ML20056G719

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Concludes That Util Safety Performance at Plant Was Good & Improvement Noted in Certain Programs.Decline Noted in Performance in Some Functional Areas & Ongoing Problems in Others
ML20056G719
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 08/19/1993
From: William Cahill
TEXAS UTILITIES ELECTRIC CO. (TU ELECTRIC)
To: Milhoan J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20056G692 List:
References
TXX-93305, NUDOCS 9309070088
Download: ML20056G719 (2)


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ENCLOSURE 3

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  • 10132  :

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  • * * *
  • August 19, 1993 Mr. J. L. Milhoan, Regional Administrator U. S. Nuclear Regulatory Commission Region IV 611 Ryan Plaza Drive, Suite 400 Arlington. Texas 76011-8064

SUBJECT:

COMANCHE PEAK STEAM ELECTRIC STATION (CPSES)

DOCKET .NCS. 50-445 AND 50-446 COMMENTS ON SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE (SALP)

Dear Mr. M11hoan- I I

By letter dated July 23, 1993, the Nuclear Regulatory Commission (NRC) )

transmitted the Systematic Assessment of Licensee Performance (SALP) Report This l for Comanche Peak Steam Electric Station (CPSES) to TU Electric.

report documented the staff's assessment of the perfornance of TU Electric with regard to CPSES during the period February 3,1992, through l May 29. 1993.

The staff concluded that TU Electric's safety performance at Comancne Peak was good and improvement was noted in certain programs. The staff found noteworthy the concurrent completion of preoperational testing on Unit 2 while undertaking a refueling outage on Unit 1. Also noteworthy was the continued strong performance in the areas of Emergency Preparedness and Engineering / Technical Support, which reflected strong management involvement and safety perspective.

A decline in performance was noted in some functional areas and c1 going problems were noted in others. Strong management support for plant activities was evident; however, weaknesses in the implementation of certain programs and a failure at times to ensure that performance expectations were noted. The staff recommended the following actions: 1) continue to emphasize the implementation of the corrective actions initiated to enhance personnel performance and further reduce personnel errors in the areas of operations and surveillance testing, 2) provide increased management oversight of the contrattor guard force, and 3) strengthen the implementation of the corrective action process and the response to self-identified issues.

9309070088 930830 PDR ADOCK 05000445 G PDR_

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TXX-93305 Page 2'of 2 The staff also recommended continued sensitivity to problems that may We surface as we fully integrate the activities of two operating units.

4 should assure ourselves that the transition to an operating plant environment is successfully achieved and ensure appropriate engineering support of plant operations.

TU Electric has carefully reviewed and evaluated the information contained in the SALP Report and, as stated at the meeting of August 18. 1993, finds it to be accurate and agrees with the overall conclusions and TU Electric is initiating actions in recommendations contained therein.

response to the recommendations and to effect improvements in the areas of weaknesses identified by the'NRC in the SALP Report.

Sincerely, William J. Cahill, Jr.

RJA/rja c- Resident Inspectors, CPSES (2)

Mr. T. A. Bergman, NRR Mr. B. E. Holian, NRR Document Control Desx i

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