 90-29.

this event was of minor

safety significance.

The licensee will report th

Heactor Coolant System (RCS) Flow Technical Specification (T.S.) Changes

On November 7 1989, the licensee and Westinghouse had a telephone

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conferencecalltodiscusstheaffectsofinstrumentuncertaintiesonRCS

flow and technical specifications associated with RCS flow.

The

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conversation was required to resolve previous operational concerns

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identified in Licensee Event Reports (LERs) 89-20, " Reactor Coolant

Average Temaerature Surveillance Performed Without Accounting for

Instrument Jncertainties," and 89-22, " Reference Temperature Value Used

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in Rod Control System Higher Than Value Used in Safety Analysis,"

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respectively.

During the discussion, Westinghouse (the reactor vendor)

told PGE that the RC5 flow value (354,000 gpm) for T.S. 3.2.3, "RCS Flow

Rate and FR " did not include instrument uncertainties and should be

revised (365,390 gpm) to include the instrument uncertainties.

PGE did

not consider an immediate change to the technical specification was

required since actual plant RCS flow was 371,539 gpm which was above the

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accident analysis required flow rate.

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On December 4, 1989, Westinghouse, via a memorandum to the Manager of

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NPE), documented that PGE could increase

Nuclear Plant Engineering (97% as long as RCS flow was maintained greater

reactor power to 100% from

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than 366,390 gpm.

On May 18, 1990, Westinghouse, via a telephone conversation, notified PGE

that after internal Westinghouse discussions on RCS flow with respect to

Trojan,itbecameapparenttherequiredvalueforRCSflowwasactually

371 700 vice 366,390 gpm.

Additionally, Westinghouse indiceted that the

minImumRCSflowrequirementcouldnotbechangedforeitherT.S.3.2,3,

"RCS Flow Rate and FR," or T.S

3.2.5, " Departure from Nucleate Boiling

(DNB) Parameters." The apparent RCS flow margins in these specifications

do not exist because other accident analyses were encompassed by these

specifications.

BecausetheactualmeasuredflowforTrojanduring

previous cycles had been-less than 371,700 gpm (371,539 gpm),the

licensee requested Westinghouse reanalyze to support a lower flow.

On

May 22, 1990, the licensee wrote corrective action request (CAR) 90-5167

to document the deficiency.

On May 30 1990, Westinghouse provided PGE

thereanalysisthatindicatedanRCSflowof 368,4)00 gpm was acceptable.

On June 5, 1990, after the Systematic Assessment of Licensee Performance

(SALP)meetingatTrojan thelicenseeinformedtheProjectManagerof

the RCS flow concern and, indicated PGE would be placing a more

restrictive administrative limit on themselves for RCS flow while the

technical specification change was being processed.

TheProjectManager

said he agreed with the licensee's approach and requested at the earliest

possible convenience marked up copies of the technical specifications be

provided for his review.

On June 25 1990,theOregonDepartmentofEnergy(ODOE) resident

inspectorInformedtheNRCresidentinspectort1atataPlantReview

Board (PRB) meeting which he attended, a change to the RCS flow technical

specification was discussed.

Since the resident had not been previously

appraised of the issue, he conducted a followup inspection.

1

From this inspection, he learned the above history.

He also learned PGE

was intending to restart from the 1990 Refueling Outage without havmg

the T.S. change ap3 roved by the NRC.

The inspector was also concerned

that the licensee lad presented the reload analysis for Cycle 14, which

included changes to the RCS flow rate, to the PRB for the PRB's review.

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The inspector expressed his concerns to licensee and to NRC Regional

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management.

As a result, the licensee sent a draft Licensee Change Ap)11 cation (LCA)

to NRC for review which was reviewed on June 30, 1990.

Tae staff

requested PGE take RCS flow measurements at 90% and 100% power to assure

that the RCS flow had not dropped below the new analyzed limits.

During

thesetests$0the RCS flow was measured at approximately 377,00 gpm.On

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July 13, ion. ,In the LCAthe licensee formally submitted the Licensee Change

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Applicat

the licensee concluded that the new T.S. values

didnotinvolveasignifIcantreductioninthemarginofsafety.

The

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licensee concluded that there was a small change in the RCS Protection

setpoint for Over Temperature Delta Temperature (K1 constant is now 1.41

versus 1.42 previously).

The licensee also determined that there was no

change in the DNB safety analysis and there was no reduction in the

margin of safety with respect to DNB.

This item remains open pending the inspector's review of the

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June 25 1990 PRB minutes and assessment of the appropriateness of not

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submittingaLCAeponlearningTechncialSpecification3.2.3and3.2.5

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wereincorrect(50-344/90-21-03).

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Unusual Event (UE) and Reactor Shutdown

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At 2:19 a.m., on July 11, 1990, with the facility in Mode 1 at

approximately 7% reactor power, the licensee, to verify the operability

of the main turbine overspeed trip mechanism, commenced Periodic

OperatingTest(POT)18-4,"MainTurbineOverspeedTripSystemTest." As

a test prerequisite the steam dumps were placed in automatic and set at

1092psigwiththeIntentionthatthesteamdumaswouldopenduringthe

test and prevent power operated relief valves ()0RVs) and main steam

safety relief valves (MSSVs) from actuating.

The main turbine was

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tripped at 2:32 a.m. and the facility entered Mode 2 at 2:36 a.m.

At

,

2:40 a.m., licensed plant operatv5 noted that the steam dumps (SDs) and

the secondary power operated relief valves (PORVs), which were expected

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to have automatically opened on increasing steam pressure, had not

opened.

The control operator briefly cycled the SDs from automatic to

manual and back to automatic which resulted in the expected SD operation.

At 2:49 a.m. the control room operator was notified by an auxiliary

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operator that the main steam safety relief valves (MSSV) were opsn.

At

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2:50 a.m. the shift supervisor declared an Unusual Event (UE) because he

concluded the MSSVs had failed to shut.

At 2:55 a.m., plant operators

began reducing reactor coolant system (RCS) temperature to reduce steam

temperature and pressure in order to get the MSSVs to reset.

At 3:02

a.m., all the MSSVs shut.

At 3:13 a.m., the licensee exited the UE.

The

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event raised questions over the proper functioning of the MSSVs, PORVs

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and the SDs.

At 5:40 a.m., the licensee as a conservative measure, shut

down the reactor and entered Mode 3 and tested the MSSVs, PORVs and SDs

for proper operation.

Testing of the MSSVs identified the MSSVs had o>erated as designed, i.e.

the MSSV lift and shut settings were correct.

urther licensee

evaluation of the event identified that the training the licensed

operators had received led the operators to believe the MSSVs would reset

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(shut) at higher pressures than the valves actually shut.

Testing of the

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PORVs identified that the PORVs did not functione as designed.

Due to

thelargeincrementsonthePORVsetpointscale(25lbs.)ftedbetween30

and the drift

tolerance of the controller output the PORVs actually li

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to 37 1sig higher than set.

Additionally,thelicenseedeterminedthat

the PORV controllers proportional band setting (full open to full close)

was incorrect (750 psig vice 60 psig).

The licensee concluded the

incorrect setting of the proportional setpoint had a limited affect on

this event because the MSSV settings were within the as-found settings

for the PORVs.

Licensee investigation of the event could 1ot determine

>

when the controller was improperly set.

Testing of the steam dumps

identified that the steam dumps functioned as designed; however

understandingbyboththelicensedoperatorsandtiesystemengIneersof

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SD controller operation when in automatic and the steam pressure control

mode was weak.

The system engineers and the licensed operators believed

the steam dumps, when in automatic, would open immediately and control

steampressure,wheninfact,thesteamdumpswereadjustedtofullyopen

on large (approximately 1000 psig) differences from set control pressure.

Additionally, the licensee also found that the controller reset

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integrator was actually set at 120 seconds vice 90 seconds.

The licensee

could not identify when the steam dump reset time integrator was misset.

Further licensee investigation determined licensed operator training does

not teach the details on the operation of the steam dumps when the

controller is in automatic and steam pressure control mode of operation.

As corrective action for this event, the licensee plans to train licensed

operators on the specific operation of the steam dump controller and the

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HSSVs.

Additionally, POT 18-2 and GOI 3-1 will be revised to alert the

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operators to the constraints of operating the steam dumps in the pressure

control mode.

The licensee also verified the present settings of both

the steam dump controller and the PORV rentroller are now at the correct

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design valuts.

The licensee will describe this event and their

corrective actions in LER 90-33.

As part of event response and followup, the resident inspector attended

the event critique, discussed the event with the Plant General Manager

and discussed with the facility licensed operators their knowledge of the

implemented corrective actions.

The resident verified that with a MSSV

blowdown (reset) value of 20%, the licensee safety analysis for a steam

generator tube rupture (SGTR) event with 1% failed fuel would not exceed

10 CFR 100 limits.

The licensee's immediate corrective actions appeared

conservative and appropriate to the inspector.

The licensee had a previous similar event occur in September 1984.

In

the 1984 event, the steam generator PORVs were set at approximately

1260 psig.

A transient occurred and the steam generator MSSVs lifted.

The control room staff was informed that the MSSVs were lifting by the

oncoming shift crew.

The licensee reduced steam generator pressure in

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order to close the MSSVs with last MSSV shutting at 890 psig (24%

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blowdown which was greater than design values).

The corrective actions-

for LER 84-17, " Delayed Reseating of Mair. Steam Safety Valve and Reactor

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Trip," were noted in letters from Mr. Withers to Mr. hartin dated October

3 and November 2, 1984.

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Some of the long term corrective actions to be taken for the

September 1984 event were to mark the normal setpoints on various

,

evaluate control room indicators for PORV setpoints,

controllers,irability of providing capability to monitor P55V position,

evaluate des

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and establish controls and routine checks on various instruments and

controllers in the control room.

The licensee labeled the controllers to

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give the nominal setpoints.

On May 24, 1985, the licensee, even though

all the controllers were set at 1125 psig and the actual setpoint setting

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of the controllers was two to three percent higher on all the

controllers, evaluated PORV setpoint on the control room indicators and

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concluded that the PORV controller setpoint had sufficient precision to

verify that the controller setpoint was set at a) proximately 1125 psig.

On December 3, 1985, the licensee, even though tie control operator had

evaluated the need and concluded

to be informed the safety had lifted,isted.

sufficient control room indication ex

During the July 1990 event,

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the operators again had to be informed by personnel external to the

control room that the MSSVs had lifted and the indication on the

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controllers was insufficient to assure lifting of the PORVs at desired

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pressures.

Based on the July 1990 event it appears the licensee's

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correctiveactionsfortheSeptember198$eventdidnotpreventarepeat

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occurrence.

Further inspector followup of this event will occur during

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the review of LER 90-33.

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No violations or deviations were identified.

8.

Follow-up of Licensee Fvent Reports (92700)

LER 90-01, Revision 0, (Closed), " Failure to Test Containment Personnel

Air Lock Equalizing Valve Compromised Containment Integrity Due to

Procedural Inadequacy." Licensee followup of failed surveillance,

Periodic Engineering Test (PET) 5-2 " Containment Local Leak Rate Testing

(LLRT),"identifiedthatthesurveillancedidnottesttheContainment

Personnel Airlock inboard equalizing valve for leakage.

The licensee

concluded the cause of the event was both the design of the door's

equalizing system and an inadequate procedure.

The licensee confirmed

PET 5-2 was adequate for leak testing the outboard Containment Airlock

doqr and its equalizing valve, inboard door equalizing valve.but was only a

inboard door seal and not the

Licensee

corrective actions incTFded (1) submitting an exemption request (April

18,1990) for not conducting a local leak rate test on the inner door

equalizing valve (2) revising the surveillance procedure and (3)

evaluating a modification to the airlock door equalizing valve.

On June

8, 1990 the NRC approved the exemption request.

The basis of the

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approvalwasacceptanceanalternativemethodofpressurizingbetweenthe

valve seals at reduced pressure and ratioing the as-found leakage to

design accident pressure.

The inspectors documented previous inspections of this event in NRC

inspection reports 50-344/89-33 and 50-344/90-11.

Additional inspection

in this period included a review of the revised surveillance procedure,

verification that the local leak rate test for the containment airlock

was within acceptable leak rate criteria (using the new procedure), and

verification that the integrated leak rate test was within leakage

criteria.

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LER 90-11, Revision 0 and Revision 1, (Closed), " Control Room Emergency

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Ventilation System Unfiltered In-leakage Exceeds F5AR Value Due to

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Missing Duct Sealant." on March 30 1990, the licensee determined

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unfiltered air in-leakage for the B train of control room emergency

ventilation system (CB-18) exceeded the aaximum allowed accident analysis

value of the FSAR (25.5 cfm vice 10 cfm).

The licensee verified that the

other train of control room emergency ventilation (CB-1A) was always

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operable with the exception of times when maintenance or surveillance

testing was in progress. -The licensee concluded the ducting was damaged

during a repair of a CB-1B seismic sup> ort during the 1989 Refueling

Outage.

The licensee also concluded t1e cause of the event was

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incomplete post-modification testing and that design documents did not

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identify that epoxy paint was being used as a temporary sealant until the

ducting was replaced.

Licensee corrective actions included repairing the

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damaged ducting, correcting the design basis documents, and replacement

of tie control room emergency ventilation ducting in 1992.

The licensee

also changed procedures to ensure adequate post maintenance testing

following work on ventilation ducting and revised drawings to indicate

the epoxy sealant was a part of the pressure boundary.

The inspectors verified the above mentioned corrective actions were

completed or scheduled as appropriate.

The inspectors reviewed the

results of the 1990 ventilation leak tests and verified no releases had

i

occurred between June 1989 and May 1990 that could have resulted in

exposure to plant operators.

As a course of routine inspection

inspectors will follow-up on the effectiveness of the licensee's, the

corrective actions.

This item is closed based on licensee completed and

proposed corrective actions.

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LER 90-13, Revision 1, (Closed), " Control Room Emercency Ventilation

Disabled Due to Door 25 Being Closed." This revisec

LER provided

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additional information with respect to the cause and corrective actions

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for the event.

The licensee concluded the cause of this event was

inadequate implementation of administrative controls and personnel error.

As corrective actions,ked the ability to pressurize the control room withthe l

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a chain and lock, chec

the emergency ventilation system and issued a lessons learned summary to

allTrojanemployees.

Additionally, the licensee is planning a permanent

modification to be installed by November 30, 1990, that will eliminate

the need to have the door open.

The inspectors verified the above corrective actions were performed or

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scheduled as appropriate.

Additionally, the inspectors discussed with

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the Plant Manager the requirements to verify that implemented

compensatory administrative controls are frequently surveilled for

adequacy.

The inspectors assessed this event to be of minor safety

significance since a positive control room pressure was achievable.

The

inspectors, as a part of routine followup inspection, will continue to

evaluate the licensee's implementation of administrative controls.

This

item is closed based on licensee completed and proposed corrective actions.

LER 90-14, Revision 0, (Closed), " Error ir Oricinal Classification and

Building of a Ventilation Boundary Wall Could Fave Rendered Control Room

Emergency Ventilation System Inoperable Due to a Seismic Event." Initial

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inspection of this event is documented in NRC Inspection Report

50-344/90-16.

Additional inspection found that had a seismic event

occurred, the ventilation boundary wall would not have collapsed even

though it may not have retained its design function as a pressure

retaining boundary.

Because a seismic event is not expected to cause a

design basis loss of coolant accident or toxic exposure to the control

room operators, the inspectors concluded the safety significance of this

event to be minor.

The licensee's corrective action was to redefine the control room

ventilation boundary (after having structurally reinforced and

seismically qualified boundary walls exterior to the wall described by

this event).

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The inspectors reviewed the boundary wall reinforcement and changes with

the design engineer, as well as the most recent surveillance test to

verify the emergency control room ventilation pressurization surveillance

met technical specification requirements.

Based on the licensee's

corrective actions and the minor safety significance of the event, this

LER is closed.

No violations or deviations were identified.

!

9.

Followup of Open and Unresolved Items (92701, 92702)

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Unresolved Item 90-02-02, (Closed), "Both Trains of Containment Hyc'rogen

vent System Inoperable." The A train of the containment hydrogen vent

ystem was declared inoperable in 1989 due to the sample point not

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providing a representative sample under low flow conditions.

The B train

sample point was modified to provide a representative samplo.

On January

24, 1990, the B Emergency Diesel Generator (EDG) which provides emceency

power to the B train hydrogen vent system was removed from service for

maintenance leaving no operable Hydrogen Vent Systems.

The B trait was

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returned to service on January 25, 1990, which was

within the 30 day

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Limiting Condition for Operation (LCO) of technical specification 3.6.4.3.

The cause of the event was inadequate coordination of work.

As

corrective action the licensee implemented a Plan of the Day that is

reviewed by all plant managers.

The safety significance was minimal

since the facility operated within the technical specifications.

This

item is closed.

Unresolved Item 90-16-01, (Closed), " Evaluation of Licensee's Degraded

Posts on Station Battery."

)

During the pe formance of a maintenance observation inspection, the

i

inspector questioned if cop)er contamination in the station batteries was

a reportable event per 10 C:R 50 Part 21.

Part 21 requires reports of

i

manufacturing defects.

The licensee had determined that a manufacturing

defect in the lead posts that have copper inserts resulted in copper

contamination in some cells of the station batteries.

Copper

contamination in the acid electrolyte can result in the cell voltage

decreasing and shortening battery life.

The battery cell voltage is

required by technical specification surveillance requirement 4.8.2.3.2 to

be greater than 2.00 volts.

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The concern over copper contamination was documented on April 10, 1990 in

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Corrective Action Request (CAR) 90-3070.

The CAR had been evaluated and

gone through initial Quality Assurance (QA) review.

The inspector asked

for the Part 21 evaluation on the station batteries on approximately June

20, 1990.

The Itcensee had not performed the Part 21 determination for

reportability at that time.

The licensee's maintenance group >erformed

an initial Part 21 determination on July 6, 1990 and stated t1at it was

notreportable,perthelicensee'sNuclearDivisIonProcedure(NDP)

700-4, "10 CFR 21 Re)orting of Nuclear Plant Defects or Noncompliances".

When questioned by tie inspector as to why they had not performed the

Part 21 determination earlier, the licensee stated that they were going

to perform the evaluation after the conclusion of the 1990 Refueling

Outage.

The inspector's concerns over the reportability of this issue were

discussed with the maintenance group with the following observations::

1)

The maintenance group stated that this was not reportable because

they could not find any technical requirement for copper

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contamination in any procurement document or NRC regulation.

The

inspector reviewed the vendor manual and noted limits on copper

contamination in the electrolyte on page 41.

Further, since the

continued use with cop)er contamination could lead to a loss of

voltage on the cell, tiis contamination can affect the NRC technical specification 3.8.2.

2)

The maintenance group also stated that this was not reportable

because the structure was not used to handle radioactive material or

control personr.el exposure.

The inspector noted that the station

batteries provide the emergency power source for power to

instruments following loss of off-site power.

Some of the

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instruments to which power is provided are radiation detectors which

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are used during an accident to control personnel exposure,

3)

The maintenance group further stated that this was not reportable

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because this potential defect would not contribute to exceeding a

i

safety limit or affecting the ability to mitigate the consequences

of an accident assuming a single failure.

The batteries are also-

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used to help mitigate the effects of a station blackout.

4)

The inspector observed that the station batteries are used to help

mitigate the effects of a station blackout.

Because the inspector raised the concern over reportability, the

Maintenance Department asked the Licensing Department to perform an

independent Part 21 evaluation.

The Licensing Department did not agree

with the maintenance department analysis,ly reported by another licensee.

but stated that this was not a

Part 21 report since it had been previous

The inspector contacted the NRC staff and confirmed that their was a

previous Part 21 on the batteries describing this situation (in 1979).

The following items may indicate a weakness in the dispositioning of

potentially reportable events:

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The Maintenance Department evaluation was not timely and was

performed apparently as a result of the inspector's questioning.

2)

The rationale of the Maintenance Department for determining

reportability did not appear correct.

i

3)

The initial QA review of the completed CAR failed to identify this

CAR may have been reportable with respect to Part 21 10 CFR.

The inspectors will continue to monitor licensee evaluatiot, of

potentially reportable issues under 10 CFR 50 Part 21 for technical

adequacy and timeliness.

Followup Item 90-02-03, (Closed), " Evaluate Licensee Actions on Event

90-21."

Steam and water were found to be cmitting from vent valve F-14-3

on the RCS sample line on January 25, 1990.

An operator and guard were

contaminated.

The leak was stopped by isolating the sample line.

An

improper valve lineup was believed to have been the cause.

The licensee

performed an evaluation of this event, documented in Event Report 90-021.

The licensee's evaluation of the event' concluded:

(1)twotestvent

valves (S-5017 ands-5018)onthesamplelinewereshutbutleakedby

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(they did not pass a subsequent pressure / leak test and were replaced);

and (2) a pipe cap on the end of the line downstream was incorrectly

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installed.

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The licensee identified a number of corrective actions as a result of

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this evaluation.

Procedures OH-3-1 and OM-3-3 were revised on March 6,

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1990, to prohibit operators from installing vent and drain caps except

during an emergency.

Operation and Maintenance revised their policies on

March 6, 1990, to provide instructions to check for leakage when

releasing clearances and when a system is repressurized.

In addition all

Teflon tape wu removed f rom site by February 23, 1990.

The actions as reviewed in Ev(nt Report 90-021 were considered adequate.

This item is closed based on licensee corrective actions.

No violations or deviations were identified.

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Unresolved Item

An unresolved item is a matter about which more information is required

to ascertain whether it is an acceptable item a deviation, or a

violation.

AnunresolveditemisdocumentedInSections3and6.

12.

Exit Interview (30703)

!

The inspactors met with the licensee representatives denoted in paragraph

1 on August 9, 1989, and with licensee management throughout the

inspection period.

In these meetings the inspectors summarized the scope

and findings of the inspection activities.

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