ML20053A833

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Responds to NRC Re Violations Noted in IE Insp Repts 50-327/82-04 & 50-328/82-04.Corrective Actions:Safety Evaluation Written to Document Unreviewed Safety Question Determination Resulting from Temporary Sys Change
ML20053A833
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 05/05/1982
From: Mills L
TENNESSEE VALLEY AUTHORITY
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20053A829 List:
References
NUDOCS 8205270334
Download: ML20053A833 (5)


Text

p TENNESSEE VALLEY AUTHORITY CHATTANOOGA. TENNESSEE 37401 400 Chestnut Street Tower II May 5, 1982 M

I-(Nd r

U.S. Nuclear Regulatory Commission E

k Region II Attn: James P. O'Reilly, Regional Administrator nig 101 Marietta Street, Suite 3100 9o Atlanta, Georgia 30303 d'

oc R

Dear Mr. O'Reilly:

SEQUOYAH NUCLEAR PLANT UNITS 1 AND 2 - NRC/0IE REGION II INSPECTION REPORT 50-327/82-04 AND 50-328/82 RESPONSE TO VIOLATION The subject OIE inspection report dated April 5,1982 from R. C. Lewis to H. G. Parris cited TVA with one Severity Level IV Violation and one Severity Level V Violation. Enclosed is our response to the subject inspection mport.

If you have any questions, please get in touch with R. H. Shell at FTS 858-2688.

To the best of my knowledge, I declare the statements contained herein are complete and true.

Very truly yours, TENNESSEE VALLEY AUTHORITY L. M. Mills, Manager Nuclear Licensing Enclosure cc:

Mr. Richard C. DeYoung, Director (Enclosure)

Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, DC 20555 820 5 27 0 3 3j An Equal Opportunity Employer

Y RESPONSE - NRC INSPECTION REPORT NOS.

50-327/82-04 AND 50-328/82-04 R. C. LEWIS' LETTER TO H. G. PARRIS DATED APRIL 5, 1982 Appendix A Item A (328/82-04-02) 10 CFR 50.59 requires that the licensee not make changes in the facility as described in the Final Safety Analysis Report (FSAR) if the change involves an unreviewed safety question.

Prior to making a change in the facility as described in the FSAR the licensee shall perform a written safety evaluation which provides the basis for the determination that the change does not involve an unreviewed safety question.

Contrary to the above, the licensee changed a system as described in the FSAR without performing a written safety evaluation to determine that the change did not involve an unreviewed safety question.

On February 10, 1982 the licensee blanked the floor drains in the unit 2 west main steam valve room and installed portable pumps to redirect the secondary steam leakage condensate to the yard drainage system.

The floor drains in the west main steam valve room normally drain to the Floor Drain Collecting Tank in the Auxiliary Building per FSAR figures 9.3-9 and 9.3-10.

This is a Severity Level IV Violation (Supplement I.D.1.).

Applicable to Unit 2.

1.

Acmission or Denial of the Alleged Violation TVA admits the violation occurred as stated.

2.

Reasons for the Violation if Admitted The floor drains were blocked in the unit 2 west main steam valve room in order that the condensate leakage could be discharged directly to the yard drainage system.

This would eliminate the processing of significant amounts of secondary water that would have been collected in the floor drain collecting tank in the auxiliary building.

It was determined that the condensing steam leakege was not contaminated and could be discharged to the yard drainage system.

Since the steam generators and steam generator blowdown were monitored for radioactivity, this action was considered not to be an unreviewed safety question.

However, a written safety evaluation was not documented before the l

drains were blocked and the portable pumps were installed to pump the steam leakage out to the yard drainage system.

l l

3 Corrective Steps Which Have Been Taken and the Results Achieved l

(1) A safety evaluation was written and approved to document the unreviewed safety question determination as a result of the temporary change to the system.

This was accomplished on February 11, 1982.

Page 2 (2) As an added precaution, periodic samples of the waste water were taken and monitored at the point of discharge to the yard drainage system.

This is in addition to the normal monitoring of the condensate described above.

(3) The steam leakage was repaired during shutdown after a trip on February 11, 1982, that was part of a startup test.

4.

Corrective Steps Which Will Be Taken To Avoid Further Violations (1) A letter has been written and distributed to all appropriate

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personnel stressing the importance of the unreviewed safety question determination (USQD) and indicating the requirements for l

documentation of safety evaluations.

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(2) The need and requirements for USQDs have been discussed and emphasized in a PORC meeting on May 3,1982.

(3) The need and requir,ments for USQDs will be discussed and emphasized at an operations section personnel meeting by May 14, 1982.

I (4) Sequoyah Standard Practice SQA 119 will be revised to clarify those situations that require USQDs.

The target date for completion is i

June 30, 1982.

5.

Date When Full Compliance Will Be Achieved l

Full compliance was achieved on February 11, 1982.

j Item B (327/82-04-01 and 328/82-04-01)

Technical Specification 31.3.3 requires that one rod position indicator (excluding demand position indication) shall be operable and capable of determining the control rod position within 112 steps for each shutdown or

~

control rod cot fully inserted in modes 3, 4 and 5 when the reactor trip breakers are closed.

Contrary to the above, the licensee did not maintain one rod position indicator operable for each shutdown rod not fully inserted capable of indicating rod position within 112 steps in modes 3, 4 and 5.

At various times on both units since initial operation the licensee has maintained shutdown control rods withdrawn with the reactor coolant system below normal operating temperature (NOT).

With rod position indication calibrated at NOT, it will not indicate actual rod position within 112 steps at less than NOT.

This is a Severity Level V Violation (Supplement I.E.).

Applicable to Units 1 and 2.

l l

. -. ~.

F Page 3 1.

Admission or Denial of the Alleged Violation TVA admits the violation occurred as stated.

2.

Reasons for the Violation if Admitted On February 17, 1982, it was discovered by the NRC resident inspector on unit 2 that the rod position indicators (RPI) of two rods in shutdown bank A were indicating greater than 312 steps with respect to the other RPIs in the bank.

Before this event, Sequoyah had been routinely maintaining the shutdown control rods fully withdrawn with the unit in modes 3, 4, or 5, regardless of system temperature, to provide additional safety in the event of a boron dilution or similar inadvertent criticality event.

The rod position indication is calibrated at normal operating temperature (NOT). The rod position indicator will not indicate actual rod position when the system temperature is less than NOT.

For these reasons, technical specification (tech spec) 3 1 3 3 was interpreted to be met if individual rod position indicators were within 112 steps of each ot h'e r.

When the February 17, 1982, event and tech spec 313 3 interpretations were discussed, it was discovered that there were differing opinions on the interpretation of tech spec 3 1.3.3 and some confusion existed.

It became apparent that no consistent clear interpretation of tech spec 3.1 3.3 existed among the operations personnel contacted.

The misinterpretation of tech spec 3 1.3.3 and the operating procedures reflecting this misinterpretation were the primary reasons for this violation.

3 Corrective Steps Which Have Been Taken and the Results Achieved (1) A licensee event report and supplemental information was sent to NRC on March 2, 1982.

(2) On February 18, 1982, a conference call was held with Nuclear Reactor Regulations (NRR) tech spec specialists concerning the tech spec 3 1 3 3 interpretation.

NRR stated that the requirements of tech spec 3 1.3.3 are met if the rod position indicator indicates actual rod position within 112 steps with reactor trip breakers in the closed position.

NRR was aware of the effects of temperature on the rod position indicators.

(3) Since the unit 2 startup event of February 17, 1982, the requirements of tech spec 3.1.3.3 have been met by both units by keeping shutdown rods fully inserted until NOT is reached.

This has been achieved by placing a statement to this effect in the operations night order book.

F Page 4 4.

Corrective Steps Which Will Be Taken To Avoid Further Violations A tech spec change request is being prepared to allow the shutdown rods to be withdrawn in modes 3, 4, and 5.

This is based on the recommendations from Westinghouse Electric Corporation and is a revision of the NRC specification on RPI operability when not critical but with trip breakers closed.

5.

Date When Full Compliance Will Be Achieved Full compliance was achieved on February 17, 1982.

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