ML20049J862

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IE Insp Rept 50-206/82-04 on 820104-29.Noncompliance Noted: Failure to Perform Design Review & Testing of Mods & Include Acceptance Criteria in Surveillance Procedures
ML20049J862
Person / Time
Site: San Onofre 
Issue date: 03/02/1982
From: Mendonca M, Miller L, Zwetzig G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML20049J857 List:
References
50-206-82-04, 50-206-82-4, NUDOCS 8203290168
Download: ML20049J862 (8)


See also: IR 05000206/1982004

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U. S. NUCLEAR REGULATORY COMMISSION

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REGION V

Report No. 50-206/82-04

Docket No. 50-206

License No.

opR_13

Safeguards Group

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Licensee: Southern California Edison Company

P.

O.

Box 800

Rosemead, California 91770

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Facility Name: San onofre Unit 1

Inspection at: San onofre, California

Inspection conducted: January 4-29, 1982

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Inspectors:

L . i bliOle r , GSi(nlo r Resident Inspector, Unit 1

Date' S,itjned

Y En l$A

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h ypo'nca

achident inspector (Diablo Canyon)

Date Signed

1

Date Signed

Approved by:

M b /NN

G.;6. Gwetz $ ,4Chici, Reactor Projects Section 1

Date $1gned

Reactor Operations Project Branch

Date Signed

Summary:

Inspection on January 4-29, 1982 (Report No. 50-206/82-04)

Areas Inspected: Routine resident operational safety

verification; monthly surveillance and maintenance

observations; follow-up on licensee event reports and

independent inspection.

The inspection involved 90

inspector-hours by two NRC inspectors.

Results:

Of the five areas examined, items of apparent

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noncompliance were identified in two areas (failure to

perform design review and testing of modifications - para-

graph 2 - Severity Level 4; and failure to include acceptance

criteria in surveillance procedures - paragraph 7 - Severity

Level 5).

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8203290168 820303

RV Form 219 (2)

PDR ADOCK 05000206

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PDR

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DETAILS

1.

Persons Contacted

  • W. Moody, Deruty Station Manager
  • B.

Katz, Station Technical Manager

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  • J,

Curran, Manager, Quality. Assurance

  • P.

Croy, Compliance and, Configuration Control Manager

  • W.

Marsh, Acting Health Physics Manager-

  • G.

ficDonald , Quality Assurance / Control Supervisor

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  • F.

Briggs, Compliance Engineer

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Salizar, Instrumentation and Control Foreman

R.

Waldo, Nuclear Engineer

S.

Goselin, Nuclear Engineer

The inspector also interviewed other licensee and contractor

employees during this inspection.

  • Denotes those attending the Exit Interview on January 29, 1982.

2.

Operational Safety Verification

The inspector observed Control Room operations frequently for

proper shift manning, for adherence to procedures and limiting

conditions for operation, and appropriate recorder and instrument

indications.

Control room valve position indications appeared

correct for power operation.

The inspector discussed the status of annunciators with Control

Room operators to determine the reasons for abnormal indications,

and to determine the operators' awareness of plant status.

Shift

turnovers were observed.

The Control Operator's Log was reviewed frequently to obtain

information on plant conditions, and to determine whether

regulatory requirements had been met.

The Watch Engineer's Log,

Tagout, Equipment Control, and Steam Generator Chemistry Logs

were also reviewed.

Radiation restricted area access points were generally safe and

clean.

Several radiation work permits were examined and found

to be completed correctly.

In addition, several radiation friskers

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and portal monitors were observed to be operating properly.

Radiation areas observed in the Auxiliary Building were correctly

posted.

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The Physical Security Plae :ppeared to be properly implemented.

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The inspector verified

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3 elected security posts were properly

manned, isolation cones w,2e clear, personnel searches were per-

formed-when required, vehicles were controlled within the protected

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area, and personnel were badged and escorted, as necessary.

Pro-

tected area barriers did not appear to be degraded.

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Plant housekeeping was adequate.

Fire barriers appeared intact.

The equipment control log and tagout log were audited.

No signif-

icant discrepancies were identified.

Several tagouts were verified

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to have been hung as indicated on the equipment control form.

Selected primary and secondary chemistry results were reviewed

and were acceptable.

The correct alignment of the feedwater recirculation flow path, the

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refueling water pumps and associated valves, the manual operators

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for the saltwater cooling pumps' discharge valves, and the diesel

generator starting air isolation valves was verified.

One signif-

icant discrepancy in the refueling water system was observed.

The inspector noted that Line 8007 (shown on the Miscellaneous Water

Systems Drawing 568776-17 ) had been cut in two places.

The line

formerly supplied seal cooling water to each refueling water

pump, but was functionally replaced with differect cooling

lines several years ago when the packing glands for the pumps

were replaced with mechanical seals.

The line was known to be

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intact on April 25, 1980, because the licensee inadvertently

borated the water in the Makeup Water Tank through it and the

adjoining Line 8028.

As a result of that event (LER 80-17), the

licensee proposed to replace and cap Line 8028.

The licensee

was unable to retrieve any documentation describing the cutting

or capping of either line, and the system drawing (568776) still

showed the line intact.

The inspector noted that the licensee's action to cut Line 8007

had created two potential leak points from the recirculation

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loop outside of containment.

Technical Specifications 3.3.1

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requires that leakage from this loop not exceed 625 cc/hr.

The

licensee verifies this requirement is met with Procedures S01-

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12.8-13, " Recirculation System Leakage Teat," and S01-12.6-1,

(same title).

However, neither procedure identified the cuts

through Line 8007 as points to observe for leakage, nor was there

any objective evidence that these points were known to the licensee

prior to their identification by the inspector

Appendix B of

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10 CFR 50 (Criteria III and XI); the licensee's approved Quality

Assurance Manual, Section 5; and ANSI N 18.7-1976, Section 5.2.7;

all require that modification activities be controlled consistent

with their importance to safety.

This modification apparently was

uncontrolled; and, as noted, created two potential leak points

from the recirculation loop directly to the environment.

Since

the recirculation loop becomes an extension of the containment

following certain accidents, this modification should have been

controlled.

This is an item of apparent noncompliance.

(0I 50-

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206/82-04-01)

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Upon being informed of this matter by tb3 inspector, the licensee

promptly performed a leakage test which demonstrated that there

was no seat leakage from either of the isolation valves to the

openings in Line 8007.

Following the test, the licensee capped

the opening at each refueling water pump.

The inspector concluded

from this test that Techical Specification 3.3.1,

limiting re-

circulation loop leakage, had not been violated due to this

modification.

At the Exit Interview, the inspector emphasized

that this event was significant in its potential for increasing

the consequences of an accident.

In addition, the inspector

noted that this was the third consecutive inspection to identify

errors in drawings or plant configuration.

In response to the last observation, licensee representatives

stated that several corrective actions had been.recently initiated.

These included a short term effort to promptly correct known error

in drawings, and a longer term effort to systematically verify

existing drawings through piping walkdowns.

The latter effort

is still in preparation.

Both activities appear to have the

active support of the Station Manager and the close supervision

of the Compliance and Configuration Control Manager.

The in-

spector stated that the performance of these corrective actions

would be closely monitored.

This previously identified item

relating to configuration control (01 50-206/81-42-01), remains

open.

3.

Follow-up on Inspector Identified Items

a.

OI 50-206/81-42-02:

Possible Waste Gas Decay System Leakage

The inspector reviewed preliminary results of two system

pressure tests which the licensee had performed.

Based on

the test results, the licensee's calculations indicate that

leakage from the system is less than 1.5 SCFH.

Further

data reduction is planned, however.

The inspector will

review the final report and corrective action.

This item

remains open

(01 50-206/81-42-02)

b.

01 50-206/81-42-03:

Seismic Qualification of Ashcroft

Pressure Gauges

The inspector reviewed a vendor report, " Seismic Testing of

Ashcroft Instruments," ASH /PI-3, dated June 23, 1978.

Based

on post-test visual inspection, this report indicated that

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the styles of gauges used by the licensee did not fail

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rtructurally at dynamic loads up to 10 G.

As in the ccse

of the seismic test of the diesel engine local panel, however,

this test did not verify the pressure integrity of the gauge

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following the test.

Nevertheless, the inspector concluded

that there was reasonable assurance that the gauges would

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not fail sufficiently to disable the system in which they

were installed.

A licensee representative stated that all

Style 1279 or 1301 Ashcroft pressure gauges used in safety-

related systems, or systems containing combustibles in

proximity to safety-related systems, would be replaced with

gauges qualified by a test comparable to that described in

the Wyle Laboratories test report dated July 14, 1977 (see

Inspection Report 50-206/81-42).

This replacement will be

performed on a time scale consistent with routine procurement

procedures upon identification of a gauge which satisfies

this test procedure.

This item remains open pending re-

placement of the gauges.

c.

01 50-206/81-42:

Seismic Supports for Feedwater Recirculation

Valves

The inspector examined drawings (568622-9, Section G-G,

and 568632-19, Section G-G) which show the piping configura-

tion for the feedwater pump recirculation lines and valves.

Based on this examination, the inspector concluded that

the drawings do not show the present piping configuration.

The inspector stated that since the present configuration

was installed in January, 1974 (Design Change 73-13), after

the licensee's Quality Assurance program was approved, records

of the scismic calculations for the feedwater recirculation

pipe should be available.

These calculations could not be

located by the licensee.

At the Exit Interview, a licensee

representative stated that the seismic calculations for this

piping would be promptly recovered or reanalyzed and supplied,

as appropriate.

The licensee also stated that any support

modifications necessary to ensure seismic adequacy would be

promptly performed following this review.

This item remains

open pending completion of the licensee's review.

No items of noncompliance or deviations were identified.

4.

Follow-up on Licensee Event Reports

a.

LER 81-24 (EFCOMATIC Valve Failures)

(0 pen)

The inspector determined that the licensee's development

of a maintenance program for these actuators had been de-

layed.

A licensee representative reaffirmed that refurbish-

ment of the existing actuators would start during the next

scheduled outage, and that the existing actuators world be

replaced on a time scale consistent with normal procurement

procedures.

At the Exit Interview, the inspector noted that

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CV-526, an EFCOMATIC Actuator Valve, failed to close on the

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first attempt when tested on January 28, 1982.

The valve

was subsequently lubricated, visually checked, and retested.

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It operated normally.

The inspector reiterated that continued

operation of this equipment with known discrepancies in the

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actuators has increased the risk of further valve failures.

The licensee maintains that multiple cycles of valve operation

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will, in any case, cause the valve to operate in a sufficiently

timely manner.

This item remains open pending demonstration of reliable

actuator performance by the licensee.

b.

LER 81-28 (Faulty Sequencer Operation)

(Closed)

Further discussions were-held with members o'f 'the technical

staff of the Office of Nuclear Reactor Regulation.

The

inspector was informed by the staff that the current sequencer

design is considered' deficient in that the block circuitry

is not redundant, and that inoperability of automatic sequenc-

ing is not annunciated.

However, the inoperability of

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automatic sequencing following sequencer reset was considered

to be acceptable.

The Office of' Nuclear Reactor Regulation

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staff is separately resolving the deficiencies cited above

with the licensee.

This item is closed.

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c.

LER 81-25 (Containment Isolation Valve Relay Failure)

(0 pen)

The licensee evaluated the failure of two containment isolation

valves to close during testing.

The conclusion reached by

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the licensee on December 8,

1981, was that the magnetic latch

relay for each associated solenoid valve failed due to mis-

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positioned contacts.

A licensee representative stated thtt

all Agastat Magnetic Latch relays would be inspected at the

next scheduled outage to verify that no others suffer from

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a similar defect.

The inspector reviewed the licensee's

evaluation of this event and stated that the proposed correc-

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tive action to inspect and replace as necessary was acceptable.

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This item remains open pending completion of this corrective

action.

d.

LER 81-22 (Low Snubber Fluid Level)

(0 pen)

The inspector determined that the licensee had not yet completed

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the preventive maintenance program revision committed to in

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its letter of October 20, 1981.

A licensee representative

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stated that this program revision would be made.

This item

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remains open.

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No items of noncompliance or deviations were identified.

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5.

Independent Inspection

A licensee representative reported to the inspector on January 5,

1982, that it was suspected that one or two rodlets on Control

Rod 6 -7 had broken free of the spider assembly hub or vane.

This

was believed to have occurred on December 12, 1981, during a reactor

startup.

At that time the rod initially did not appear to move

with its bank (Control Bank 2).

After adjusting a fuse clip for

the rod, the rod appeared to move normally.

However, incore therm-

ocouple maps and flux maps taken before and after December 12

indicate a region of uniform axial flux depression in the vicinity

of Control Rod

C-7.

The reactivity effect of this depression

appeared to be less than 40pcm.

No power distribution or thermal

limits were significantly changed.

The inspector thoroughly re-

viewed the licensee's analysis, and descriptions of rodlet failures

at

D.

C.

Cook, Salem and Yankee Rowe.

The inspector stated that the

licensee's evaluation appeared acceptable.

However, to provide

greater assurance that the analysis was correct, two commitments

were solicited.

A licensee representative agreed that at the

next scheduled shutdown the control rod would be fully exercised

over its entire range of travel.

In addition, the licensee would

obtain predictions of the flux depression expected if Control

Rod C-7 lost one or more rodlets or pieces of rodlets.

This item

remains open pending physical confirmation of the cause of the

observed reactivity changes.

(01 50-206/82-04-02)

6.

Follow-up on TMI Task Action Plan Item II.E.1.1 - Luxiliary

Feedwater System Evaluation

The inspector verified that procedures were implemented to ensure

(1) Auxiliary Feedwater System (AFW) valve alignment was estab-

lished and checked monthly (S01-12.3-6, " Safety Related Systems

Valve Alignment); (2) transfer to alternate soucces of AFW was

controlled (S01-1.2-1, " Loss of Coolant," and S01-7-3, " Auxiliary

Feedwater System"); (3) independent verifiaation of AFW re-

alignment following maintenance or testing was provided (S01-0-

114) and (4) manual initiation and control of AFW flow following

a loss of all AC power (S01-1.7-1, " Loss of Offsite Power",

Paragraph 4.6.2).

The inspector also verified that a dedicated fire hose had been

installed from the fire protection system to the AFW System suction

header.

This item remains open pending further review.

7.

Monthly Surveillance Observations

The inspectors witnessed portions of the following surveillances:

Monthly Control Rod Exercise Test (S01-12.3-24)

Monthly EFCOMATlc Valve Exercising (S01-12.3-25)

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Biweekly Recctor Plant Instrumentation Testing (S01-II-1.1)

Weekly Battery Inspection (S01-L-2.5)

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The inspector verified that the procedures used conformed with

applicable Limiting Conditions for Operation, that any test in-

strumentation used had been calibrated, and that test results

were acceptable.

The systems tested were properly removed from

and returned to service.

No test discrepancies were observed by

the inspectors.

While reviewing the completed biweekly reactor plant

instrumentation testing procedure, however, the inspector dis-

covered procedural errors.

This procedure provided quantitative

acceptance criteria generally by reference to values in the most

recent refueling interval calibration (S01-II-1.4).

However,

the values used in the biweekly test were not those reported in

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the most recent refueling interval calibration.

After discuss-

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ions with licensee personnel, it was determined that a decision

had been made informally to change the acceptance criteria of

the refueling interval test to more conservative values to

facilitate biweekly testing.

The method used to make this shift

in acceptance criteria was not specified in any procedure.

Con-

sequently, even after taking the shift into account, many minor

unexplained differences were observed between refueling interval

and biweekly interval reactor plant instrumentation testing accep-

tance criteria.

Following these observations, the inspector

reviewed the refueling interval calibration procedure (S01-II-1.4).

It was noted that in nearly all cases no quantitative acceptance

criteria for reactor plant trip setpoints were provided.

Licensee

personnel indicated that the setpoints were obtained from the

previous refueling calibration or from documents informally pro-

vided by other licensee personnel following system or Technicc1

Specification changes.

Technical Specification 6.8.1 and ANSI N

18.7-1976 require that procedures contain acceptance criteria

against which the success or failure of test-type activity should

be judged.

In this case, such criteria were not present.

This

is an item of apparent noncompliance.

(0I 50-206/82-04-03)

The

inepector reminded the licensee that this apparent violation was

a repetition of the violation cited by the Performance Appraisal

team in 1979, for which corrective actions were reported complete

in 1981.

8.

Monthly Maintenance Observations

The inspector observed the performance of test measurements on

the north saltwater pump circuit breaker (part of monthly pre-

ventive maintenance requirement SWO-2M-1).

This activity was

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performed in accordance with the approved procedure, did not

violate Limiting Condition for Operations, and had been a ppr( ved

as required prior to commencement of the work.

The inspector also

observed the return to service of this pump following completion

of this inspection and related maintenance on December 18, 1981.

The discharge valve for the pump (POV-6) failed to open until the

plant operator in attendance at the pump adjusted the manual con-

trol for the colenoid valve which controls the discharge valve.

The plant operators performing this test did not record this

deficiency, and returned the pump to service.

Subsequently, the

inspector also determined that some plant operators were unawcre

of the correct position of the manual controls for automatic

operation of these valves.

The inspector discussed with licensee

representatives his concern that sluggish operation of POV-6 was

not identified as a potential nonconformance.

These represen-

tatives agreed that it should have been identified, and promptly

took action to prevent recurrence:

A design review of the

valve manual operators was initiated to make these operators

less susceptible to inadvertent engagement than the present

operators; and operating personnel were formally reminded to

identify and document problems observed during the operation of

safety-related equipment.

This item remains open pending com-

pletion of the design review.

(OI 50-206/82-04-04)

No items of noncompliance or deviations were identified.

9.

Exit Interview

A meeting was held on January 29, 1982, to summarize the scope

and findings of this inspection.

In addition to the two items

of apparent noncompliance identified, the inspector emphasized

the importance of resolving the seismic condition of the feed-

water recirculation valves (Paragraph 3c) and of consistently

identifying nonconformances (Paragraph 8).

The inspector also

discussed some recent commitments in response to LERs 81-24.

81-25, and 81-22 which were not met on schedule.

A licensee

representative stated that these had been an administrative

oversights and would not become habitual.

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