ML20054C127
| ML20054C127 | |
| Person / Time | |
|---|---|
| Site: | Crystal River |
| Issue date: | 04/13/1982 |
| From: | Bogart D, Culver M FLORIDA POWER CORP. |
| To: | |
| Shared Package | |
| ML20054C125 | List: |
| References | |
| NUDOCS 8204200084 | |
| Download: ML20054C127 (4) | |
Text
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'8b OPERATING DATA REPORT DOCKET NO.
50-302 DATE 4/1/82 COSIPLLIED ltY D.
Engan TE LI PilONE (904) 795-6486 OPER ATING STATUS
- 1. Unit Name:
Crystal River Unit #3 Note'
/
- 2. iteporting Period:
3/1/82 - 3/31/82
- 3. Licensed Thermal Power t51%:):
2544 g
- 4. Nameplate Rating (Grow %1We):
890 825
- 5. Design Electrical Rating (Net $1We):
845
- 6. Stasimum Dependable Capacity (Grow S1We):
806
- 7. Stasimum Dependable Capacity (Net $1We):
- 8. If Changes Occur in Capacity Ratings (items Number 3 Through 7) Since Last Report.Gise Reasont N/A 9 Power Lesel To hhich Restricted. lf Any tNet \\1 Wen N/A N/A
- 10. Reasons l'or Restrictions. If Any:
This Slonth Yr.to.Date Cumu!. itis e
- 11. Ilours In Reporting Period 744 2160 44280 12 Number Of flours Reactor has Critical 646.3 1303.1 26752.49
- 13. Reactor Resene Shutdown Hour, 0
3.9 1213.12 638.I 1282.6 26094.78 14 ilours Generator On-Line
- 15. Unit Resene Shutdown !!ours 0
0 0
1444365 3049088 58416029 16 Grow Thermal Energy Generated (5thil, 492327 1047109 19846700 17 Gross Electrical Energy Generated t%1h }l, 468784 998576 18827874 lb. Net Electrical Energy Generated (\\1h Hi 85.8%
59.4%
58.9%
- 19. Unit Senice f actor 85.8%
59.4%
58.9%
- 20. Unit bailabihty Factor 78.2%
57.4%
54.3%
- 21. Unit Capacit3 factor #Using \\lDC Neti 76.4%
56.0%
51.5%
l 22 Unit Capacity Factor (Usm; DER Net) 14.23 40.6%
2 7. 4,T, 23 l' nit Fon ed Outag Rate
- 24. Shutdowns Scheduled Oser Nest 6 \\lonths tTs pe. Date, and Duration of Fach t Nnno 1
25 If Shut Down \\t I nd Of iteport Period. Estemated Date of Startup 4/2/82 2 t>
Unit In Test Status (Prior to Commercul Operation r Forecast A chies ed IMil \\ L ( RIIK \\ LIT Y 1/14/77 INill \\l. LLLCI RICII Y l/30/77 3/13/77
( O\\1\\11 RCI \\L OPI R \\1ros 8204200084 820413 PDR ADOCK 05000302 R
PDR l
AVER AGE D AILY UNIT POWER LEVEL DOCKET NO.
50-10?
L* NIT FLCRP-3 l
4/1/82 DATE i
COMPLETED BY D.
Bogart TELEPilONE (904) 795-6486 i
(,
MONTil March 1982 DAY AVER AGE D AILY POWER LEVEL DAY AVER AGE DAILY POhER LEVEL (MWe NetI (MWe NetI i
n i;
Ro?
2 106 lb 827 0
831 3
39 4
??n 20 R27 5
623 2]
834 619 823 6
7; 611 743 23 738 g
619 24 651 9
25 763 760 10 26 716 11 653 i
829*
i:
3g 590 833 546 i3 79 l
34 832 30 833 15 33 0
16 827 s
1 l5 INSTRL'CTIONS Ua th og Jad> -
M'J.t Ne! n : ea,h Ja3 - A wr
'm_
n:8 ( m r....
'he :.ca r
- .-timated due to bad meter reading, ei-,
1 I
DOCKIINo 50-3Q2 t' Nil slllt ilH)hNS \\NI) PO%I R RI DttrilONS IJNii N AMI
__FLCRP-3 Il\\ll _41.3.l82 COMPT.E1LD M M _ tt rulver 1(I e'OR I '.;ON Iil 378'3 I El I PilONI.
(904) 795-6486 g
=... -
5 i
,=
I n eir.cc ye, rg ranse & rorectinvc
{L.!
Action to
.; 5$
1 cnt V7
\\i l'ni f5 5
5 :f, 3 R epos e tIi G E
Present itesnriente e
c V
d 82-3 820301 F
32.8 A
1 See last re-SF VALVEX Continuation of outage from last re-(cont) port.
port.
82-4 820302 F
43.0 A
3 N/A IA INSTRU Plant tripped by the RC pump power monitors. Exact reason why unknown.
82-5 820304 F
0 D
N/A N/A IA INSTRU Restricted to 75% FP until a time de-lay question concerning the RC pump power monitors could be resolved.
82-6 820322 F
0 A
N/A N/A HF MOTORX Problem with a circulating water pump motor caused a reduction in power to the 85-95% FP range.
82-7 820327 F
0 A
N/A N/A CB MOTORX RCP-C motor tripped on a phase diff-erential; forced a power reduction to the 65-70% FP range.
82-8 820330 F
30.1 A
3 N/A IA INSTRU An upset in the electrical transmission system caused the RC pump power moni-tors to trip the plant.
I Ioisr.1 Itcason Met hotl.
I Alnbit G. Instintrions N Si hol nicil A I quipment I.nture (laplain) l-Mannat f or Pir,'. nation of Data ll.Maintenante or Test 2 Mannal Scram.
1 ntry Shects foi i nemcc F-Ref ucimi:
.L Antomatic Scram.
I-vent Rcroit il i 11) I ile (Niliti (;
in-Regulatory itesirittmn
.I Other II.xpl.un) 0161) i Opciator 1.unmp & l ts ense ! x.naination 5
I Atlll11 tost r.it h e
(, Oper.ihon.il I t ros (I spl.nn) i shibit 1 - S.nne Somie r #17 7 :
I! f)ihei il spl.nn)
MONTHLY OPERATIONAL SUDIARY STATDIENT DOCKET NO. 50 '107 UNIT FLCRP-3 DATE 4/5/82 COMPLETED BY M.W. Culver TELEPHONE (904) 795-6486 MONTH March 1982
SUMMARY
STATDIENT: The unit experienced two forced shutdowns and three forced power reductions during the month.
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