ML20040H036
| ML20040H036 | |
| Person / Time | |
|---|---|
| Site: | Crystal River |
| Issue date: | 02/01/1982 |
| From: | Bogart D FLORIDA POWER CORP. |
| To: | |
| Shared Package | |
| ML20040H035 | List: |
| References | |
| NUDOCS 8202170041 | |
| Download: ML20040H036 (4) | |
Text
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OPERATING DATA REPORT DOCKET NO.
50-302 DATE 7/1/82 CO.\\1PLETED BY n nncAnr TELEPif0NE ronn 79%6486 OPERATING STATUS
- 1. Unit Name:
Crystal River Unit #3 Notes
- 2. Reporting Period:
1/1/82 - 1/31/82
- 3. Licensed Thermal Power (31Wt):
2544
- 4. Nameplate Rating (Gross SIWE):
890
- 5. Design Electrical Rating (Net 31We):
825
- 6. 3!aximum Dependable Capacity (Gross $1We):
845
- 7. 31aximum Dependable Capacity (Net alwe):
806
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report.Gise Reasons:
Mnc rnrines chanced based on limited operatine history at new power level of 2544 M L
- 9. Power Lesel To which Restricted,if Any (Net 31We):
None
- 10. Reasons For Restrictions. I.f Any:
N/A This Stonth Yr..to.Date Cumulative
- 11. liours in Reporting Period 744 744 42864
- 12. Number Of ifours Reactor Was Critical 656.8 656.8 26106.19
- 13. Reactor Resene Shutdown flours 3.0 3.9 1213.12
- 14. liours Generator On-Line 644.',
644.5 25456.68-
- 15. Unit Resene Shutdown flours 0
0 0
- 16. Gross Thermal Energy Generated 61Wil) 1604723 1604723 56971664 11 Gross Electrical Energy Generated (51Will 554782,_,
529792 18359090 554782 19354373
- 15. Net Electrical Energy Generated (3 WII) 529792
- 19. Unit Senice Factor 86.6%
86.6%
59.4%
- 20. Unit Asailability Factor 86.6%
86.6%
59.4%
- 21. Unit Capacity factor (Using.\\tDC Net t 88.3%
88.3%
53.1%
2.'
Unit Capacity Factor tU>ing DER Neti 86.3%
86.3%
51.9%
2.'
Unit Forced Outage R:,te 13.4%
13.4%
26.3%
- 24. Shutdowns Scheduled Oser Next 6 %!onths IT pe. Date.and Duration of Fach1:
3 N/A 25 If Shut Down \\t End Ol' Report Period. Estimated Date of Startup:
2/6/82 26 Units in Test St.aus iPrior io Commercial Operation r Foreca t Achiesed INITi \\ L CRITICA LITY 1/14/77 INITI \\L ELECTRICITY 1/30/77 CO\\1\\lERCI \\L OPER \\ TION 3/13/77 i
8202170041 820208
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PDR ADOCK 05000302 R
.. AVER AGE DAILY UNIT POWER LEVEL i
4 DOCKET NO.' 302 UNIT FLCRP-3 DATE 2/1/82 CON!PLETED BY D. Bogart
. TELEPHONE (9041 795-6486 SiONTH January 1982 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL
(%1We NetI (slwe Net)
I 825 17 819 2
843 824 33 3
837 19 671 4
861 20 707 817 821 e
21 6
22 885 848 816 7
33 s
838 24 843 9
838 854 25 10 543 26 839 492 11 27 842 e
12 825 73 359 832 0
13 39 844 14 30 I5 31 0
g e, 864 i
F INSTRUCTIONS On this : - nat. ist tin:. m p a n.,
!we Nei f or eash Ja> n: :h. rep.irtug m,. nth. (.mpute to
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'hc (104l61 w h' >lf.'?ic y ; A.,
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DOCKET NO. Snan?
UNIT S!!UIDOWNS AND POWER REDUCTIONS UNII NAME FT rup t DATE Z/1/_d2 COMPLETED IlY hi U.
CULVER RI i'ORI MONTil 1/82 TELEPilONE,(Sna) 74c;_Aagg c
I u,.
Cause & Corrective i.er$t
- .b; I'
- 5) h 3
N A' ' '"" 8 "
- 53 S.!
253 Repori Ed Proent Recurrence
~
6 e6 82-1 820110 F
14.98 A
3 N/A Cll VALVEX FWV-31 failed to stroke during a monthly feedwater functional test.
This resulted in the trip of "A" mainfeed pump and eventually in a trip of the unit on high pressure.
82-2 820118 S
46.8 B
N/A N/A IIF llTEXCll Reduced power to clean all four condenser waterboxes.
82-3 820128 F
84.5 A
1 No LER num-SF VALVEX Unidentified leakage > 1gpm. After bers assigne<l shutting down the leak was discovered yet.
NCOR to be a crack in the weld between numbers are:
MUV-43 and the IIPI nozzle on loop A.
82-27 MUV/HP :
Plan to check the other nozzles for nozzle crack cracking as well as repair the known 82-25 RCP A crack before starting up.
Also, a seal package cract was discovered in RCP A seal crack package. The seal will be rebuilt.
l 2
3 4
l' l'ou ed Reason Method:
lixhibit G-Instructions S S beit n!cd A Equipment Failure (Explain) 1 -Manual for Picparation of Data II. Maintenance of Test 2 Manual Scram.
Entry Sheets fot 1.icensee C Itefueling
'3. Automatic Scram.
Event ReporI(1.l R)l'ile tNURI G-D Regulatory Restriction 4.Ot her (lixplain) 0161) i Operator Training & l.icense Examination I.Adnunkirative 5
G Operational I.rror (lixplain)
Exhibit I-Same Source es/77)
I! 01her t hplain)
o MONTHLY OPERATIONAL SU!2iARY STATDIENT DOCKET NO.50-302 UNIT FLCRP-3 DATE 2/1/82 COMPLETED BYM.W. CULVER TELEPHONE'(904) ~i95-6486 MONTH January 1982' SRSIARY STATDIENT:
The init experienced two forced shutdowns and'one power reduction during the raonth.
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