ML20040A555

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Monthly Operating Rept for Dec 1981
ML20040A555
Person / Time
Site: Crystal River 
Issue date: 01/05/1982
From: Culver N
FLORIDA POWER CORP.
To:
Shared Package
ML20040A553 List:
References
NUDOCS 8201210239
Download: ML20040A555 (4)


Text

-.

1 OPERATING DATA REPORT DOCKET NO.

50-302 DATE 1/5/82 COh!PLETED BY Mu culver

)

TELEPHONE.19041 795-6486 OPERATING STATUS i

Notes

1. Unit Name:

crue n t River Unit 3

2. Reporting Period:

12/1/81 - 12/31/81

3. Licensed Thermal Power (51Wt):

7544

4. Nameplate Rating (Gross 51We):

890

5. Design Electrical Rating (Net 31We):

825

6. 51asimum Dependable Capacity (Gross 51We):

R?1

7. Sf aximum Dependable Capacity (Net 31We):

782 S. If Changes Occur in Capacity Ratings (items Number 3 Through 7) Since Last Report.Give Reasons:

li3 - From 2452 to 2544 because of power level upgrade.

  1. 6 and #7 will be changed after operational data at this level has been gathered.
9. Power Lesel To Which Restricted. If Any (Net 51Wel:

Nona

10. Reasons For Restrictions,l.f Any:

N/A This hionth Yr. to-Date Cumulatise

11. Hours in Reporting Period 744 8760_

42120

12. Number Of Hours Reactor Was Critical 485.83 5564.88 25449.39
13. Reactor Resene Shutdown Hours 0

80.0 1209.22 1

14. Hours Generator On.Line 423.7 5446.8 24812.18
15. Unit Resene Shutdown Hours 0

0 0

16. Gross Thermal Energy Generated (51WH) 905638 2083927 55366941 17 Gross Electrical Energy Generated (SIWH) 311171 4295660 18799591 lb. Net Electrical Energy Generated (51WH) 294859 4083728 17829298
19. Unit Senice Factor 56.9%

62.2%

58.9%

20. Unit Asailability Factor 56.9%

62.2%

58.9%

21. Unit Capacity Factor (Using 51DC Net) 50.7%

59.6%

54.1%

22. Umt Capacity Factor (U>ing DER Net) 48.0%

56.5%

51.3%

23. Unit F or ed Outage Rate 6.6%

16.6%

26.6%

24. Shutdowns Scheduled Oser Next 6 51onths (Type.Date,and Duration of Each):

N/A

25. If Shut Down At End Of Report Period. Estimated Date of Startup:

N/A

26. Umts In Test Status tPrior to Commercial Operation).

Forecast Achies ed INITI A L CRITICALITY 1/14/77 INITi \\L ELECTRICITY 1/30/77 CO\\l\\lERCI AL OPER ATION 3/13/77 8201210 M i

,o

AVER AGE DAILY UNIT POWER LEVEL DOCKET NO.

50-302 UNIT FLCRP-3 DATE 1/5/82 COMPLETED BY M W-Culver TELEPHONE (904).795-6486 MONTH December 1981 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL Of We-Net )

(Mwe.Ne:3 1

0 17 630 761 2

0 jg 3

0 19 819 4

0 70 844 832 5

0 7,

0 6

22

'10 1 7

0 23 588 0

827 8

74 9

0 25 837 0

526 10 26 0

II 27 575 12 0

835 33 254 13 29 838 14 296 30 nA3 302 i

15 31 835 16 541 INSTRUCTIONS j

j On this format. :st the.

.ih usut p.,u er lese: in ilm.Nei for each day in the reporting in inth. C. impute to the nearest wh >k mcy.,

i F1/77 I i

I 1

[.

s

...,,7...4-.~,---~.3

p ItNII SIftlil OWNS AND POWER RI DilrilONs DOCKEINO.40-302 UNII N AME FTrup t i

DA II.

4 /S/p?

j COMPLETED HY - M t.r c,,1 uo r Hl POR T ?.f 0 Nill 12/81 IELErilONE (904) 795-6486 i

l f7 l.!

5?

' i-dE I stenste pt, t

C.mw & rorreceive

s.,

n*

i 5=

4

.3 :; a r.ze ni p

g ao,.,n in g

Repor: -

uN o'

Pecsent Returrence j

fE y

3 g =g u

w C

81-51 811201 S

290.23 C

1 N/A.

ZZ ZZZZZZ Continuation of scheduled refueling i

outage.

81-52 811222 F

17.6 A

3 N/A IA INSTRU While reducing power to take the turbine off-line, the pump power monitor tripped the unit when the 6900 volt buses were swapped.

i 81-53 811226 F

12.4 A

3 N/A IA INSTRU An upset in the electrical trans-mission system caused the pump power monitor to trip the unit.

I 2

3 4

I : Foried Reason -

Methmi:

Exhibit G - Instructions A li nipment Failure (Esplain)

1. Manual for Preparation of Data N Si hninic(I i

li Maintenance of Test 2.Mannal Scram.

Entry Sheets for 1.icensee U.itefucting -

'3. Automatic Scram.

Event Report II.1:R) File INtlRI G.

D. Regulatory Restriction 4-Ot her (lixplain) 0161) 1 Operator Training & Ucense 1% amination I' Administrative 5

G-Operational 1:r ror ( E xplain)

I'.shibit I - Same Source cr!77)

I! Other (1%plaini A

~

._,..=-,., -.

--,...-.........- ~. -. _.. -. =.

l MONTHLY OPERATIONAL

SUMMARY

STATDENT DOCKET NO. 50-302 UNIT FLCRP-3 DATE 1/8/82 COMPLETED BY M.W. Culver TELEPHONE (904) 795-6486 MONTH December 1981

SUMMARY

STATDENT:

The Unit suffered two trips after returning to power from a refueling outage on December 13.

O D

e l

.