ML20054C127

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Monthly Operating Rept for Mar 1982
ML20054C127
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 04/13/1982
From: Bogart D, Culver M
FLORIDA POWER CORP.
To:
Shared Package
ML20054C125 List:
References
NUDOCS 8204200084
Download: ML20054C127 (4)


Text

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'8b OPERATING DATA REPORT DOCKET NO.

50-302 DATE 4/1/82 COSIPLLIED ltY D.

Engan TE LI PilONE (904) 795-6486 OPER ATING STATUS

1. Unit Name:

Crystal River Unit #3 Note'

/

2. iteporting Period:

3/1/82 - 3/31/82

3. Licensed Thermal Power t51%:):

2544 g

4. Nameplate Rating (Grow %1We):

890 825

5. Design Electrical Rating (Net $1We):

845

6. Stasimum Dependable Capacity (Grow S1We):

806

7. Stasimum Dependable Capacity (Net $1We):
8. If Changes Occur in Capacity Ratings (items Number 3 Through 7) Since Last Report.Gise Reasont N/A 9 Power Lesel To hhich Restricted. lf Any tNet \\1 Wen N/A N/A
10. Reasons l'or Restrictions. If Any:

This Slonth Yr.to.Date Cumu!. itis e

11. Ilours In Reporting Period 744 2160 44280 12 Number Of flours Reactor has Critical 646.3 1303.1 26752.49
13. Reactor Resene Shutdown Hour, 0

3.9 1213.12 638.I 1282.6 26094.78 14 ilours Generator On-Line

15. Unit Resene Shutdown !!ours 0

0 0

1444365 3049088 58416029 16 Grow Thermal Energy Generated (5thil, 492327 1047109 19846700 17 Gross Electrical Energy Generated t%1h }l, 468784 998576 18827874 lb. Net Electrical Energy Generated (\\1h Hi 85.8%

59.4%

58.9%

19. Unit Senice f actor 85.8%

59.4%

58.9%

20. Unit bailabihty Factor 78.2%

57.4%

54.3%

21. Unit Capacit3 factor #Using \\lDC Neti 76.4%

56.0%

51.5%

l 22 Unit Capacity Factor (Usm; DER Net) 14.23 40.6%

2 7. 4,T, 23 l' nit Fon ed Outag Rate

24. Shutdowns Scheduled Oser Nest 6 \\lonths tTs pe. Date, and Duration of Fach t Nnno 1

25 If Shut Down \\t I nd Of iteport Period. Estemated Date of Startup 4/2/82 2 t>

Unit In Test Status (Prior to Commercul Operation r Forecast A chies ed IMil \\ L ( RIIK \\ LIT Y 1/14/77 INill \\l. LLLCI RICII Y l/30/77 3/13/77

( O\\1\\11 RCI \\L OPI R \\1ros 8204200084 820413 PDR ADOCK 05000302 R

PDR l

AVER AGE D AILY UNIT POWER LEVEL DOCKET NO.

50-10?

L* NIT FLCRP-3 l

4/1/82 DATE i

COMPLETED BY D.

Bogart TELEPilONE (904) 795-6486 i

(,

MONTil March 1982 DAY AVER AGE D AILY POWER LEVEL DAY AVER AGE DAILY POhER LEVEL (MWe NetI (MWe NetI i

n i;

Ro?

2 106 lb 827 0

831 3

39 4

??n 20 R27 5

623 2]

834 619 823 6

7; 611 743 23 738 g

619 24 651 9

25 763 760 10 26 716 11 653 i

829*

i:

3g 590 833 546 i3 79 l

34 832 30 833 15 33 0

16 827 s

1 l5 INSTRL'CTIONS Ua th og Jad> -

M'J.t Ne! n : ea,h Ja3 - A wr

'm_

n:8 ( m r....

'he :.ca r

  • .-timated due to bad meter reading, ei-,

1 I

DOCKIINo 50-3Q2 t' Nil slllt ilH)hNS \\NI) PO%I R RI DttrilONS IJNii N AMI

__FLCRP-3 Il\\ll _41.3.l82 COMPT.E1LD M M _ tt rulver 1(I e'OR I '.;ON Iil 378'3 I El I PilONI.

(904) 795-6486 g

=... -

5 i

,=

I n eir.cc ye, rg ranse & rorectinvc

{L.!

Action to

.; 5$

1 cnt V7

\\i l'ni f5 5

5 :f, 3 R epos e tIi G E

Present itesnriente e

c V

d 82-3 820301 F

32.8 A

1 See last re-SF VALVEX Continuation of outage from last re-(cont) port.

port.

82-4 820302 F

43.0 A

3 N/A IA INSTRU Plant tripped by the RC pump power monitors. Exact reason why unknown.

82-5 820304 F

0 D

N/A N/A IA INSTRU Restricted to 75% FP until a time de-lay question concerning the RC pump power monitors could be resolved.

82-6 820322 F

0 A

N/A N/A HF MOTORX Problem with a circulating water pump motor caused a reduction in power to the 85-95% FP range.

82-7 820327 F

0 A

N/A N/A CB MOTORX RCP-C motor tripped on a phase diff-erential; forced a power reduction to the 65-70% FP range.

82-8 820330 F

30.1 A

3 N/A IA INSTRU An upset in the electrical transmission system caused the RC pump power moni-tors to trip the plant.

I Ioisr.1 Itcason Met hotl.

I Alnbit G. Instintrions N Si hol nicil A I quipment I.nture (laplain) l-Mannat f or Pir,'. nation of Data ll.Maintenante or Test 2 Mannal Scram.

1 ntry Shects foi i nemcc F-Ref ucimi:

.L Antomatic Scram.

I-vent Rcroit il i 11) I ile (Niliti (;

in-Regulatory itesirittmn

.I Other II.xpl.un) 0161) i Opciator 1.unmp & l ts ense ! x.naination 5

I Atlll11 tost r.it h e

(, Oper.ihon.il I t ros (I spl.nn) i shibit 1 - S.nne Somie r #17 7 :

I! f)ihei il spl.nn)

MONTHLY OPERATIONAL SUDIARY STATDIENT DOCKET NO. 50 '107 UNIT FLCRP-3 DATE 4/5/82 COMPLETED BY M.W. Culver TELEPHONE (904) 795-6486 MONTH March 1982

SUMMARY

STATDIENT: The unit experienced two forced shutdowns and three forced power reductions during the month.

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