ML20040H036

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Monthly Operating Rept for Jan 1982
ML20040H036
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 02/01/1982
From: Bogart D
FLORIDA POWER CORP.
To:
Shared Package
ML20040H035 List:
References
NUDOCS 8202170041
Download: ML20040H036 (4)


Text

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OPERATING DATA REPORT DOCKET NO.

50-302 DATE 7/1/82 CO.\\1PLETED BY n nncAnr TELEPif0NE ronn 79%6486 OPERATING STATUS

1. Unit Name:

Crystal River Unit #3 Notes

2. Reporting Period:

1/1/82 - 1/31/82

3. Licensed Thermal Power (31Wt):

2544

4. Nameplate Rating (Gross SIWE):

890

5. Design Electrical Rating (Net 31We):

825

6. 3!aximum Dependable Capacity (Gross $1We):

845

7. 31aximum Dependable Capacity (Net alwe):

806

8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report.Gise Reasons:

Mnc rnrines chanced based on limited operatine history at new power level of 2544 M L

9. Power Lesel To which Restricted,if Any (Net 31We):

None

10. Reasons For Restrictions. I.f Any:

N/A This Stonth Yr..to.Date Cumulative

11. liours in Reporting Period 744 744 42864
12. Number Of ifours Reactor Was Critical 656.8 656.8 26106.19
13. Reactor Resene Shutdown flours 3.0 3.9 1213.12
14. liours Generator On-Line 644.',

644.5 25456.68-

15. Unit Resene Shutdown flours 0

0 0

16. Gross Thermal Energy Generated 61Wil) 1604723 1604723 56971664 11 Gross Electrical Energy Generated (51Will 554782,_,

529792 18359090 554782 19354373

15. Net Electrical Energy Generated (3 WII) 529792
19. Unit Senice Factor 86.6%

86.6%

59.4%

20. Unit Asailability Factor 86.6%

86.6%

59.4%

21. Unit Capacity factor (Using.\\tDC Net t 88.3%

88.3%

53.1%

2.'

Unit Capacity Factor tU>ing DER Neti 86.3%

86.3%

51.9%

2.'

Unit Forced Outage R:,te 13.4%

13.4%

26.3%

24. Shutdowns Scheduled Oser Next 6 %!onths IT pe. Date.and Duration of Fach1:

3 N/A 25 If Shut Down \\t End Ol' Report Period. Estimated Date of Startup:

2/6/82 26 Units in Test St.aus iPrior io Commercial Operation r Foreca t Achiesed INITi \\ L CRITICA LITY 1/14/77 INITI \\L ELECTRICITY 1/30/77 CO\\1\\lERCI \\L OPER \\ TION 3/13/77 i

8202170041 820208

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PDR ADOCK 05000302 R

PDR

.. AVER AGE DAILY UNIT POWER LEVEL i

4 DOCKET NO.' 302 UNIT FLCRP-3 DATE 2/1/82 CON!PLETED BY D. Bogart

. TELEPHONE (9041 795-6486 SiONTH January 1982 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL

(%1We NetI (slwe Net)

I 825 17 819 2

843 824 33 3

837 19 671 4

861 20 707 817 821 e

21 6

22 885 848 816 7

33 s

838 24 843 9

838 854 25 10 543 26 839 492 11 27 842 e

12 825 73 359 832 0

13 39 844 14 30 I5 31 0

g e, 864 i

F INSTRUCTIONS On this : - nat. ist tin:. m p a n.,

!we Nei f or eash Ja> n: :h. rep.irtug m,. nth. (.mpute to

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DOCKET NO. Snan?

UNIT S!!UIDOWNS AND POWER REDUCTIONS UNII NAME FT rup t DATE Z/1/_d2 COMPLETED IlY hi U.

CULVER RI i'ORI MONTil 1/82 TELEPilONE,(Sna) 74c;_Aagg c

I u,.

Cause & Corrective i.er$t

  1. .b; I'
5) h 3

N A' ' '"" 8 "

53 S.!

253 Repori Ed Proent Recurrence

~

6 e6 82-1 820110 F

14.98 A

3 N/A Cll VALVEX FWV-31 failed to stroke during a monthly feedwater functional test.

This resulted in the trip of "A" mainfeed pump and eventually in a trip of the unit on high pressure.

82-2 820118 S

46.8 B

N/A N/A IIF llTEXCll Reduced power to clean all four condenser waterboxes.

82-3 820128 F

84.5 A

1 No LER num-SF VALVEX Unidentified leakage > 1gpm. After bers assigne<l shutting down the leak was discovered yet.

NCOR to be a crack in the weld between numbers are:

MUV-43 and the IIPI nozzle on loop A.

82-27 MUV/HP :

Plan to check the other nozzles for nozzle crack cracking as well as repair the known 82-25 RCP A crack before starting up.

Also, a seal package cract was discovered in RCP A seal crack package. The seal will be rebuilt.

l 2

3 4

l' l'ou ed Reason Method:

lixhibit G-Instructions S S beit n!cd A Equipment Failure (Explain) 1 -Manual for Picparation of Data II. Maintenance of Test 2 Manual Scram.

Entry Sheets fot 1.icensee C Itefueling

'3. Automatic Scram.

Event ReporI(1.l R)l'ile tNURI G-D Regulatory Restriction 4.Ot her (lixplain) 0161) i Operator Training & l.icense Examination I.Adnunkirative 5

G Operational I.rror (lixplain)

Exhibit I-Same Source es/77)

I! 01her t hplain)

o MONTHLY OPERATIONAL SU!2iARY STATDIENT DOCKET NO.50-302 UNIT FLCRP-3 DATE 2/1/82 COMPLETED BYM.W. CULVER TELEPHONE'(904) ~i95-6486 MONTH January 1982' SRSIARY STATDIENT:

The init experienced two forced shutdowns and'one power reduction during the raonth.

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