ML20040E600

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IE Insp Repts 50-259/81-32,50-260/81-32 & 50-296/81-32 on 810926-1025.Noncompliance Noted:Notification to NRC by Telephone within 1-h Not Made When Unit 1 Reactor Tripped During Preparation for Turbine Overspeed Trip Test
ML20040E600
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 11/23/1981
From: Cantrell F, Chase J, Paulk G, Sullivan R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20040E585 List:
References
TASK-2.E.4.2, TASK-TM 50-259-81-32, 50-260-81-32, 50-296-81-32, NUDOCS 8202050157
Download: ML20040E600 (11)


See also: IR 05000259/1981032

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

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REGION 11

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101 MARIETTA ST

N.W.. SUITE 3100

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ATLANTA, GEORGIA 30303

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Report Nos. 50-259/81-32, 50-260/81-32 and 50-296/81-32

Licensee: Tennessee Valley Authority

500A Chestnut Street

Chattanooga, TN 37401

Facility Name:

Browns Ferry Nuclear Plant

Docket Nos. 50-259, 50-260, and 50-296

License Nos. DPR-33, DPR-52, and DPR-68

Inspection at Browns Ferry site near Athens, Alabama

Inspectors:

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R. F. Sullivan

Date Signed

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J. W. Chase

Date Signed

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nG. L. Paulk

Date Signed

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Approved by:

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Date ' Signed

F. S. Cantrell, Sectiot) Project Inspection

Resident and Reactor

SUMMARY

Inspection on September 26 - October 25, 1981

Areas Inspected

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This routine inspection involved 326 resident inspector-hours in the areas of-

operational safety, plant physical protection, reactor trips, surveillance

testing, maintenance, training, reportable occurrences, TMI action items,

independent inspection effort, organization changes and respirator protection.

Resul ts

Of the eleven areas inspected, no violations or deviations were identified in

eight areas.

Violations were found in three areas; (Violation of 10 CFR ~50

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Appendix B, Criterion V, two examples (Units 1, 2 and 3), paragraphs 8 and 12;

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violation of a Limiting Condition for Operation (Unit 2) paraaraph 5;

Failure to report as required by 10 CFR 50.72 (Unit 1) paragraph 5,

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8202050157 820121

PDR ADOCK 05000259

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DETAILS

1.

Persons Contacted

Licensee Employees

G. T. Jones, Power Plant Superintendent

J. R. Bynum, Assistant Power Plant Superintendent

J. R. Pittman, Assistant Power Plant Superintendent

R. T. Smith, Quality Assurance Supervisor

R. G.11etke, Engineering Section Supervisor

A. L. Clement, Chemical Unit Supervisor

D. C.111ms, Engineering and Test Unit Supervisor

A. L. Burnette, Operations Supervisor

R. Hunkapillar, Operations Section Supervisor

T. L. Chinn, Plant Compliance Supervisor

11. W. Haney, Mechanical Maintenance Section Supervisor

J. A. Teague, Electrical Maintenance Section Supervisor

R. E. Burns, Instrument Maintenance Section Supervisor

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J. E. Swindell, Field Services Supervisor

A. W. Sorrell, Supervisor, Radiation Control Unit BFN

R. E. Jackson, Chief Public Safety

R. Cole, QA Site Representative Office of Power

Other licensee employees contacted included licensed senior reactor

operators and reactor operators, auxiliary operators, craftsmen,

technicians, public safety officers, QA, QC and engineering personnel.

2.

Management Interviews

Management interviews were conducted on October 2, 9,16 and 23,1981, with

the Power Plant Superintendent and/or his Assistant Power Plant Super-

intendents and other members of his staff. The inspectors summarized the

scope and findings of their inspection activities. The licensee was

informed of four apparent violations identified during the report period.

No dissenting comments were received from the licensee concerning these

violations.

3.

Licensee Action on Previous Inspection Findings

Not inspected.

4.

Unresolved Items

Unresolved items are matters about which more information is required to

determine whether they are acceptable or may involve violations or

deviations. New unresolved items identified during this inspection are

discussed in paragraphs 8, 12 and 13.

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5.

Operational Safety

The inspectors kept informed on a daily basis of the overall plant status

and any significant safety matters related to plant operations.

Daily

discussions were held each morning with plant management and various members

of the plant operating staff.

The inspectors made frequent visits to the control room such that each was

visited at least daily when an inspector was on site.

Observations included

instrument readings, setpoints and recordings; status of operating systems;

status and alignments of emergency standby systems; purpose of temporary

tags on equipment controls and switches; annunciator alarms; adherence to

procedures; adherence to limiting conditions for operations; temporary

alterations in effect; daily journals and data sheet entries; and control

room manning.

This inspection activity also included numerous informal

discussions with operators and their supervisors.

General plant tours were conducted on at least a weekly basis.

Portions of

the turbine building, each reactor building and outside areas were visited.

Observations included valve positions and system alignment; snubber and

hanger conditions; instrument readings; housekeeping; radiation area

controls; tag controls on equipment; work activities in progress; vital area

controls; personnel badging, personnel search and escort; and vehicle search

and escort.

Infomal discussions were held with selected plant personnel in

their functional areas during these tours.

In addition a complete walkdown,

which included valve alignment, instrument alignment, and switch positions,

was performed on the Nuclear Instrument System and the Containment

Atmosphere Dilution System (CAD). These walkdowns were performed on Unit 1

just prior to startup from an extended refueling and modification outage.

No discrepancies were observed.

During the inspector's review of TRs, it was noted that TR-236278, performed

on September 1,1981, required the removal of Flow Indicator Controller

(FIC)71-36A [ Reactor Core Isolation Cooling (RCIC)] from service for

cali bra tion.

An inspection of this TR by the resident inspectors revealed

that removal of the FIC-36A for calibration rendered the RCIC system

inoperable for automatic operation.

Even though the flow controller was

only out of the system for approximately ten minutes, no provisions were

made by operations personnel on shift to manually start the system if needed

or to test HPCIS as required by the technical specifications.

This

oversight resulted because operations personnel did not recognize the system

was inoperable when the flow controller was removed.

In addition, an

evaluation made by the Mechanical Maintenance Supervisor as to whether this

event was reportable to the NRC did not reveal that the RCIC was inoperable

so no thirty-day report was made as required by Technical Specification 6.7.2.b.(2).

On October 9,1981, the resident inspectors informed the Plant Superin-

tendent that failure to recognize that the RCIC system was inoperable and

take appropriate corrective action to satisfy a limiting condition for

operation was an apparent violation of Technical Specifution 3.5.F.2 which

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requires HPCIS to be demonstrated operable if the RCICS is inoperable.

(260/81-32-01).

During a routine tour of the reactor building, which is classified as a

regula'ted area, the inspectors noted three out of three craftsmen obtaining

drinking water from a water cooler without frisking as required by the

posted instructions.

1e inspectors contacted a Health Physics (HP)

supervisor and requested that he observe with the inspector the water

cooler.

During the time interval that the HP sapervisor and inspectors

observed the water cooler, two out of four personnel 'obtained drinking water

without frisking.

On October 23, 1981, the Plant Superintendent was infonned that ebtaining

drinking water from water coolers in regulated areas without frisking was an

open item (259/81-32-08) and drew attention to che past NRC HP reports which

reconniended that drinking from water coolers and smoking in regulated areas

not be allowed.

The Plant Superintendent stated that this recommendation was

currently being studied by TVA.

There was a trip of Unit 1 on October 1,1981, in which the staff failed to

notify the NRC by telephone within one hour as required by 10 CFR 50.72. The

cause was an oversight by the operating crew. The licensee was notified on

October 2,1981, that failure to make the telephone report was an apparent

violation (259/81-32-01).

6.

Reportable Occurrences

The below listed licensee event reports (LERs) were reviewed to determine if

the information provided met NRC reporting requirements.

Th3 determination

included adequacy of event description and corrective action taken or

planned, existence of potential generic problems and the relative safety

significance of each event.

Additional in plant reviews and discussion with

plant personnel as appropriate were conducted far tcose indicated by an

asterisk.

LER No.

Date

Event

259/81-39

7/3/81

Inverter for alann panel XA-55-8E

inoperable

259/81-51

9/8/81

Turbine builuing ventilation exhaust

radition monitor inoperable

259/81-53

9/8/81

RHR valve FCV-74-66 inoperable

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  • 259/81-50

9/3/81

Secondary containment emergency bypass

switch misused causing secondary

containment breaching

  • 259/81-47

8/22/81

A2 RHRSW pump air relief valve failed to

seal flooding RHRSW pump room "A"

260/81-44

9/13/81

H202 analyzer B sample pump inoperable

  • 296/81-47

9/7/81

RHR system II valve FCV-74-75 inoperable

296/81-39

8/17/81

Turbine 1st stage permissive switch

PS-1-81-A out of specification

  • 296/81-46

9/5/81

3EA reactor motor operated valve board

MG set coupling failure

296/81-48

9/8/81

Torus temperature indicator TI-64-55A

inoperable

In the areas inspected no deviations or violations were identified.

7.

Surveillance Testing Observation

The inspectors observed the performance of the below listed surveillance

procedures. The inspection consisted of a review of the procedure for

technical adequacy, conformance to technical specifications, verification of

test instrument calibration, observation on the conduct of the test, removal

from service and return to service of the system and a review of test data.

Surveillance Instruction (SI) 4.4.A.1

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In the above area, no violations or deviations were observed.

8.

Maintenance Observation

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During this report period, the inspectors observed the below listed

maint.' nance activities for procedure adequacy, adherence to procedure,

Technical Specification, radiological controls, Quality Co.ntrol hold points

.and posting of-tagouts.

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a.

flechanical flaintenance Instruction - 15.2.2B Leak Test and Repair of

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HPCI Lube Oil Cooler

b.

~llechanical flaintenance Instruction - 23 Change Out of Oil HPCI.

c.

Instrument flaintenance Instruction - 92.1 Power Range Neutron

lionitoring System

d.

Trouble Report (TR) - 241667, 241486 H2-02 Sample Pump Troubleshoot and

Repair.

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The inspectors also reviewed the use of emergency TRs. The N-0QAM Part II

Section 2.1 states that the plant QA Staff shall review itR's and TR's prior

to performance of the work to assure format, content and QC inspection hold

points comply with plant quality assurance requirements.

It further states

that during off-shifts, holidays, or other times when QA is not available,

the QA Staff review for i1R's/TR's may be performed by the SE or STA.

The

licensee could not produce any instructions, procedures or training docu-

mentation which instructed the SE's and STA's in how to perform this review

for the QA Staff. The only training they receive is that given in General

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Employee Training.

On October 16, 1981, the inspectors identified to the Plant Superintendent

that failure to provide training and instructions to the SE's and STA's in

how to ;arform a QA Staff review of emergency TR's and i1R's was an apparent

violation of 10 CFR 50 Appendix B Criter Mn V which requires that activities

affecting quality shall be prescribed by uocumented' instructions or

procedures of a type appro riate to the circumstances.

(259/81-32-02,

260/81-32-03, 296/81-32-01 .

During-this inspection the inspector held numerous discussions with the

Plant Superintendent and members of his staff discussing the use of

emergency Trs. The N-0QAM defines emergency condition as "... normally

those that require action to place the plant in a safe configuration, to

prevent loss of power generation, to remove the plant from a limiting

condition for operation, or to correct serious personnel safety hazards."

If the SE declared a item of work an emergency condition, then the SE was

authorized to perfonn the QA review of the TR or MR if QA was not available.

The inspector questioned whether to prevent loss of power generation or to

remove the plant from a limiting condition for operation were emergencies

which justified bypassing the normal QA review of TRs or MRs prior to work.

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On 10-16-81, the inspector identified the definition of emergency as defined

in the N0QAM as an unresolved item to the Plant Superintendent. The

inspector stated that he has requested Region II to evaluate this item.

The

licensee stated that power generation is the primary objective of the plant

and hence anything which would disrupt its goal was an emergeacy.

(259/81-32-03).

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9.

Plant Physical Protection

During the course of routine inspection activities, the inspectors made

observations of certain plant physical protection activities. These

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included personnel badging, personnel search and escort, vehicle search and

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escort, communications and vital area access control.

No violations or deviations were identified within the areas inspected.

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10. Tlil Action Items

The following Tfil action item was reviewed by the inspectors during this

report period:

II.E.4.2.(1)-(4)ContainmentIsolation

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The status of this item was reviewed on February 19-20, 1980 by staff

personnel from flRR who visited the site and were accompanied by the resident

inspectors.

The results of this review were reported by letter, 2/29/80, to

TVA from T. A. Ippolito, flRR, which confirmed that the system had been

evaluated as required by the action item and that certain modifications had

been made to prevent inadvertent re-opening of isolation valves. On certain

valves which normally remained closed, TVA had modified the controls for

ganged reset which was questioned by the NRC staff as providing sufficient

assurance to prevent inadvertent opening. TVA subsequently agreed to

further modify the controls for individual valve resetting.

The inspectors verified that the additional design changes were completed on

all three Units according to approved work plans (WP) as follows:

Unit 1

9/14/81

WP-6434

Unit 2

11/12/80

WP-9857

Unit 3

1/4/81

WP-7804

The inspectors consider this item closed.

11.

Reactor Trips

The inspectors reviewed activities associated with the below listed reactor

trips during this report period.

The review included determination of

cause, safety significance, performance of personnel and systems, and

corrective action. The inspectors examined instrument recordings, computer

printouts, operations journal entries, scram reports and had discussions

with operations, maintenance and engineering support personnel as

appropriate,

a.

On October 1,1981, Unit 1 scrammed from 616 MWt caused by the ilSIVs

isolating on a main steam line low header pressure.

The cause of the

low pressure was attributed to having too many bypass valves open in

preparation for turbine overspeed testing.

No relief valves operated.

HPCIS and RCIC were initiated manually to control water level.

Plant

safety systems performed satisfactorily.

b.

On October 3,1981, Unit 1 scrammed from 325 f1We on receiving a low

vacuum signal from the main condensor.

The cause of the low vacuum was

the result of inleakage of air to the 1B1 high pressure heater while

attempting to drain the heater.

No relief valves operated, nor did any

emergency core cooling systems initiate.

Safety systems performed

satisfactorily.

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c.

On October 5,1981, Unit 1 scrammed fror; 316 ftWe on receiving a low

reactor water level signal. The cause of the low reactor water level

was due to the short cycle valve inadvertantly opening, while instru-

ment mechanics were removing test equipment, causing a partial loss of

feedwa ter. fio relief valves actuated and no emergency core cooling

systems actuated.

Safety systems performed satisfactorily.

d.

On October 12, 1981, Unit I was removed from service by performing a

manual scram.

The shutdown was to perfom required maintenance on a

loose backing plate on #1 generator. fio emergency core cooling systems

actuated and no relief valves operated.

Safety systems perfomed

sa tisfactorily.

Within the areas inspected no deviations or violations were identified.

12.

Independent Inspection Effort

During this report period, the inspectors performed a review of surveys

being performed by the QC organization.

It was determined that approxi-

mately 50% of the surveys scheduled for April - September 1981 had not been

performed.

Typical examples of surveys scheduled but not performed were:

Title

fiumber

Frequency

last performed

Use of Radiation

HP-15

Weekly

July 24, 1981

flonitor

(f4RC commitment)

Radioactive

HP-1

Bimonthly

May 13, 1981

Waste Management

Plant Security

S-3

fionthly

July 4, 1981

Fire Hose Reel,

SA-3

lionthly

July 16, 1981

Cart and Hose

Inspection

Radiochemical

CR-1

Monthly

July 16, 1981

Lab flanual

Material Handling

P-1

Bimonthly

June 18, 1981

and Storage

QA Records

DC-lb

Semi-Annually

April 3, 1980

Management

Health Physics

On October 16,1981, the Plant Superintendent was informed that failure to

perform QC surveys as scheduled by Section Instruction Letter - S.1, was an

apparent violation of 10 CFR 50 Appendix B, Criterion V which requires that

activities affecting quality be prescribed by instructions or procedures and

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shall be accomplished in accordance with these instructions or procedures.

(81-32/259-04,81-32/260-04,81-32/296-02).

Other independent inspection efforts was an inspection of drywell electrical

penetrations as outlined in Electrical Maintenance Instruction EMI-51. The

ir.spectors noted that the nitrogen charge on 20% (4 out of 20) of the

penetrations checked were below the minimum acceptable value stated in

EMI-51. The quarterly inspection required by EMI-51 had not been performed

in September 1981 as scheduled because of a lack of an operating Bechman

Trace Moisture Analyzer needed for checking nitrogen moisture content prior

to penetration purging and charging.

Action has been taken by the licensee

to obtain an operable analyzer to complete the quarterly maintenance. This

item will remain open and followed up on future inspections (259/81-32-05).

During the review of records for EMI-51, the inspectors found the latest

record held of EMI-51 by plant document control was for maintenance done in

June, 1980.

The inspector located maintenance records for dates after June,

1980 in the QA office waiting for QA supervison review.

Additionally,

approximately 200 other maintenance records were stacked in the QA office

awaiting the review cycle. The majority of unreviewed records indicated

work had been completed 6-15 months previously. This item will remain

unresolved (259/81-32-06).

13.

Respiratory Protection Program

The inspectors conducted an inspection during the weeks of October 12 and

October 19, 1981 of the radiation protection operation to determine

compliance with regulatory protection. Areas reviewed included medical

status of respirator users, individual fitting of respirator training,

maintenance of respiratory protective equipment, operational and admini-

strative control of the respiratory protection program and the selection and

use of respirators.

The inspectors conducted the inspection in accordance with requirements of

10 CFR 20.103(c), Regulatory Guide 8.15 and Browns Ferry Radiological

Control Instruction 3.

The inspectors attended the mask fit training for

new employees and the biannual health physics requalification training

during this inspection.

Regulatory Guide 8.15 requires that respiratory particulate recycled filters

be used within the limitations for type and mode of use.

Additionally, a

quality assurance program should be established to ensure reused filters

meet the requirements for efficiency and resistance to breathing specified

for unused filters. Guidance for a quality assurance program is outlined in

NUREG 41.

The inspector found that no quality assurance program existed and

that particulate filters are routinely reused without efficiency or

resistance checks.

Similar concerns were identified during the licensee

radiological hygiene quality assurance inspection of October 2,1981.

The

licensee is taking action to correct this program deficiency, therefore,

this item will remain an unresolved item (259/81-32-07).

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No violations were identified in the areas inspected.

14. Training

During this report period the inspectors attended the Health Physics and

Security retraining program which is required of each employee every two

years. The inspectors held discussions with the instructors and various

personnel on site to determine their level of knowledge in the two areas

already mentioned. The inspectors determined that the training was adequate

and met or exceeded the minimum requirements.

Discussions with the Health

Physics instructor revealed that the initial training program is being

re-organized to develop a more hands on approach to training, such as

actually dressing out in contamination clothing.

In the above area no violations or deviations were identified.

15.

Organization Changes

Recent changes in the Browns Ferry organization have been made as follows:

On October 5,1981, H. L. Abercrombie, Plant Superintendent, was promoted

within the Nuclear Power Division and was transferred to the Chattanooga

Office.

On October 5,1981, G. T. Jones, was assigned the Plant Superintendent

position. . Mr. Jones had previously been the Assistant Branch Chief of .the

Outage Management Branch.

On October 2,1981, J. L. Harness, Assistant Plant Superintendent -

Maintenance, terminated employment with TVA.

On September 28, 1981, J. R. Pittman, Instrument Maintenance Supervisor, was

promoted to Assistant Plant Superintendent - Maintenance.

On September 28, 1981, R. E. Burns, Lead Instrument Engineer, was promoted

to Instrument Maintenance Supervisor.

On January 11, 1981, J. R. Bynum, who was an Assistant Plant Superintendent

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at Sequoyah was transferred to Browns Ferry as the Assistant Plant

Superintendent-Operations and Engineering

A third Assistant Plant Superintendent position has been authorized but not

yet filled.

The inspectors reviewed the qualifications of the above personnel for

conformance to the minimum acceptable levels as described in ANSI-18.1,

Selection and Training of Nuclear Power Plant Personnel, dated March 8,

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1971, which is a technical specification requirement.

The inspectors

confirmed that qualification requirements were met with one possible

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exception; that being whether one of the personnel in the position of Plant

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Superintendent or Assistant Plant Superintendent, had the necessary training

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to be eligible for the NRC examination for Senior Reactor Operator (SRO).

TVA made the determination that Mr. Bynum satisfied the SR0 equivalency

requirements.

Further review of this matter was requested of the

IE Regional office where it was determined that Mr. Bynum satisfied the

quaification requirements of ANSI 18.1.

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