ML20042C503
| ML20042C503 | |
| Person / Time | |
|---|---|
| Site: | Indian Point |
| Issue date: | 10/02/1981 |
| From: | Connell C POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK |
| To: | |
| Shared Package | |
| ML20042C497 | List: |
| References | |
| NUDOCS 8203310460 | |
| Download: ML20042C503 (6) | |
Text
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OPERATLNG DATA REPORT DOCKET NO.
50-286 DATE 10-2-81 CONIPLETED BY C. Connell TELEPHONE (914) 739-8200 OPERATING STATUS
- 1. Unit Name: Incli nn Pnine w.1 wcle,r pnver 91,ne Notes
- 2. Reporting Period:
An*n+nr 1981
- 3. Licensed Thermal Power (5 twt):
1025
- 4. Nameplate Rating (Gross StWe):
1013
- 5. Design Electrical Rating (Net StWe):
965
- 6. Staximum Dependable Capacity (Gross 5tWc):
926
- 7. Staximum Dependable Capacity (Net $1We):
891
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7)Since Last Report. Give Reasons:
'ffone
- 9. P:wcr Level To Which Restricted. !f Any (NetatWe):
607 Mwo (At unity Factor).
- 10. Reasons For Restrictions. If Any:
rini r innel restricted to the canacity of one main trans-former.
This Stonth Yr..to.Date Cumulative
- 11. Ilours In Reporting Period 720 6551 4'4,592
- 12. Number Of liours Reactor Was Critical 98.4 4469.1 31,219.1
- 13. Reactor Reserse Shutdown !!ours 0
0 05
- 14. Hours Generator On Line 96.9 4381.6 30.084.7
- 15. Unit Reserve Shutdown Hours 0
0 0
- 16. Gross Thermal Energy Generated (5tWH) 196.767 9,048,940 76,680,210
- 17. Gross Electrical Energy Generated (SIWH) 51.480 2.505.960 24,097,461
- 18. nit Electrical E.crgy Generated (SIWH1 48,470 2,364,707 23,078,867
- 19. Unit Service Factor 13.5 66.9 67'.5
- 20. Unit Availability Factor 13.5 66.9 67.5
- 21. Unit Capacity Factor (Using 51DC Net) 76 40 s sa 1
- 22. Unit Capacity Factor'(Using DER Net) 7.0 37.4 53.6
- 23. Unit Forced Outage Rate 63.6 28.1 1.4
- 24. Shutdowns Scheduled Over Next 6 Stonths (Type. Date and Duration of Eacht:
p.-
Mnfuelino Outace in January.
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Units In Test Status (Prior to Commercial Operation):
Forecast' Ac'hieve'd '
INITIA L CRITICA LITY N/A N/A INITIAL ELECTRICITY N/A N/A
~
CONIM ERCI A L OPER ATION N/A N/A t
8203310460 811015 14/77)
PDR ADOCK 05000286 R
=__
s UNIT SilUTDOWNS AND POWER REDUCTIONS DOCKETNO.
50-286 UNIT NAME NO-3 DATE 10-2-91 COMPLET1?D BY c connell REPORT MONT11 Sentember 1981 TELEPilONE 314-739-8200-E E
jg 3
yYl Licensee
,E, r, En Cause A Currective o
N...
Date Q
gg i
2g&
Event y
pV Action to f
g;f3 g Report 2r in U Prevent Recurrence H
g c5 08A 810905 S
454.2 B
1 EB TRANSF Scheduled maintenance / installation of
- 32 Main Transformer.
~08B 810923 P
Abt. 9 A
4 81-007/OlT-O CB HTEXCH 431 Steam Generator tube leak.
Per-F forming eddy current inspection of all four steam generators and plug any defective tubes.
Method of Shutting Down (Other)
Criticality was never achieved. When proceeding to Hot Shutdown a primary.
to secondary leak was verified and the unit was returned to cold shutdown.
l-1 2
3 4-F: Forced Reason:
Mettu>d:
Exhibit P-Insteuctions S: Scheduled A Eiluipment Failure (Explain) 1-Manual
.for Preparation of Data Il Maintenance of Test 2 Manual Scram.
Entry Sheets for Licensee C Refueling 3 Aufomatic Scram.
Event Reposi (I.ER) File (NtlREG-D Regulatory Restriction 4-Ot her (Explain) 016I)
E-Operator Training & License Examination
' F Administ ative 5
G-Operational Eiror (Explain)
Exhibit II-Same Source (9/77)
Il-Olher (Explain) a
AVI It AGl. D AILY UNil POWI.It 1.INEl.
DOCKET NO.
4h17 T63s.ui Pbint tyggy tJo.3
~
DATE
-Oct. 2.
1981 C051PLETED IlY C. Connei1 TELEPl!ONE 914-739-8200 AlONT!!
nont ombo r 1981 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (S!We Net)
DiWe Net) 51b 17 0
I 2
si; 18 0
3 516 19 0
4 471 20 0
5 0
21 0
6 O
22 0
7 n
23 0
8 0
24 0
9 0
25 0
10 0
26 0
11.
0 27 0
12 0
2S 0
13 0
29 0
.l4 0
30 0
0 3g 16 0
INSTitUCTIONS
-.On this fornut, list the userage daily unit power level hih!We Net for each dayin tiie reposting month. Comp ste to ii,
,,e m,i,,lmie m eg, 2ii.
(9/771 e
MOTITII1Y tikIllTE!IAliCE 16PCRT I
S nterber 1981 Month
- DATE, W. R.
E EQUIPMElfr MAIEUtiCTIOt3 CORRECTIVE ACTIOli 9-29 I-2193 Radiation Monitors Rll/R12, Gasket Leak Tightened Joints.
R13 9-11 I-2311 valve 869A Valve Leaked Through Disassembled / Cleaned Seating Eurface Reasserbled 9-14 I-2308 Valve SOV-1539 Valve Will Not Operate Tightened Loose Connection 9-13 I-2312
- 31 Fan Cooler Unit NONE Replaced Motor Coils I-2313
- 32 Fan Cooler Unit Replaced Motor Coils I-2314
- 33 Fan Cooler Unit Replaced Motor Coils I-2315
- 34 Fan Cooler Unit Replaced Motor Coils I-2316
- 35 Fan Cooler Unit Replaced Motor Coils 9-28 I-2328 Steam Generator Blowdown Packing Leaks Furmanited Stuffing Boxes Stop Valves 9-17 I-2264 SWN-4-5-6-7 Valves Leaked Through Replaced Valves 9
O e
HONT11LY I & C CATEGORY I REPORT Serto-ber 1941 Month
(
Date i
W.R.
Equipment Malfunction Corrective Action 3
6/10/81 IC-1-1412-2 Primary Auxiliary Bldg.
Control & Readout Drawer in Replaced slow speed drive Air Particulate Detector control room was blowing fuses motor 6/11/81 IC-1-1316-2 Boric Acid Heat Trace Circuit #40 thermostat was Replaced defective therme-defective stat 9/28/81 IC-1-1471-2 FT-981 & FT-902 Safety NOME Replaced amplifiers in Injection 6 inch cold transmitters to meet leg flow instruments on Environmental Qualifi-loops 2 and 4 cations 9/30/81 IC-1-1419-2 Reactor Protection RT-10 relay in reactor trip Replaced RT-10 relay Train B logic was defective, coil burned out 9/30/81 IC-1-1398-2
- 32 Auxiliary Boiler Tachometer reads low Replaced local indicator i
s
Summary of Operating Experience September 1981 Indian Point Unit 3 was synchronized to the bus for a total of 96.9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br />, producing a gross generation of 51,480 !!We for this reporting period.
The unit was removed from service at 0051 hours5.902778e-4 days <br />0.0142 hours <br />8.43254e-5 weeks <br />1.94055e-5 months <br /> on September 5 for a scheduled outage. The purpose of the outage was to complete the installation of a replacement transformer for No. 32 main transformer and perform type B and C testing of the containment isolation valves. Upon completion of the outage related work the unit commenced a r.ormal startup. While at hot shutdown a primary to secondary leak developed in #31 steam generator.
At 2305 hours0.0267 days <br />0.64 hours <br />0.00381 weeks <br />8.770525e-4 months <br /> that same day the unit commenced an orderly cooldown and cold shutdown was achieved at 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br /> on September 24, 1981. The reactor coolant system has been drained, the leakir.g tube identified (Row 12 column 2 cold leg) and extensive eddy current inspects of all four generators is
'9 presently in progress.
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