ML20054E693
| ML20054E693 | |
| Person / Time | |
|---|---|
| Site: | Nine Mile Point |
| Issue date: | 06/01/1982 |
| From: | Roman T NIAGARA MOHAWK POWER CORP. |
| To: | |
| Shared Package | |
| ML20054E692 | List: |
| References | |
| NUDOCS 8206140075 | |
| Download: ML20054E693 (6) | |
Text
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i NIAGARA M0llAWK POWER CORPORATION NINE MILE POINT NUCLEAR ~ STATION UNIT #1 i
NARRATIVE OF OPERATING EXPERIENCE May 1982 i.
The Station operated during the month of May.1982 with a monthly avail-l ability factor of 0.0% and a net design electrical capacity factor of
-0.0%.
The Station'was shut down March 19, 1982, for a scheduled main-
.tenance outage. The Station remains shut down due to Reactor Recircula-i tion system piping cracks found during Vessel llydro on March 23, 1982.
CLASS I WORK - MAINTENANCE - MAY 1982 7.
WR #17441 - Cleaned air motor and strainer on #102 Diesel Generator -
WR #17452 - Replaced oil seal on #12 Liquid Poison pump (5/17/82) 4 CLASS I WORK - INSTRUMENTATION AND CONTROL - MAY 1982 i
WRs 17295 Emer. Cond. Condensate Return IV #39-05 and #39-06 Solenoids and 17296 _Icaking air.
(Rebuilt solenoids and tightened fittings.)
WR #16178 - F.C.V. on C.R.D. Sys. Blowing Air Out of Positioner.
(Replaced fitting on air line.)
WR #17285 - I.R.M. #16 spiking bringing in half scram.
(Breaking down at 480V replaced detector.)
CLASS I WORK - ELECTRICAL - MAY 1982 MO #2151 - Mark I Containment - New Torus Temp. Monitoring i'
WR #16126 - Rebrush M.G. Set #162 N1-MST-M1 - 125 V.D.C. Battery Pilot Cell Voltage and Specific Gravity i
Test v
i:
8206140075 820608 PDR ADOCK 05000220 4
R PDR
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HlA2 ARA *.
M2 HAWK sis t.*? * :. fen NUCLEAR STATION 5;EPCM OF CPER Af to's FOR PERICO ENDING 12:00 hlN [ts?
[ost k UN i
Diesel Die'sel l
unit
- 1 luair 102 Ju=ir 103 i
vont MO.
No
-No.
s'a m g Ettetoscat j
0.0 0.0
- s. st=Imatio - =tf u.,
- a. utust stavect
'mou i
0.0 t O.O i
0.0 10.o
- s. Gt=tnatio= - Geoss uw,
- 4. K121Euu Nous GEqthattog - htf uw I
- s. II tiMuu Mout GENttafiog - Ntf Nw l
- 4. o ftaftut-man me Loao
- f. Noulmat avt. MTORoGIM Petssuat Les.
i 6.000 3.000 9.000
- e. o st.sto castaafe.
n.=
la tCH a N f C al 0'
o
- 9. TuR9tht - ho. of staRfs i0. 01CE PRtssuRE shaf t )
IN MG l t.
CC4089saf t itMP. (Note )
'F I
it. CINC. waf t4 E47. f tMP (Nott )
'F 1
0 o
is. 8 tactor.mo. or sf ants l
0.0 I oo is. twtivat ec.c.
- u. 3 v s 1
0.0 l
0,0 es. euas ue uno/'o=
14.167.4 1
3,157 4 is. eue uP arvacuu to struct v om, I
I 2
1 t
i t. citsto Gas. u. :n sta=f s i
8 490 San 7tn is. ontsto acto st.asto Gat
!LAlLI ie. noust steveCE 0.0 n n 1
0.0 I
5'n to Carneiurv racion enof t si l
UU I
0~0 si. Leaa raCfon enof t si 0.0 0.0
- 21. MToIoGEM Lt EaGE Raf t. oaf Cu FT 3s. IIFaite aaf t = Gross L9:!NwH ta.
t 0.0 0.0
- 35. utaf mate enof t at ef e.tr...
24.
UNir wouns 0
0 af. on tono sens 0
0
- . avsetaste nas
- 29. UNavatLa8LE Mes 20 fusttut.Causto IDLt. (Nott si Mas a
si. Tuteint aus Mas 1
sa. Ga=tenfoe.Causto sott.
was
- 33. Giunaron aus. -
i.n s 744F 744 744
- 24. et a: :s :a ato ::Lt.ts: -
was I
- 35. eta:t.aus.-
uns st. sT=CMootous CoNCt4stR cPt4.
MRs I
st.
rorat ty l
0235 U 2 38; U:19 PU 39 AU240 PU 4i l PU 42 FUJ Sg ypY 1s. staa? Cr Ptei00
- 39. #CCIl%cD
- 83. SalP*t:
an. si't%f.(*e00u0t$
at. EM C8 Ptes:0 tLqtu T.E. Lempges W. Arlukewicz J. Hallenbeck C. Piper S. Wilczek Power Control
- i. taats at ti=t or.
...Loao
. itfu i int'r saf to Car e etnion #es.
T. Bassett M.A. Silliman J. ?!arris
- ift=i-istc=s= etion..si D. P. Dise Factory Mutual C.V. Mangan a D irtv v4: = ra son + irtw i C. Geniac
.nces Bleskoski
- s. f t:Clo ouf ace. F. ScatDutto ouf aGt - s.
f
' # #f stG%ED
. q s..m. :w -
s i s. i n u..... na.1 (UFAGES -tNITS #D NNILINilES
- t. m ill.May 1982
,ygga PARilALLY a wf f T AVAILAeLE etouRS Jaya, I a ni i HEASLNS/ REPAIRS C f 4)lf.18,((LL DAY Ott TIMF trHAVytAntF 180t 8 84 S
- CAP,
- ' l Rx 3/23/82 March Crack in Recire. piping discovered during hydro, 154.0F major repairs underway.
April 719.0F May 744.0F I
6*
i e
)
9 O
OPERATING DATA REPORT DOCKET NO.
50-220 DATE 6/1/82 CO5tPLETED 11Y TW
- nnm, tu' TELEPilONE (3151343-211 X1383 OPER ATING ST.'.TUS
- 1. Unit Name: Nine blile Point Unit #1 Notes
- 2. Reporting Period:
05/01/82 to 05/31/82
- 3. Licensed Thermal Power (31Wt):
1850 640
- 4. Nameplate Rating (Gross AlWe):
- 5. Design Electrical Rating (Net S!We):
- 6. Staximum Dependable Capacity (Gross hlwe):
630
- 7. Staximum Dependable Capacity (Net AlWe):
610 S. If Changes Occur in Capacity Ratings (items Number 3 Through 7)Since Last Report. Give Reasons:
- 9. Power Level To Which Restricted,if Any(Net 51we):
- 10. Reasons For Restrictions.lf Any:
This >!onth Yr..to Date Cumulatise I1. licurs In Reporting Period 744.0 3623.0 J 10.279.0
- 12. Number Of flours Reactor Was Critical 0.0 1874.0 81.308.5
- 13. Reactor Reserve Shutdow n llours 0.0 0.0 1.204.2
- 14. Ilourt Generator On Line 0.0 1872.5 78,562.3
- 15. Unit Reserve Shutdown llours 0.0 0.0 20.4
- 16. Gross Thermal Energy Generated (51WII) 0.0 3.421.093.0 129.374.390.0
- 17. Gross Electrical Energy Generated (SIWil) 0. 0,,,
1,169.791.0 42.743.090.0
- 18. Net Electrical Energy Generated (51Wil) 0.0 1,134,758.0 41.392.651.0
- 19. Unit Senice Factor 0.0 51.7 71.2
- 20. Uni Availability Factor 0.0 51.7 71.2
- 21. Unit Capacity Factor (Using 51DC Net) 0.0 51.3 61.5
- 22. Unit Capacity Factor (U>ing DER Net) 0.0 50.5 60.5
- 23. Unit Forced Outage Rate 100.0 46.3 9.8
- 24. Shutdowns Scheduled Oser Next 6 Stunths iType. Date.ata: Duratiaa of Each::
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
5farch 1983
- 26. Units In Test Status (Prior to Commercial Operation).
Forecast Achiesed INITIA L CRITICA LITY INITIA L ELECTRICITY CO\\l.\\lERCI A L OPER ATION (W77)
e AVER ACE IgILy UNIT POuCR LEVEL DOCidET NO.
50-220 UNIT 9 Miin Pt. #1 DATE 6/1/82 CONIPLETED BY T W.
Roman A
TELEPilONE -(315)'343-2110 X1383 AIONTH 6fa y, 1982.
DAY AVERACE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL IMWe Net)
(alwe.Neil 3
0 0
37 2
o IS 0
3 0
19 0
4 0
20 0
5 0
21 0
6 0
O 2.'
7 0
0 23 8
0 0
24 9
0 25 0
10 0
0 26 11 0
^
27 0
0*
12 13 0
29 0
14 0
0 30 IS 0
31 0
16 0
l INSTRUCTIONS On this format.hst the average daily umt pimer leselin MWe. Net for e.sch day att flic rep ** tine in.nirls.C the nearest uhole mepawatt.
19177 l
l l
L
1 UNITSilUTDOWNS AND POWER REDUC 110NS DOCKET NO.
50-220 UNIT NAME 9 hiite Pt. at DATE 6/1/82 REPORT MONTil May 1982 COMPLETED BY T.W_ Romn Ay TELEPHONE f 315) 34 3-2110 4
X1383 3
3 = ='g c
e r.
j _e Licensee
~
c g"3 Cause & Corrective y
.a.
Date g
e@
M
.E g cc Event 3?
x 9-Action to 5E E
j15j Report a N0 j'
Prevent Recurrence i
5 8206 820323 F
1617 A
4 82-009 Major repairs continue on recire.
4 g
piping, core off-loaded to SFP.
4
~.
4 1
1 2
3 4
F: Forced Reason:
Method:
Exhibit C. instructions S: Scheduled A Equipment Failure (Explain) 1 Manual for Preparation of Data B Maintenance of Test 2 Manual Scram.
Entry Sheets for Licensee O. Refueling 3 Automatic Scram.
Event Reporn (LER) File (NUREG.
D Regulatory Restriction 4-Other (Explain) 0161)
E-Operator Training & Ucense Examination F Administrative 1
5 G-Operational Error (Explain)
Eshibit I Sang Source I
(9/77)
Il Other (Explain)
-