ML20045A821

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Insp Rept 50-298/93-18 on 930426-30 & 0510-14.Violations Noted.Major Areas Inspected:Onsite Followup of Licensee Event Repts & Other Followup
ML20045A821
Person / Time
Site: Cooper Entergy icon.png
Issue date: 06/03/1993
From: Powers D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20045A814 List:
References
50-298-93-18, NUDOCS 9306150032
Download: ML20045A821 (14)


See also: IR 05000298/1993018

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APPENDIX B

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection Report:

50-298/93-18

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Operating License: DRP-46

Licensee:

Nebraska Public Power District (NPPD)

Facility Name:

Cooper Nuclear Station (CNS)

Inspection At:

CNS, Brownville, Nebraska

Inspection Conducted: April 26-30 and May 10-14, 1993

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Inspector:

C. E. Johnson, Reactor Inspector, Maintenance Section

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Division of Reactor Safety

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Approyed:

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d/3/98

Dr. Dale A. Powers, Chief, Maintenance Section

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Division of Reactor Safety

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Inspection Summar.y

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Areas Inspected:

Routine, announced inspection of onsite followup of licensee

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event reports and other followup.

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Results:

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A violation was identified pertaining to inadequate corrective

action and root cause determination taken in response to

performance problems with the control room ventilation radiation

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monitor (Section 2.4).

A violation was identified pertaining to an inadequate

10 CFR 50.59 safety evaluation of Design Modification DC 90-0226,

which contained an unreviewed safety question (Section 2.4).

The licensee's corrective actions pertaining to four licensee

event reports and unresolved items were adequate and met

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regulatory requirements, license conditions, and commitments.

However, the licensee's corrective actions and safety evaluation

of changes to radiation monitors were inadequate (Section 4.0).

Summary of Inspection Findinos:

Licensee Event Report 298/92-002 was closed (Section 2.1).

9306150032 930609

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Licensee Event Report 298/93-005'was closed (Section 2.2).

Licensee Event Report 298/93-006 was reviewed but not closed

(Section 2.3).

Licensee Event Report 298/91-020 was closed (Section 2.4).

Violations 298/9318-01 and 298/9318-02 were opened (Section 2.4).

Unresolved Item 298/9223-01 was closed (Section 3.1).

The licensee made a commitment to revise the Standard Clearance

Order to incorporate the use of the newly installed vents and

drains for the local leak rate testing of the reactor feedwater

check valves (Section 3.1).

Attachments:

Attachment 1 - Persons Contacted and Exit Meeting

Attachment 2 - Documents Reviewed

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DETAILS

1 PLANT STATUS

At the beginning of this inspection period, the plant was in day 52'of an 82

day scheduled refueling outage. The reactor was defueled and the reactor

cavity was flooded up with the fuel pool gates installed.

2 ONSITE REVIEW 0F LICENSEE EVENT REPORTS (92700)

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The purpose of this inspection was to determine through onsite followup of

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selected event reports, whether the licensee has taken corrective actions as

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stated in written reports of the events and if responses to the events were

adequate and met regulatory requirements, licensee conditions, and

commitments.

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2.1

(Closed) Licensee Event Report 298/92-002:

Reactor Vessel Water Level

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Setooint Inaccuracy Resultino from Reference Leo Temperature Effects that

had not been Correctly Addressed

On January 20, 1992, an advance copy of Supplement 2 to General Electric

Service Information Letter 299 was received by the licensee. The purpose of

the supplement was to notify boiling water reactor owners that the information

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in Service Information Letter 299, dated July 25, 1979, had been

misinterpreted by one utility and was potentially subject to misinterpretation

by others.

A clarification of the information was provided to the licensee,

along with a recommendation that a check of level instrument setpoint

calculations be conducted.

An evaluation was performed which determined that although the Service

Information Letter had been reviewed and properly considered when it was

originally received, incorrect initial conditions and incomplete calculations

for the Reactor Water Level 1 setpoint, prescribed in the Technical

Specifications, resulted in a non-conservative setpoint performed in 1981.

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The inspector reviewed the licensee's immediate corrective actions to adjust

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the setpoint within the required limit. Temporary Procedure Change

Notice 92-005 contained corrections to the calibration and functional test

procedure.

The licensee implemented the change immediately.

The licensee had

proceduralized the calculational methodology and provided for independent

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design basis reviews.

The licensee's immediate and long-term corrective actions were determined to

be appropriate.

This licensee event report is closed.

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2.2

(Closed) Licensee Event Report 298/93-005:

Excessive Primary Containment

Leakaae Discovered durina Local Leak Rate Testina of Reactor Feedwater

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Check Valves

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On March 10, 1993, upon completion of the local leak rate testing of the

reactor feedwater check valves, the as-found primary containment leak rate was

determined to exceed the acceptance criterion. The leakage of the reactor

feedwater check valves was too great to be accurately quantified using the

available test equipment.

A review by the licensee of the as-found leakage

rate of other components tested during this outage indicated that, had the

reactor feedwater check valves performed acceptably, the total as-found

leakage would not have exceeded the allowable containment leak rate.

This licensee event report is associated with Unresolved Item 298/9223-01

pertaining the reactor feedwater check valve leak rate and the valve and

system modifications, which have been completed.

Details of the modifications

are discussed in Section 3.1.

Local leak rate tests have been successfully

completed. The licensee committed in the exit meeting to updating the

Standard Clearance Order to incorporate the use of the new vents and drains as

part of the process for performing the local leak rate test.

Based on completion of the local leak rate tests, acceptable system

performance, and the commitment made by the licensee, this licensee event

report is closed.

2.3

(00en) Licensee Event Report 298/93-006:

Fire Barrier Doors Discovered

Open and Obstructed without a Continuous Fire Watch due to Personnel

Error

On March 16, 1993, at 11 p.m., two fire barrier doors were found open and

obstructed with no fire watch assigned as required by Technical

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Specifications.

The doors provided for passage from a stairwell into the high

pressure coolant injection pump room and residual heat removal pump room. The

door to the high pressure coolant injection pump room was obstructed with a

stanchion, while the door to the residual heat removal pump room was

obstructed with a 12-inch temporary ventilation duct that was connected to a

filter unit in the stairwell.

On April 10, 1993, at approximately 8:20 p.m., a fire barrier door to the

service water pump room at the intake structure was found open and obstructed.

A fire watch had been posted in the area continuously since April 4,1993,

because of work activities in progress.

Upon completion of work on April 10,

1993, the halon system was restored, but the integrity of the fire barrier

door was not re-established prior to departure of the fire watch at 5:20 p.m.

Review of the licensee's corrective action indicated that immediate corrective

actions were taken by removing obstructions and closing the doors. The

problems were reviewed by the outage directors at the outage coordination

meetings conducted at the beginning of each shift, and compliance with station

fire protection requirements were stressed.

Personnel involved were

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counseled. Additionally, a rovi'ng fire door patrol was initiated as a means

to assure that fire doors were closed or that a fire watch was stationed.

The inspector informed the licensee that it was not clear that'this issue was

stressed to other workers who might have the opportunity to place obstructions

in fire barrier doorways.

The inspector was informed that the licensee

planned on getting this message out to all personnel by memoranda or some

other means. The licensee was also in the process of reviewing the fire watch

implementation process to identify enhancements that will prevent recurrence.

This licensee event report will remain open pending NRC's review of the

licensee's completion of the aforementioned corrective actions.

2.4 (Closed) Licensee Event Report 298/91-020:

Failure of the Primary

Containment Intearated Leak Rate Test due to Drywell Ventilation Monitor

System and Containment Penetration leakaae

On December 10, 1991, at 12:35 a.m., during the performance of the primary

containment integrated leak rate test, the drywell ventilation monitor gaseous

detector mounting bolts were stripped from the lead shield to which_they were

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mounted.

This resulted in the detector being ejected from the lead shield

chamber.

Primary containment pressure was approximately 51.6 psig and was

being raised to the integrated leak rate test pressure of 58 psig.

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addition to this leak there were others, which were in the reactor water

cleanup system and the reactor feedwater system.

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The leakage from the drywell ventilation radiation monitor was quantified.

The monitor was then isolated and pressurization of the primary containment

continued to the required test pressure.

The drywell ventilation radiation monitor, Model I-RAK-225-lF, manufactured by

Nuclear Measurements Corporation, was designed, fabricated, and installed as

part of the original plant equipment. Over the years, numerous detector

calibration and maintenance efforts have required removal of the detector from

the shield chamber, which is primarily constructed of lead. This frequent

disassembly and reassembly resulted in degrading the shield chamber threaded

connections into which the detector was bolted.

When the unit was pressurized

during performance of the integrated leak rate test, the threaded engagement

of the retaining bolts in the shield chamber failed, resulting in ejection of

the detector.

On October 30, 1992, the licensee issued Design Change 90-0226, which replaced

the existing drywell ventilation monitor (RMV-RM-4) and the control room

ventilation radiation monitor (RMV-RM-1) during a scheduled refueling

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outage (RF15).

The licensee informed the inspector that there were many

problems over the years with these particular two monitors.

The inspector

requested from the licensee, Design Change 90-0226 and the history of the

monitors for review.

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The past and recent maintenance history revealed that over 50 nonconformance

reports were written against RMV-RM-1 and -4 (29 and 35, respectively). This

appeared to be an excessive amount of nonconformance reports for the two

monitors. The inspector inquired of the licensee what corrective actions had

been taken to resolve these problems, and if any root causes were ever

determined. The licensee stated that there has been no single root cause to

the problems, and that the monitors were obsolete and needed replacing.

The inspector reviewed a sample of these nonconformance reports. Of the

nonconformance reports reviewed by the inspector, several indicated that

different problems could have contributed to some of the failures,

i.e.,

vibration or high voltage.

However, it was not evident that the licensee

pursued either of these possibilities to determine if indeed these monitors

may have had inadequate supports or bracing to preclude vibration or whether

high voltage could have caused the monitors to be out of calibration. There

appeared to be no adequate corrective actions or root causes determined in the

nonconformance reports reviewed to prevent repetitive occurrences. Corrective

action that was taken was to replace or repair subcomponents.

Discussions on the current nonconformance reports with the licensee revealed

that these monitors were to be replaced during the outage in 1993; therefore,

the licensee's intent to repair or replace subcomponents was very limited.

The inspector informed the licensee that with no root cause determination,

there is no assurance that the new radiation monitors will resolve the

recurring problems.

Two specific examples of problems with the Control Room Ventilation Radiation

Monitor RHV-RM-1 are as follows:

(1)

Inadequate procedural guidance resulted in unintended high voltage

being admitted into the monitor during maintenance activities.

There were approximately four nonconformance reports written

pertaining to this issue on RMV-RM-1.

For instance,

Nonconformance Report 87-112 was written where failure was

attributed to procedure error, in that high voltage was not

reduced prior to the disconnection of the detector assembly of

RMV-RM-1. The vendor recommended maintenance practices required

that high voltage be turned off prior to disconnection and

reconnection of the detector assembly. The licensee's corrective

action was to revise certain procedures.

One year later,

Nonconformance Reports89-061, 89-156, and 89-157 were written for

procedure errors also relating to high voltage.

However, a

different procedure was involved for these problems.

It was

apparent that the scope of corrective measures did not capture all

applicable procedures relating to this error; therefore, recurrent

problems continued.

(2)

On January 29, 1993, Deficiency Report 93-018 was issued after the

control room ventilation radiation monitor was found by Chemistry

personnel to be malfunctioning.

In particular, the particulate

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channel's filter paper drive unit was not advancing. . Maintenance

Work Request 93-0347 was generated to investigate and repair the

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unit.

Subsequently, the filter paper drive unit was repaired.

The inspector learned, however, that the maintenance history on

this unit contained Nonconformance Report 90-125 that had also

been written against the filter paper drive unit due to a failed

belt. This earlier nonconformance report was voided after it was

determined that failure of the filter paper drive unit did not

render the monitor / channel inoperable. Consequently, Maintenance

Work Request 90-3578 was initiated to replace the belt.

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Engineering evaluated this event and concluded that a failure rate

of once every 9 years was not enough to warrant the addition of a

preventive maintenance item.

Later, in June 1991, Maintenance

Work Request 91-1868 was generated against this monitor / channel

because of another failure.

This maintenance work request also

found it necessary to replace the belt. The second failure of the

belt should have indicated to the licensee that the filter paper

drive unit could have possibly been defective causing the belt to

fail; therefore, the entire unit should have been replaced. These

examples indicate inadequate corrective action and root cause

determination to prevent recurrent problems.

The inspector concluded that corrective action and root cause determination of

RMV-RM-1 performance problems was inadequate. This is a violation of 10 CFR 50, Appendix B, Criterion XVI (50-298/9318-01).

Further review of Design Change 90-0226 by the inspector indicated that

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RMV-RM-1 and -4 were to be replaced by newer models. The inspector reviewed

the data sheets of the new monitors and determined that the new monitors were

rated at a design pressure of only 2 psig. The old monitors, specifically

RMV-RM-4 was rated at a design pressure of 58 psig, which would withstand the

design basis accident pressure.

The inspector reviewed the licensee's justification for the modification

change that included the following:

The existing control room and drywell ventilation radiation

monitors had become high maintenance items and were obsolete.

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Replacement would reduce equipment down time and maintenance cost.

The modifications to Penetration X-51 would make it possible to

protect the drywell ventilation radiation monitor from over

pressurization during the integrated leak rate test without

isolating the post accident sampling (PAS) system during the

integrated leak rate test.

Normally open isolation valves PC-V-43

and PC-V-229 would be required to be closed prior to the

integrated leak rate test.

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The inspector questioned the licensee's justification on whether this

modification considered the likelihood of a containment breach through

RMV-RM-4 during a design basis accident. The licensee told the inspector that

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RMV-RM-4 was not needed during a design basis accident because of the

following:

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(1)

There were two essential high radiation monitors installed that

would be utilized during design basis accident conditions, and

(2)

There are two manual isolation valves installed that would be

isolated during the integrated leak rate test to protect the

radiation monitor.

The licensee informed the inspector that additional justification for

containment breach was derived from General Electric Owners' Group Evaluation

of Containment Isolation Concerns, NEDC-22253, 82NED114 Class II, October

1982, Reference 9.0.1.12, which stated that potential offsite exposure from a

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break of a 1-inch inside diameter line was substantially below the 10 CFR 100

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offsite radiological limits.

The inspector reviewed the licensee's Station Safety Evaluation of this

modification change which included a 10 CFR 50.59 analysis.

Review of this

evaluation indicated that the licensee concluded the following:

The proposed change would not affect the safety function of any

system because the new RMV-RM-1 and -4 monitors met seismic

requirements.

This new design would not increase the chances for a release of

radioactivity.

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The new radiation monitors for the control room (RMV-RM-1) and

drywell (RMV-RM-4) performed the same Updated Safety Analysis

Report functions as the previous monitors.

The modification made for this design change would not create a

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possibility for an accident or malfunction of a different type

than any previously evaluated in the Updated Safety Analysis

Report.

The licensee also concluded in the 10 CFR 50.59 analysis that there were no

unreviewed safety questions that existed for this modification.

The inspector informed the licensee that his review of Design Change 90-0226

determined that Engineering did not perform an adequate 10 CFR 50.59 review,

in that, there was an unreviewed safety concern involved with the proposed

change.

This unreviewed safety concern pertained to the new radiation

monitor RMV-RM-4 design pressure rating of 2 psig, which was far below the

design basis accident pressure of 58 psig.

It appeared to the inspector that

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operation of the new radiation monitor at the time of a design basis accident

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would:

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Breach primary containment;

Subject personnel inside secondary containment to high radiation

levels as they exited (the monitor is located at a personnel

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access / egress point);

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Delay reentry into secondary containment as a result of

radioactive contamination; and

Increase the likelihood of radiation exposure to the general

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public.

The licensee informed the inspector that this concern was previously

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identified by them earlier in correspondence QAC93168 and QAC93169 dated

April 21 and April 22, 1993, respectively.

These documents addressed a

concern with the integrated leak rate test; however, they did not address the

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significant safety concern which was a breach of primary containment during a

design basis accident. The inspector questioned the licensee why no action

was ever taken to resolve their concern, especially when Design Change 90-0226

had been approved by nine groups (e.g., Engineering, Quality Assurance,

Standard Operation Review Committee). No conclusive answer was.given. Also,

no deficiency report or nonconformance report was written prior to the end of

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this inspection.

Discussions with . licensee design personnel indicated that there was no formal

hold on the field installation of this modification, and that final

configuration of this modification had not been decided. At the end of this

inspection, the inspector was informed that the licensee planned to use dual

automatic isolation valves that will be powered from a Class IE electrical

bus. This modification was in review.

Field observation by the inspector determined that the new RMV-RM-4 had been

installed in parallel with the old radiation monitor.

This change was

initiated by On-The-Spot Change No. 5.

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The inspector concluded that the licensee did not adequately evaluate this

modification, in that an unreviewed safety question existed and that the

modification was approved by the responsible organizations and installed in

the field without NRC approval.

This issue of proposing a design change that involved an unreviewed safety

question is a violation of 10 CFR 50.59 requirements (298/9318-02).

This violation does not oeet the criteria of a non-cited violation in that the

licensee identified a concern with emphasis pertaining to meeting Appendix J

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testing criteria to be close to the "as is" condition as practical. Whereas,

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a significant safety issue pertained to a breach of containment during a

design basis accident through a radiation monitor not designed to withstand

design basis accident pressure.

This licensee event report is closed.

3 FOLLOWUP (92701)

The purpose of this inspection was to perform an onsite followup inspection of

an unresolved item.

3.1

(Closed) Unresolved item 298/9223-01:

Timeliness and Effectiveness of

Corrective Actions Associated with local Leak Rate Test Failures of

Individual Feedwater Valves and Effects on Primary Containment System

Inteority

NRC Inspection Report 50-298/92-23 documented that there had been a number of

local leak rate test failures involving four feedwater system check valves

(RF-CV-13V, -140V, -15CV, and -16CV). These failures contributed to the

primary containment system exceeding its allowable leakage rate (.6 La).

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occurrence had resulted in the issuance of a nonconformance report and a

licensee event report, which documented the failures.

Each occurrence had

caused initiation of corrective actions which, by themselves, did not appear

to be effective.

Engineering provided a final written report on September 25, 1992, ir which

the results of a survey of check valves at other boiling water reactor

facilities were discussed.

Based on the survey results and a review of all

maintenance history applicable to the feedwater check valves, the following

recommendations were initiated:

A change to the feedwater check valve preventive maintenance,

which would require notification to the system engineer prior to

performing preventive maintenance to allow for a detailed

examination and evaluation of all internal components of the check

valves.

An engineering work request to install high point vents and low

point drains to provide adequate vent and drain paths during

system draining.

An engineering work request to remove the soft-seat rings, which

were not part of the original design. Also included in the plan,

was disc / seat / hinge pin bore alignment.

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which the required alignment and necessary machining was performed

in-situ and in one setup to provide the ultimate alignment and

disc / seat fitup (considered to be crucial for achieving acceptable

local leak rate test results).

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The inspector reviewed the corrective actions proposed by the licensee

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-documented in Engineering Work Request Nos.92-125 and 92-126 and Maintenance.

Work Requests Nos. 92-2719, 92-2720, 92-2721, 92-2722, 93-1097, and 93-1159.

Review of the. maintenance work requests indicated that the modification on the

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reactor feedwater valves had been completed with the exception of. the. soft

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seats, which were not replaced during this outage because-of a-six-month wait

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following purchase order issuance. The license planned to evaluate the soft

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seats at the next outage to determine if hard seats are actually necessary.

The licensee informed the inspector that use of a hard seat requires a

different disk which has to be' ordered at least 6 months in advance. After

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the completion of the. aforementioned repairs, the valves were tested.

During the inspection discussed in NRC Inspection Report 50-298/93-12, there

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were discussions on the method by which to test the valves.

The license

indicated that they would test the reactor feedwater valves by the following

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two methods:

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Fill the reactor feedwater system, secure the system,' drain down

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using the historical method, and perform the local leak rate. test.

Fill the reactor feedwater system, secure the system, drain down

using newly installed vents and drains, and then perform the local

leak rate test.

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This followup inspection determined that the licensee had conducted the two

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tests on these valves. The licensee had determined that use of the-historical.

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method of draining down had resulted in unacceptable check valve leakage;

whereas, the use of the newly installed vents and drains resulted in

acceptable check valve performance.

It is, therefore, believed that the

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licensee's long-standing problem with reactor feedwater check valve leakage

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arose when the licensee converted from the use of. water to air as the fluid

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for testing check valves. Apparently, when' draining down the system, a vacuum

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was pulled that unseated. check valves, and air pressure was not capable of re-

seating the check valve discs.

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The licensee committed to updating the Standard Clearance Order to incorporate

the new vents and drains as part of the process for performing the local leak

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rate test.

Based on completion of the local leak rate tests, acceptable

system performance, and the commitment made by the licensee in the exit

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meeting, this unresolved issue is closed.

4 CONCLUSION

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The licensee's corrective actions pertaining to four licensee event reports

and unresolved items were adequate and met regulatory requirements, license

conditions, and commitments. . However, in regard to a safety-related control

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room ventilation radiation monitor, the licensee's corrective actions and root

cause-determination to preclude repetitive problems were inadequate. Also,

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the licensee's 10 CFR 50.59 review of a design change modification to a

containment drywell ventilation radiation monitor was inappropriate.

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ATTACHMENT 1

1 PERSONS CONTACTED

1.1

Licensee Personnel

  • L. Bray, Regulatory Compliance Specialist

D. Buman, Lead Electric Engineer

  • M. Dean, Supervisor, Nuclear Licensing and Safety

K. Done, Supervisor, Mechanical

J. Dykstra, System Engineer

  • J. Flaherty, Manager, Engineering
  • R. Gardner, Plant Manager
  • S. Gayler, Administrative Secretary

B. McClillen, Lead Instrumentation and Controls Engineer

S. McClure, Manager, Nuclear Engineering

  • J. Meacham, Site Manager
  • C. Moeller, Supervisor, Technical Staff
  • S. Peterson, Senior Manager, Operations

M. Siedlik, Supervisor, Civil and Structural

  • G. Smith, Manager, Quality Assurance
  • M. Unruh, Manager, Maintenance

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  • W. Wenzl, Manager, Site Nuclear Engineering Department

B. Wilcox, Lead Mechanical Engineer

1.2 Stone & Webster Enaineerina Corporation

R. Sanchez, Senior Principal Mechanical Engineer

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1.3 NRC Personnel

  • R. Kopriva, Senior Resident Inspector
  • D. Powers, Section Chief, Maintenance Section, Division of Reactor Safety
  • W. Walker, Resident Inspector

In addition to the personnel listed above, the inspector contacted other

personnel during this inspection period.

  • Denotes personnel that attended the exit meeting.

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2 EXIT MEETING

An interim exit meeting was conducted on April 30, 1993, and an exit meeting

was conducted on May 14, 1993.

During these meetings, the inspector

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summarized the scope and findings of the inspections. The licensee did not

identify as proprietary, any information provided to, or reviewed by the

inspector.

During the May 14, 1993, exit meeting, Mr. J. Heacham, Site Manager, made a

commitment to revise the Standard Clearance Order to incorporate the use of

the newly installed vents and drains for the local leak rate testing of the

reactor feedwater check valves.

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ATTACHMENT 2

DOCUMENTS REVIEWED

DESIGN CHANGE (DC)

DC 90-0226

MINOR DESIGN CHANGE (MDC)

MDC 80-55

MAINTENANCE WORK RE0 VESTS (MWR)

MWR 93-1159

MWR 92-2721

MWR 92-2722

MWR 92-2720

MWR 92-2719

MWR 93-1097

OVALITY ASSURANCE LETTERS

QAC93168, dated April 21, 1993

QAC93169, dated April 22, 1993

EQUIPMENT OVALIFICATION DATA PACKAGES (HIGH RADIATION MONITORS)

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NO. 225

NO. 225, APPENDIX A

NO. 227

REGULATORY DOCUMENTS

NUREG-0800, Standard Review Plan, " Containment Isolation System"

NUREG-0737, TMI Action Plan

SAFETY GUIDE II, " Instrument lines Penetrating Primary Reactor

Containment," dated March 10, 1971

PROCEDURES

Surveillance Procedure 6.2.2.1.1, "CSCS Water Level Calibration

And Functional Test," Revision 23

Maintenance Procedure 7.0.8, " Pressure Testing," Revision 7

Engineering Procedure 3.26, " Instrument Setpoint Control,"

Revision 16

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General Operating Procedure 2.1.1, "Startup Procedure,"

Revision 62

CNS Procedure 0.5.1, "Nonconformance And Corrective Action,"

Revision 9

ENGINEERING WORK RE0 VESTS (EWR)

EWR 92-079

EWR 92-126

EWR 92-125

NONCONFORMANCE REPORTS (NCR)

NCR 90-130

NCR 90-018

NCR 90-028

NCR 90-110

NCR 91-014

NCR 91-092

NCR 91-123

NCR 92-118

NCR 92-058

NCR 93-028

OTHER ITEMS REVIEWED

Integrated leak rate test results (containment)

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Local leak rate test results (reactor feedwater check valves)

Procurement records (high radiation, control room and drywell

monitors)

CNS USAR

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