ML20042C503

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Monthly Operating Rept for Sept 1981
ML20042C503
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 10/02/1981
From: Connell C
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
Shared Package
ML20042C497 List:
References
NUDOCS 8203310460
Download: ML20042C503 (6)


Text

'

OPERATLNG DATA REPORT

> DOCKET NO. 50-286

. DATE 10-2-81 CONIPLETED BY C. Connell -

TELEPHONE (914) 739-8200 OPERATING STATUS *

1. Unit Name: Incli nn Pnine w.1 wcle,r pnver 91,ne Notes
2. Reporting Period: An*n+nr 1981
3. Licensed Thermal Power (5 twt): 1025
4. Nameplate Rating (Gross StWe): 1013 ,
5. Design Electrical Rating (Net StWe): 965
6. Staximum Dependable Capacity (Gross 5tWc): 926
7. Staximum Dependable Capacity (Net $1We): 891
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7)Since Last Report. Give Reasons:

'ffone

9. P:wcr Level To Which Restricted. !f Any (NetatWe): 607 Mwo (At unity Factor).
10. Reasons For Restrictions. If Any: rini r innel restricted to the canacity of one main trans-former. ,'

This Stonth Yr..to.Date Cumulative

11. Ilours In Reporting Period 720 6551 4'4,592
12. Number Of liours Reactor Was Critical 98.4 .

4469.1 31,219.1

13. Reactor Reserse Shutdown !!ours 0 0 05
14. Hours Generator On Line 96.9 4381.6 30.084.7
15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Thermal Energy Generated (5tWH) 196.767 9,048,940 76,680,210
17. Gross Electrical Energy Generated (SIWH) 51.480 2.505.960 24,097,461
18. nit Electrical E .crgy Generated (SIWH1 48,470 2,364,707 23,078,867
19. Unit Service Factor 13.5 66.9 67'.5
20. Unit Availability Factor 13.5 66.9 67.5
21. Unit Capacity Factor (Using 51DC Net)
  • 76 40 s sa 1
22. Unit Capacity Factor'(Using DER Net) 7.0 37.4 53.6
23. Unit Forced Outage Rate 63.6 28.1 1.4
24. Shutdowns Scheduled Over Next 6 Stonths (Type. Date and Duration of Eacht: p.-

Mnfuelino Outace in January. - -

25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units In Test Status (Prior to Commercial Operation): Forecast' Ac'hieve'd '

INITIA L CRITICA LITY N/A N/A INITIAL ELECTRICITY N/A N/A ~

CONIM ERCI A L OPER ATION N/A N/A t

8203310460 811015 14/77)

PDR ADOCK 05000286 .

R PDR _

=__

s DOCKETNO. 50-286 UNIT SilUTDOWNS AND POWER REDUCTIONS UNIT NAME NO- 3 DATE 10-2-91 REPORT MONT11 Sentember 1981 COMPLET1?D BY c connell _,

TELEPilONE 314-739-8200-

- E E

-, jg 3 yYl Licensee ,E, r, Eno Cause A Currective N. .. Date Q gg i 2g& Event y pV Action to H

f $ g;f3 g Report 2r in U g Prevent Recurrence .

c5 08A 810905 S 454.2 B 1 EB TRANSF Scheduled maintenance / installation of

  1. 32 Main Transformer.

~08B 810923 P Abt. 9 A 4 81-007/OlT-O CB HTEXCH 431 Steam Generator tube leak. Per-F forming eddy current inspection of all four steam generators and plug any defective tubes.

Method of Shutting Down (Other)

Criticality was never achieved. When proceeding to Hot Shutdown a primary.

to secondary leak was verified and the unit was returned to cold shutdown.

l- 1 2 3 4-F: Forced Reason: Mettu>d: Exhibit P-Insteuctions S: Scheduled A Eiluipment Failure (Explain) 1-Manual .for Preparation of Data Il Maintenance of Test 2 Manual Scram. Entry Sheets for Licensee C Refueling 3 Aufomatic Scram. Event Reposi (I.ER) File (NtlREG-D Regulatory Restriction 4-Ot her (Explain) 016I)

E-Operator Training & License Examination

' F Administ ative 5 G-Operational Eiror (Explain) Exhibit II- Same Source (9/77) Il-Olher (Explain) a

AVI It AGl. D AILY UNil POWI.It 1.INEl.

DOCKET NO. 4h17 T63s.ui Pbint tyggy tJo.3

' ~

DATE -Oct. 2. 1981 C051PLETED IlY C. Connei1 TELEPl!ONE 914-739-8200 AlONT!! nont ombo r 1981 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL '

(S!We Net) DiWe Net)

I .. 51b 17 0 2 si; 18 . 0 3 ._ 516 19 0 4 471 20 0 5 0 21 0 6 O 22 0 7 n 23 0 8 0 24 0 9 0 25 0 10 0 26 0 _

11. 0 27 0 12 0 2S 0 13 - 0 29 0

.l4 - - - -

0 30 0 _ , _ _ _ _ _ _ , _ _

!$ 0 3g _ , , , _ , _ , , , .

16 0 INSTitUCTIONS

, -.On this fornut, list the userage daily unit power level hih!We Net for each dayin tiie reposting month. Comp ste to ii, ,,e m ,i ,,lmie m eg , 2ii. -

(9/771 e

I MOTITII1Y tikIllTE!IAliCE 16PCRT -

S nterber 1981

. Month DATE, W. R. E '

EQUIPMElfr MAIEUtiCTIOt3 CORRECTIVE ACTIOli 9-29 I-2193 Radiation Monitors Rll/R12, Gasket Leak Tightened Joints.

R13 9-11 I-2311 valve 869A Valve Leaked Through Disassembled / Cleaned Seating Eurface Reasserbled 9-14 I-2308 Valve SOV-1539 Valve Will Not Operate Tightened Loose Connection 9-13 I-2312 #31 Fan Cooler Unit NONE Replaced Motor Coils I-2313 #32 Fan Cooler Unit "

Replaced Motor Coils I-2314 #33 Fan Cooler Unit "

Replaced Motor Coils I-2315 #34 Fan Cooler Unit "

Replaced Motor Coils

. I-2316 #35 Fan Cooler Unit "

Replaced Motor Coils 9-28 I-2328 Steam Generator Blowdown Packing Leaks Furmanited Stuffing Boxes Stop Valves 9-17 I-2264 SWN-4-5-6-7 Valves Leaked Through Replaced Valves 9

O e

HONT11LY I & C CATEGORY I REPORT ,

Serto-ber 1941 Month Date W.R.

(

i # Equipment Malfunction Corrective Action 3

6/10/81 IC-1-1412-2 Primary Auxiliary Bldg. Control & Readout Drawer in Replaced slow speed drive Air Particulate Detector control room was blowing fuses motor 6/11/81 IC-1-1316-2 Boric Acid Heat Trace Circuit #40 thermostat was Replaced defective therme-defective stat 9/28/81 IC-1-1471-2 FT-981 & FT-902 Safety NOME Replaced amplifiers in Injection 6 inch cold transmitters to meet leg flow instruments on Environmental Qualifi-loops 2 and 4 cations Reactor Protection RT-10 relay in reactor trip Replaced RT-10 relay 9/30/81 IC-1-1419-2 Train B logic was defective, coil burned out

  1. 32 Auxiliary Boiler Tachometer reads low Replaced local indicator 9/30/81 IC-1-1398-2 i

s

Summary of Operating Experience September 1981 Indian Point Unit 3 was synchronized to the bus for a total of 96.9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br />, producing a gross generation of 51,480 !!We for this reporting period.

The unit was removed from service at 0051 hours5.902778e-4 days <br />0.0142 hours <br />8.43254e-5 weeks <br />1.94055e-5 months <br /> on September 5 for a scheduled outage. The purpose of the outage was to complete the installation of a replacement transformer for No. 32 main transformer and perform type B and C testing of the containment isolation valves. Upon completion of the outage related work the unit commenced a r.ormal startup. While at hot shutdown a primary to secondary leak developed in #31 steam generator.

At 2305 hours0.0267 days <br />0.64 hours <br />0.00381 weeks <br />8.770525e-4 months <br /> that same day the unit commenced an orderly cooldown and cold shutdown was achieved at 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br /> on September 24, 1981. The reactor coolant system has been drained, the leakir.g tube identified (Row 12 column 2 cold leg) and extensive eddy current inspects of all four generators is

'9 presently in progress.

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